ML20054F756

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IE Insp Repts 50-317/82-07 & 50-318/82-07 on 820413-0511. Noncompliance Noted:Failure to Follow Requirements for Tagouts & Failure to Have Operable Hydrogen Analyzer During Cycle 5.Page 6 Withheld (Ref 10CFR73.21)
ML20054F756
Person / Time
Site: Calvert Cliffs  Constellation icon.png
Issue date: 05/18/1982
From: Architzel R, Mccabe E, Trimble D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20054F731 List:
References
50-317-82-07, 50-317-82-7, 50-318-82-07, 50-318-82-7, NUDOCS 8206170290
Download: ML20054F756 (20)


See also: IR 05000317/1982007

Text

DCS 50317 820417

020421

50318 820417

50320 790328

820314

820504

820320

820319

820429

820402

820321

820503

820407

The report details

820316

820328

contain Safeguards Info l

820407

(Page 6 only)

820401

i

U. S. NUCLEAR REGULATORY COMMISSION

THE INFORMATION ON THIS

Region I

PAGE IS DEEMED TO BE

APPROPRIATE FOR PUBLIC

50-317/82-07

DISCLOSURE PURSUANT TO

Report No.

50-318/82-07

10 CFR 73.21

50-317

Docket No.

50-318

DPR-53

C

License No. DPR-69

Priority

--

Category

C

Licensee:

Baltimore Gas and Electric Company

P. O. Box 1475

Baltimore, Maryland 21203

Facility Name: Calvert Cliffs Nuclear Power Plant, Units 1 and 2

Inspection At: Lusby, Maryland

Inspection Conducted: April 13 - May 11,1982

Inspectors:

5~

Z

R~. E. Architze), Senior' Resident Reactor Inspector

date signed

ll

Y 07

b 7s

D.

C~. Trimble, Resid'ent Reactor Inspector

date signed

Approved By:

CO

5'/IB / Tr?.

i

E. C. McCabe, Jr. , Chief, Reactor Projects

date signed

Section 2B

Inspection Sumary:

Inspection on 4/13 - 5/11/82 (Combined Report Nos. 50-317/82-07and50-318/82-07).

Areas Inspected: Routine, onsite regular and backshift inspection by the resident

inspector (119 hours0.00138 days <br />0.0331 hours <br />1.967593e-4 weeks <br />4.52795e-5 months <br />). Areas inspected include the control room and the accessible

portions of the auxiliary, turbine, service, and intake buildings: radiation protection;

physical security; fire protection; plant operating records; plant operations; main-

tenance; radioactive waste releases; open items; TMI Action Plan Items; Containment

Leakage Test requirements; and reports to the NRC.

Violations: Three: Failure to follow requirements for tagouts (detail 9.c), failure

to have operable hydrogen analyzer during Cycle 5 (deta.1 ll.c), and containment

leakage rate greater than allowed (detail 1 ,

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_ DETAILS

1.

Persons Contacted

The following technical and supervisory level personnel were c

entacted:

J. T. Carroll, Ganeral Supervisor, OperationsM. E. Bo

R. E. Denton, General Supervisor, Training / Technical Services

C. L. Dunkerl

W. S. Gibson,y, Shift Supervisor

J. E. Gilbert, Shift SupervisorGeneral Supervisor, Electrical & Controls

A. M. Hetrick, Radiation Safety Enginee,-R. P. Heibel, P

J. R. Hill, shift Supervisor

L. S. Hinkle, Engineering halyst

Electrical & Control Section

J. Lenhart, Radiological Support SupervisorD. W. Latha

e y Unit

J. F. Lohr, Shift Supervisor

G. S. Pavis, Engineer, OperationsR. G. Mathews, Assistant G

J. E. Rivera, Shift Supervisor

L. B. Russell

R. B. Sydnor,,EngineerPlant Superintendent

Electrical & Controls

D. Zyriek, Shift SupervisorJ. A. Tiernan, Manager,, Nuclear Power

Other licensee employees were also contacted.

2.

