ML20085D292

From kanterella
Jump to navigation Jump to search
Steam Generator Pressure Test
ML20085D292
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 12/01/1972
From:
CAROLINA POWER & LIGHT CO.
To:
Shared Package
ML20085D289 List:
References
NUDOCS 8307210105
Download: ML20085D292 (11)


Text

. .

. i

_ _o. o I t

H. B. ROBIUSON SEG PLAliT Robinson File No. 2-0-9-a .

STEAM GENERATOR PRESSL9.S TEST December 1, 1972

i

'. l

., y Recc=end Approval e . h2< ,_ ,

h rd. Date: /3-S -73 Operating Shpervi::or l'

Approved A '. M' Date: M-k-

~

P1glerdger lI .

9307210105 730129

. PDR ADOCK 05000261 p PDR ,

i ss. -e *y o ,_

1-.., ., . . - . . . , - , -. -. - ..

~

. . 0- o i

./

H. B. ROBINSON STEAM ELECTRIC PIAiT

/

STEAM GENERATOR PRESSURE TEST 1

December 1,1972 Robinson File No. 2-0-9-a jd-J -71 Date of Test OBJECTIVE

,1. Establish a 1900 psi differential pressure between the primary and secondary systems for purpose of a pressure test.

INITI AL CONDITIONS

1. Reactor is in hot shutdown condition with reactor coolant pumps running

. as required.

r

2. All control and shutdown rods are inserted. 9/

f

3. Pressurizer heaters are in " auto" control. M f
4. Pressurizer power operated relief valves are set up for normal operation. M f

S. Pressurizer continuous spray valves are ','open" and pressurizer control spray valves are in " auto" control. M

6. Reactor makeup in " auto" control with boron adjusted to

/

makeup at reactor coolant system concentration. M f

7. Letdown is maxicum for purification of the primary system i) water. ,

r M

r.

L k A

_f

, Steam Generator Pressure Test Cont'd. December 1, 1972 s

8. One charging pump is in " auto" control.

f .

9. heenmdumpsystemisbeingutilizedtomaintainthehot shutdown condition.

Id.' Steam generator isolation valves are open. hb

/

11. Feedwater is being supplied through the feedwater bypass valves.
12. Primary coolant has been sampled for iodine and tritium, and leak rate of each S/G has been determined. M f

PPICAUTIONS

1. Primary system pressure should not exceed the normal operating pressure of 2235 psig.
2. Calibrated gauges are to be utilized on the primary and secondary system to determine pressure.

~

3. Only authorized personnel are to be allowed inside the

/

containment vesscl.

f

4. Insure a positive labyrinth seal as required for the reactor ecolant pumps. "

^

5. The limitation of a 200 F delta temperature between the pressurizer and the primary system is not applicable (Permanent change) . ,

l .

f

_ _ ~

~

, t o

- .O-Steam Generacor Pressure Test Cont'd. December 1, 1972 1

6. If test exceeds seventeen hours duration it will be necessary to compensate with boron addition for Xe decay to maintain shutdown margin. )h5 7 . Do not exceed a cooldown or heatup rate of 50 F. per hour.
8. During cooldown, monitor nuclear instrumentation and plot a 1/H curve.
9. Do not utilize the secondary system power operated relief valves unless it becomes necessary to prevent the safetics from lifting.
10. Sample and determine boron concentration of the primary system at .

30 minute intervals or as requested by the shift foreman.

11. Pressurizer sprays should not be used if the spray fluid is more than 320 F below the pressurizer temperature.
12. All normal precautions for cooldown and heatup remain in effect unless specifically altered by this procedure.

l l

l l* l 8

l

-- .y-. , -. # -._ ,~_, . . . , . . , , , _ _c., y e- -rt r--

(7. p)

  • s L

-h-INSTRUCTIONS 1 i

\

1. Borate to the bcron concentration as specified in the attached shutdown margin calculations for the test period. Shu+.dewn margin calculated for
17. shutdown at 2000F.

