ML20085D292
ML20085D292 | |
Person / Time | |
---|---|
Site: | Robinson |
Issue date: | 12/01/1972 |
From: | CAROLINA POWER & LIGHT CO. |
To: | |
Shared Package | |
ML20085D289 | List: |
References | |
NUDOCS 8307210105 | |
Download: ML20085D292 (11) | |
Text
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H. B. ROBIUSON SEG PLAliT Robinson File No. 2-0-9-a .
STEAM GENERATOR PRESSL9.S TEST December 1, 1972
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., y Recc=end Approval e . h2< ,_ ,
h rd. Date: /3-S -73 Operating Shpervi::or l'
Approved A '. M' Date: M-k-
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9307210105 730129
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H. B. ROBINSON STEAM ELECTRIC PIAiT
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STEAM GENERATOR PRESSURE TEST 1
December 1,1972 Robinson File No. 2-0-9-a jd-J -71 Date of Test OBJECTIVE
,1. Establish a 1900 psi differential pressure between the primary and secondary systems for purpose of a pressure test.
INITI AL CONDITIONS
- 1. Reactor is in hot shutdown condition with reactor coolant pumps running
. as required.
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- 2. All control and shutdown rods are inserted. 9/
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- 3. Pressurizer heaters are in " auto" control. M f
- 4. Pressurizer power operated relief valves are set up for normal operation. M f
S. Pressurizer continuous spray valves are ','open" and pressurizer control spray valves are in " auto" control. M
- 6. Reactor makeup in " auto" control with boron adjusted to
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makeup at reactor coolant system concentration. M f
- 7. Letdown is maxicum for purification of the primary system i) water. ,
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, Steam Generator Pressure Test Cont'd. December 1, 1972 s
- 8. One charging pump is in " auto" control.
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- 9. heenmdumpsystemisbeingutilizedtomaintainthehot shutdown condition.
Id.' Steam generator isolation valves are open. hb
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- 12. Primary coolant has been sampled for iodine and tritium, and leak rate of each S/G has been determined. M f
PPICAUTIONS
- 1. Primary system pressure should not exceed the normal operating pressure of 2235 psig.
- 2. Calibrated gauges are to be utilized on the primary and secondary system to determine pressure.
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- 3. Only authorized personnel are to be allowed inside the
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containment vesscl.
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- 4. Insure a positive labyrinth seal as required for the reactor ecolant pumps. "
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- 5. The limitation of a 200 F delta temperature between the pressurizer and the primary system is not applicable (Permanent change) . ,
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- .O-Steam Generacor Pressure Test Cont'd. December 1, 1972 1
- 6. If test exceeds seventeen hours duration it will be necessary to compensate with boron addition for Xe decay to maintain shutdown margin. )h5 7 . Do not exceed a cooldown or heatup rate of 50 F. per hour.
- 8. During cooldown, monitor nuclear instrumentation and plot a 1/H curve.
- 9. Do not utilize the secondary system power operated relief valves unless it becomes necessary to prevent the safetics from lifting.
- 10. Sample and determine boron concentration of the primary system at .
30 minute intervals or as requested by the shift foreman.
- 11. Pressurizer sprays should not be used if the spray fluid is more than 320 F below the pressurizer temperature.
- 12. All normal precautions for cooldown and heatup remain in effect unless specifically altered by this procedure.
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-h-INSTRUCTIONS 1 i
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- 1. Borate to the bcron concentration as specified in the attached shutdown margin calculations for the test period. Shu+.dewn margin calculated for
- 17. shutdown at 2000F.
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- 2. Begin cooldewn from hot shutdown conditions utilizing the turbine and/or condenser steam dumps to dissipate energy. Pressurizer autonatic systems should r: air.tain no load level and pressure in the pressurizer. Do not exceed a cooldown rate of 50 F / hour._
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- 3. When Tavg decreases to $h3 F. go to the "37 pass Tavg Interlock" position on the steam dunp centrols.
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- h. Block the High Steam Flow, Low Steam Pressure / Low Tavg safety injection signal at Tavg of 5h3 F.
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- 5. Continue cooldown until a differential pressure of 1900 psi exists between the primary syste:n (primary system pressure deterained by PI LOh & h05) and the secondary syste t (secondary pressure determined from test gauges on the three steam lines).