Licensee Action on Previous Inspection Findings

Yellow Dots on Control Boards or Remove.(Clo

_

y Placement of

inspector verified that the yellow dots have been removed fDuring Control

rom Control Boards.

The NRC Performance Appraisal Secticn (PAS) report on Calvert C

318/82-01),

section 3.a.(8) dated April 14, 1982 noted that auditor indepen

s (317/82-01,

was conducted of the Off Site Safety Review Comm

QA was also the Chairman of the OSSRC.

eManager),

. . . .a

completed 5/13/81.

The subject audit was #81-0SSRC-1

individual replaced the Manager, QA as OSSRC Chaiman la

Also, reports of comencement and completion (with summary findi

a endar year 1981

requested audit were addressed directly to the Vice President

ngs) of the CSSRC

to the OSSRC Chairman wi ch somewhat removed the lead

, Supply, as opposed

direct management reporting chain.

r from his normal

Manual to ANS

which states that "While perfoming theThe licensee is

3.2-1976

auditors) shall not report to a management representative who has

audit, they (the

responsibility for the activity being audited."

e

auditor, at the request of the individual who was and

e lead

pervisor

_ _ _ _ .

3

throughout the audit period, audited activities for which his supervisor was

i

responsible. True auditor independence was not maintained. The inspector

reviewed this issue with the Manager, QA on 4/30/82 who stated that various

alternatives would be evaluated and long-term corrective action taken to ensure

that auditor independence is maintained in future audits of OSSRC activities.

This item is unresolved pending licensee action and subsequent NRC:RI review

(317/82-07-01,318/82-07-01).

The NRC PAS report also pointed out licensee weaknesses in the quality of

written safety evaluations (SE) for facility design changes accomplished

pursuant to 10CFR50.59.

It stated that SE's for numerous Facility Change

Requests (FCR) had been reviewed and quoted the SE's for FCR's 79-1024 on

the halon system and 81-1011 on fire barrier modifications.

It pointed out

the following observations associated with SE's:

Failure to provide "the bases for detemination that the change

--

does not involve an unreviewed safety question";

"nothing more than simple statements of conclusion providing no

--

bases for the detemination"; and

-- " required the reviewer to accept the evaluation on the assumption

that proper installation would resolve any concerns".

The inspector reviewed the SE's for the FCR's referenced in the PAS report and

three additional FCR's (80-1027 on the halon system, 80-1017 on the replacement

of solenoid valves, and 79-1055 onESFASresetmodifications).

One of the three additional FCR's reviewed (80-1027) exhibited the problems

discussed in the PAS report. The SE's for FCR's 79-1024 and 80-1027 stated

only that "Halon systems are not required to be safety related or function

in a seismic event. However, the systems are seisrically supported to preclude

the possibility of falling on safety related equip.nent". The SE for FCR 81-

1011 stated only that "Ductwork will be purchased and installed SR (safety

related) and will be seismically supported.

Barriers are seismically designed

and installed safety related.

Barriers will close up openings between existing

structure and will be seismically designed and installed safety related".

10CFR50.59(b) requires that records of changes to a facility as described in

the Safety Analysis Report (SAR) be maintained which include written SE's

providing the bases for detemination that the changes do not involve unreviewed

safety questions (USQ), A USQ is involved if the probability or consequences of

an accident or malfunction of equipment important to safety previously evaluated

it, the SAR may be increased, or the possibility for an accident or malfunction

of a different type than any previously evaluated in the SAR may be created, or

if the margin of safety as defined in the bases for any Technical Specification

is reduced. The SE's for FCR's 80-1027, 79-1024, and 81-1011 do not provide

sufficient bases infomation to adequately support their conclusions that no

USQs existed in that they were not sufficiently detailed in their discussions of

FCR and applicable SAR design criteria to make any meaningful comparisons. They

did not sufficiently describe what accidents or malfunctions (if any) were

addressed in the SAR or what items were considered in reaching the conclusion

that the changes did not increase the probabilities of SAR described accidents

or malfunctions or introduce accidents or malfunctions different than those

evaluated in the SAR.