.. /

2. Begin cooldewn from hot shutdown conditions utilizing the turbine and/or condenser steam dumps to dissipate energy. Pressurizer autonatic systems should r: air.tain no load level and pressure in the pressurizer. Do not exceed a cooldown rate of 50 F / hour._

7-

3. When Tavg decreases to $h3 F. go to the "37 pass Tavg Interlock" position on the steam dunp centrols.

/

h. Block the High Steam Flow, Low Steam Pressure / Low Tavg safety injection signal at Tavg of 5h3 F.

/

M

5. Continue cooldown until a differential pressure of 1900 psi exists between the primary syste:n (primary system pressure deterained by PI LOh & h05) and the secondary syste t (secondary pressure determined from test gauges on the three steam lines).

/

M NOTE: Insure that a 1900 psi differential does exist. Secondary pressure indication shculd be 33h psig with primary pressure at 2235 psig.

6. Maintain the required pressure differential until the data required on the attached data sheet is obtained.

r h

1 e

. . - ~ , - - e .e. _, e

s-Instructions Cont'd. December 1, 1972 1

7. If no primary to secondary leakage is detected as indicated by an increase in stean generat b levels, return the systen to normal .

operating pressure and begin nomal heatup of the prinary system

, as per GP-1.

NOTE: Refer to precaution number 6.  %[

f

8. Determines /Gleakage. N ,,/98ggh
9. Return to cr'.tical operation if S/G leakage is less than 0.3 gpm total.

h'

( (I

10. Return to power operatien as per GP-1. h 6

0 t

k i

e e 6

u. .

- 6-Pressure Recuirements s r

\

)

Prima:7 systen pressure 2235 psig ,

t Required differential 1900 psig Corrected secondar/ pressure 335 psig Correction for friction losses -10 psig s

Correction for head icssas on test gauges +9.0 psig Total corrections -1 psig To insure 1900 psig differential require secondary pressure of 33h psig on the secondarf systen test gauges.

1 .

a

+

4 A

e f * * . .

1 4.:. .~.v .. a .... : .. . ... r.

. .~ ......

e

f 1

i I- . .

\ .

f _, 8 *

"r. s ** *

  • T.-. .- . ,  ; ,I

.y o i j

Shutdown Marcin i

h5 Rods In Worth (Cold SD Worth = 78% Hot Worth) -6100 pcm ,

Power Defect and Rod Bite +2558 pcm Temperature Defect (5h7-200 F) +5600 pcm I' e buildup after 2 hrs. -1000 pcm 1% SD Margin +1000 pen Required Boration +2058 pcm Add boron to obtain a concentration &f 250 opn (Borenworth1hpen/ ppm)

S.D. Margin valid between two and seventeen hours after shutdown. After 17 hours1.967593e-4 days <br />0.00472 hours <br />2.810847e-5 weeks <br />6.4685e-6 months <br /> add boron to co.,pensate for I e decay.

  • ......t

. * *'. . . . .g : .4...t .. 4,t. ., .,w., ,...,..g . -, .. . ;,. t, ,,,

,,g;,.,,,,,,,.,,,

, ,,,,;.,,.,..,.,g,.,, , ,

t p +.8r rw.i. n.::.v .w ,,. ,..e. g ,.v..e.v .v4.w. . .w.s..e.g.,,.8. w.ye. m...au m a.r.,.n+,e .. ..x...

.a..- . _ .

_Q

I Primary to Seconddrr Lea'< ace Data Sheet -

ICDIt!E - 131 'fRITIU'8 LEAK RATE TDE/DATE Before Test -

RCS II/tB/12 j. +7yit['n},/,g 9]ffIo

~" ~' O < 08 c, S{G - A it/3clst. .921x 10 or/i/p 6.lfXto I 'Z.- I - 11.