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M NOTE: Insure that a 1900 psi differential does exist. Secondary pressure indication shculd be 33h psig with primary pressure at 2235 psig.
- 6. Maintain the required pressure differential until the data required on the attached data sheet is obtained.
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s-Instructions Cont'd. December 1, 1972 1
- 7. If no primary to secondary leakage is detected as indicated by an increase in stean generat b levels, return the systen to normal .
operating pressure and begin nomal heatup of the prinary system
, as per GP-1.
NOTE: Refer to precaution number 6. %[
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- 8. Determines /Gleakage. N ,,/98ggh
- 9. Return to cr'.tical operation if S/G leakage is less than 0.3 gpm total.
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- 10. Return to power operatien as per GP-1. h 6
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- 6-Pressure Recuirements s r
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Prima:7 systen pressure 2235 psig ,
t Required differential 1900 psig Corrected secondar/ pressure 335 psig Correction for friction losses -10 psig s
Correction for head icssas on test gauges +9.0 psig Total corrections -1 psig To insure 1900 psig differential require secondary pressure of 33h psig on the secondarf systen test gauges.
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Shutdown Marcin i
h5 Rods In Worth (Cold SD Worth = 78% Hot Worth) -6100 pcm ,
Power Defect and Rod Bite +2558 pcm Temperature Defect (5h7-200 F) +5600 pcm I' e buildup after 2 hrs. -1000 pcm 1% SD Margin +1000 pen Required Boration +2058 pcm Add boron to obtain a concentration &f 250 opn (Borenworth1hpen/ ppm)
S.D. Margin valid between two and seventeen hours after shutdown. After 17 hours1.967593e-4 days <br />0.00472 hours <br />2.810847e-5 weeks <br />6.4685e-6 months <br /> add boron to co.,pensate for I e decay.
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I Primary to Seconddrr Lea'< ace Data Sheet -
ICDIt!E - 131 'fRITIU'8 LEAK RATE TDE/DATE Before Test -
RCS II/tB/12 j. +7yit['n},/,g 9]ffIo
~" ~' O < 08 c, S{G - A it/3clst. .921x 10 or/i/p 6.lfXto I 'Z.- I - 11.
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~b igjij,, t. 91/10 o.O& l 2 -/~1 L F. W. i.o s tio'5 O.Wcb 17 -/- 7%
O' After Test
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After Return to Fewar
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Steam Generator Pressure Test Data
- s Time: O 3 > 2 ///5 Dite: >>-J-73 Primary System Pressure:
PI hoh 3 2 6 f- psig PI h05 J.2 4 8 psig Average $266 psig Correction for elevation head -#3 psi Corrected Prinary System Pressure -23 4-7 psi Secondary System Pressure:
Test Gauge Stean Line "A" 31 P psig Test Gauge Steam Line "B" 32.2 psig Test Gauge Steam Line "C" 32 6 psig Average 3,~)),6 /. psig Pressure Differential:
Primary System Average A2//- 3 psig
- Secondary System Average 3.:2 f,6 ( psig Differential fk21,y4- psi
- Friction Losses fron S/G
- 1G psi Differential (Friction loss Corrected) 1 9/f,~4 4 psi
+ Pressure. Head from steam lines .
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, . ,. , 9,9 . . pgg, Corrected Differential Pressure /9 2 n g psi )
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};acu&..:;.*/...jLossesfromS/G'stopressuregaugelines,
- ' 20.5 ft, elevation difference resulting in 9 0 psi.
"f l Data Collected By: '# M~ 'Mv / z 72.
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l Trimary Systen Data 1
Identity Cc= uter Address Value O
RCS Loop "A" Hot Log Temperature T0h19A Y33d RCS Loop "A" Cold Leg Temperature T0h06A 433,d7 RCS Loop "3" Hot Leg Temperature T0h39A 433 /
{ RCS Loop "B" Cold Leg Tenperature T0h26A 43.2,7 i .
RCS Loop "C" Hot Leg Tenperature ?]h59A -I-3),8 RCS Loop "C" Cold Leg Tenperatu'e T0hh6A 437,2-Pressurizer H O 2 Temperature T0h20A dM,I Pressurizer Stea Temperature T0h81A / 27[
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i j Data Co11ceted By: Date:
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