_-_.

. - -

_ - -

_ _ _ _ _ _ _ _ _ _

.

4

The inspector determined that the above examples of 10CFR50.59 Safety

Evaluations were indicative of historical lack of depth of the Safety

Evaluations, confirming the validity of the findin

mance Appraisal Team (Report 317/82-01, 318/82-01)gs of the NRC's Perfor-

and Inspection Report

317/82-05, 318/82-05 (failure to evaluate certain aspects of a facility

change). The NRC will closely follow the licensee's corrective actions in

this area, which are required to be detailed in writing bv the licensee in

response to the referenced inspection reports (317/82-0) ')2, 318/82-07-02).

3.

Review of Events Requiring One Hour Notification to the NRC

The circumstances surrounding the following event requiring prompt NRC (one

hour) notification via the dedicated telephone (ENS-line) was reviewed.

At 7.39 a.m. on 4/17/82 a technician attempting to post a tagout on

--

the Unit 1 Control Element Drive System (CEDM) mistakenly op(ened the

breaker supplying power to Unit 2 Control Element Assembly CEA) 21

causing it to drop into the reactor core. At 7:41 a.m. CEA 20 dropped

when the same technician opened its supply breaker. The shift super-

visor, after failing to establish communications with the technician,

in anticipation of additional CEA drops ordered that Unit 2 be manually

tripped.

(Unit 1 had been shutdown earlier that day for a refueling

outage.) Prior to the Unit 2 trip, pressurizer levei fell 30 inches

below its program value. The licensee notified the NRC Operations

Center by ENS at 8:11 a.m.

Safety systems functioned as designed

following the trip.

4.

Radioactive Waste Releases

Records and sample results of the following liquid and/or gaseous radioactive

waste releases were reviewed to verify conformance with regulatory requirements

prior to release.

Gaseous Waste Permit G-039-82, Unit 1 Containment Modified Purge,

--

released on 4/18/82. Group I release rate 1.46 x 105 m3/sec.,

Group II release rate 1.25 x 102 m3/sec.

Release of Reactor Coolang Waste Monitor Tank 12 on 4/11/82.

--

Total released 4.51 x 10- curies, excluding tritium and noble

gases.

Liquid Waste Release Pennit R-033-82,12 RCWMT released 5/6/82.

--

Expected curies released 2.99 E-2 (pre-release results).

Containment Release Permit G-049-82, Unit 2 Vent via ECCS Pump

--

3

Room on 5/6/82. Group I rglease rate 8.81 E+2 m /sec., Group

II release rate 5.37 E-2 m3/sec.

No unacceptable conditions were identified.

l

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_ . .

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5

5.

Plant Maintenance

The inspector observed and reviewed maintenance and problem investigation

activities to verify compliance with regulations, administrative and

maintenance procedures, and codes and standards, proper QA/QC involvement,

safety tags use, equipment alignment, jumpers use, personnel qualifications,

radiological controls for worker protection, fire protection, retest require-

ments, and reportability per Technical Specifications. The following

activities were included.

Troubleshooting of Unit 2 CEDM 38 after rod drop on 4/17/82.

--

MR-82-8194, Modification to Electrical Penetration (FCR-79-65)

--

45 foot elevation, west penetration on 4/20/82.

MR-82-8016, Steam Generator 12 Support Plate Rim Cut, implemer. ting

--

Maintenance Procedure SG-14 (approved 4/19/82) observed 4/26/82.

No unacceptable conditions were identified.

6.

General Orientation Retraining

The inspector ai. tended General Employee Orientation Retraining, Part I (facility

access) and Part II (radiation protection) on April 15, 1982. The training was

comprehensive in nature and in accordance with the lesson plan. The examination

for Part II training was prepared by the Institute of Nuclear Power Operations

as part of a pilot program to develop generic radiation protection retraining.

The inspector noted that the examination appeared to be comprehensive and was

more difficult than historical exams for Part II training. The instructor

commented that a higher failure rate was being experienced on the newer

examination (about 30%) requiring more instensive retraining for selected

individuals.