B lt/.h/11 759xio tzj,jpg S3Stic o , o 5a,,lff /7.-l-22

~'

C /t/3c/rt f.c ar io

~b igjij,, t. 91/10 o.O& l 2 -/~1 L F. W. i.o s tio'5 O.Wcb 17 -/- 7%

O' After Test

~

P.CS 9.1s x tu /JJVCflifr/7z S/G - A f.c S'y I o '

~

() 615r,s/y PJVS//2/t/yt

<- i B 4,tsyit'S O, esq n pJ, pyr/ ttftl7i

/'

C 9 e 4.sici ' M'+s n], f)1Yf/ n/z,/;z.

d' (

After Return to Fewar

  • ' ~

RCS 1.4 l F16 f.61F/3 2/Jo /n-1-7%

  • I -I S/G - A 1. f t.wia y,3 3ff3 O,,06'7eIh /950//t.-1'7' I

B Soi1* f.ft. y ra $

/75o/I1-1 -nt o.OOLcf

/73* lI t-1 -1' 9.n v16"'

C *

  • / 4 0 /t0" #. 0 0 0 k' es h M

F. W. 1.4 5 *10 ' O.1'2- q;$ jf}v/11-1-it-V 8.?'i r t*

, .. R C ,5 , .

2.32 Vio , ,

/ e.,s -7s 5/<e - A I. 9s Fl* ~ ' n.-r-7 t_

o .o 4,a'1(

M o t J. n.v.so o . I ~1 s 1.-f -~1'l-

y. L w.. m.n +.,n..r .:: :n ... w i. . n.,.,.u. a,. s. .wm ,.

.. , . . . . . . . >.o.e.>.g e......,m. .... n...o. ., u,, c., . g, ,

._ s . . _

,,_y

~

( ... .

o

.o l

i 9- ,

Steam Generator Pressure Test Data

s Time: O 3 > 2 ///5 Dite: >>-J-73 Primary System Pressure:

PI hoh 3 2 6 f- psig PI h05 J.2 4 8 psig Average $266 psig Correction for elevation head -#3 psi Corrected Prinary System Pressure -23 4-7 psi Secondary System Pressure:

Test Gauge Stean Line "A" 31 P psig Test Gauge Steam Line "B" 32.2 psig Test Gauge Steam Line "C" 32 6 psig Average 3,~)),6 /. psig Pressure Differential:

Primary System Average A2//- 3 psig

- Secondary System Average 3.:2 f,6 ( psig Differential fk21,y4- psi

- Friction Losses fron S/G

  • 1G psi Differential (Friction loss Corrected) 1 9/f,~4 4 psi

+ Pressure. Head from steam lines .

  • a -

..gf gggg.ggnge, - .

, . ,. , 9,9 . . pgg, Corrected Differential Pressure /9 2 n g psi )

1

};acu&..:;.*/...jLossesfromS/G'stopressuregaugelines,

    • ' 20.5 ft, elevation difference resulting in 9 0 psi.

"f l Data Collected By: '# M~ 'Mv / z 72.

s

  • ~,. ,. -' ,

a

~

1

. p.

f t  :

1 Q .

i I

l Trimary Systen Data 1

Identity Cc= uter Address Value O

RCS Loop "A" Hot Log Temperature T0h19A Y33d RCS Loop "A" Cold Leg Temperature T0h06A 433,d7 RCS Loop "3" Hot Leg Temperature T0h39A 433 /

{ RCS Loop "B" Cold Leg Tenperature T0h26A 43.2,7 i .

RCS Loop "C" Hot Leg Tenperature  ?]h59A -I-3),8 RCS Loop "C" Cold Leg Tenperatu'e T0hh6A 437,2-Pressurizer H O 2 Temperature T0h20A dM,I Pressurizer Stea Temperature T0h81A / 27[

]

i j Data Co11ceted By: Date:

{,YlO ': t ' l>l '

).2--) - QL 1

I i

l., ,

..x. . ,. . . . ..,.

~ . .. , :.. .; .. .. w .....,..e..

. . . . c. , ..

. . ...,,..y,....

. . .. ....,........,.,..4..

l .

^

G} ;..,:__'Q ':

  • q,; f.s.' :i.,'. l?
  • l[' ' . '- g.' ' '.".;. ','?jh .#,,,
  • g. s ' <' ,;.l.,. ; &[l ' . 1d: . p *. ,., .'; .f q'.,' . .,},; * . }.f*. , .<s;.

., l . . ). .._ . .

,. . - .