No unacceptable conditions were identified.

7.

Observation of Physical Security

the inspector checked, during regular and off-shift hours, on whether selected

aspects of security met regulatory requirements, physical security plans, and

approved procedures,

a.

Security Staffing

01servations and personnel interviews indicated that a full time

--

trember of the security organization with authority to direct

physical security actions was present, as required.

Manning of all three shifts on various days was observed to be

--

as required.

b.

Physical Barriers

Selected barriers in the protected area (PA) and the vital area (VA) were

observed.

Random monitoring of isolation zones was performed. Observa-

tions of truck and car searches were made. One finding relating to the

protected area barrier is addressed on the following page.

_-

. _ _

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c.

Access Control

Observations of the following were made:

Identification, authorization, and badging;

--

Access control searchts;

--

.

Escorting;

--

Communications;

--

Compensatory measures when required.

--

d.

Bomb Threat

One bomb threat was received during this reporting period. The

required security procedures were followed. Appropriate searches

were conducted with negative results.

e.

Potential Strike

During this inspection period the licensee made preparations to cope

with a threatened local union picket line of pipe insulators against

an onsite subcontractor. The picket line, anticipated to begin about

4/19/82 was never established. The inspector reviewed the licensee's

preparations and arrangements for coping with the picket line.

No unacceptable conditions were identified.

8.

Licensee Action on NUREG 0660, NRC Action Plan Developed as ~a Result of the

TMI-2 Accident

The NRC's Region I Office has inspection responsibility for selected action

plan items. These items have been broken down into numbered descri

(enclosure 1 to NUREG 0737, Clarification of TMI Action Plan Items)ptions

Licensee

.

letters containing commitments to the NRC were used as the basis for accept-

ability, along with NRC clarification letters and inspector judgment. The

following items were reviewed.

I.C.6, Verify Correct Performance of Operating Activities. This item

--

had previously been inspected and remains open pending implementation

of licensee commitments.

During the review of the tagging associated

with a Unit 2 CEDM drop and reactor trip on 4/17/82, the inspector

noted that independent verification was not required.

CCI 112C, Safety and Safety Tagging requires a second, independent

verification of correct implementation of equipment control measures

for the use of apparatus service tags, including return to service.

These are the principal tags in use at the site for both mechanical

and I&C maintenance work. For the use of low voltage permits (600

volts or lower) an independent verification is not required.

In

addition, the return to service position is not required to be

_.

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8

specified or documented, just the lifting of the tags. For the use

of high voltage electrical equipment (greater than 600 volts) CCI ll2C

requires an independent verification of switch position by the job

supervisor and in addition, potential tests by electricians to verify

the equipment is deenergized. Documentation of these checks is not

required. The inspector noted that this methodology was not according

to the guidance of I.C.6 nor the licensee's comitments in their letter

dated December 15, 1980. The licensee stated that they were investigating

methods to implement independent verifications for High and Low Voltage

Permits. This item is unresolved (317/82-07-04, 318/82-07-04).

II.K.3.17, ECCS System Outages. The inspector reviewed the licensee's

--

second submittal supplying infomation on Emergency Core Cooling System

unavailability. The letter, dated April 13, 1982 was in response to an

NRC request to go beyond a listing based on LER's and include outages

due to surveillance testing, planned and unplanned, and preventive

maintenance.

The inspector noted that the licensee's submittal did not include all

preventive maintenance. As an example, removal of the Service Water and

Component Cooling Water Heat exchangers from service to mechanically clean

tubes was not included, however, the length of time these were out-of-

service for preventive maintenance had been the subject of a previous

unresolved item. The licensee acknowledged the inspector's coments and

stated that a review would be perfomed of the Calvert Cliffs preventive

maintenance program and revised outage infomation forwarded to the NRC

by May 28,1982. This item is unresolved (317/82-07-05, 318/82-07-05)

pending resubmission by the licensee and NRC review.

9.

Review of Plant Operations

a.

Daily Inspection

The inspector toured the facility to verify proper manning and access

control, and observed adherence to approved procedures and LCOs.

Instrumentation and recorder traces were observed. Status of control

room annunciators was reviewed. Nuclear instrument panels and other

reactor protective systems was examined.

Control rod insertion limits

were verified. Containment temperature and pressure indications were

checked against Technical Specifications. Stack monitor recorder traces

were reviewed for indications of releases.

Panel indications for on-

site /offsite emergency power sources were examined for automatic

operability. Control room, shift supervisor, tagout log books, and

operating orders were reviewed for operating trends and activities.

During egress from the protected area, the inspector verified operability

of radiological monitoring equipment and that radioactivity monitoring

was done before release of equipment and materials to unrestricted use.

These checks were performed on the following dates: April 15,17,19,

20, 21, 27, 29, 30, May 5, 6, 7, and 10,1982.

On 4/21/82 the inspector obserycd that Unit 1 shutdown cooling flow

--

was 2200 gallons per minute. The unit was in Mode 5 and drained

9

down to the top of the hot leg to facilitate getting water out of

the steam generator U-tubes. The Reactor Coolant System was being

borated to refueling concentration. The inspector questioned the

operator about the minimum requirement for shutdown cooling flow.

Technical Specifications for Modes 4 and 5 require that at least

2 coolant loops (of 4, including 2 shutdown cooling and 2 reactor

coolant) be operable and at least I be in operation.

(Undercer-

tain conditions all flow can be stopped for up to I hour.)

Technical Specifications for Reactor Coolant System flow requires

at least 3000 gallons per minute during any dilution of the reactor

coolant. Technical Specifications for refueling operations (Mode 6)

require at least I shutdown cooling loop be in operation at 3000

gallons per minute, however, this is allowed to be relaxed to 1500

gallons per minute if the water level is drained below the mid-plane

of the hot leg.

Because no dilution was in progress there was

apparently no specified requirement for flow. The inspector noted

that the conditions listed for reduced flow in Mode 6 were more

coninon occurrences in Mode 5, for example during replacement of

Reactor Coolant Pump seals and the evolutions in progress on 4/21/82.

The basis for the Technical Specifications included reasons for the

specified flow (Mode 6) to ensure sufficient cooling capacity, to

minimize the effects of a boron dilution incident and to prevent

boron statification. The inspector noted that these were valid

concerns in Mode 5 as well and stated that the licensee should

consider requesting an amendment to specify required Reactor Coolant

flow in Modes 4 and 5.

.'his item is unresolved (317/82-07-06)

and will be further reviewed by the NRC.

b.

Weekly System Alignment Inspection

Operating confirmation was made of selected piping system trains.

Accessible valve positions in the flow path were verified correct.

Proper power supply and breaker alignment was verified. Visual

inspections of major components were performed. Operability of

instruments essential to system perfonnance was verified. The fol-

lowing systems were checked.

Various system lineups in the Units 1 and 2 east and west 10

--

foot Penetration Rooms on 4/16/82, including Service Water

lineup to Containment Coolers 12, 14, 22, and 24, Containment

Spray and Low Pressure Safety Injection Valves.

Low Pressure Safety Injection train 22 on 4/19/82.

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Unit 2 Component Cooling Water lineup in the Component Cooling

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Water and ECCS Pump Rooms on 4/27/82.

Containment Spray train 22 on 5/7/82.

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No unacceptable conditions were identified.

. _ _ _ _ _ _ - - _

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10

c.

_ Biweekly Inspection

Verification of the following tagouts indicated the action wa

conducted.

s properly

Penetration, verified on 4/20/82.Tagout 19022, Loca

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on

Tagouc .9140, 21

-

Charging Pump 011 Leak, verified on 4/30/82

Tank levels were also confimed. Boric acid tank samples

.

cations.

During a review of the Unit 2 Tagout Book on 5/5/82 the ins

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noted that Service Water Pump 22 was listed as tagged i

pector

to lock position.

The tagout had been issued on 4/30/82 and

placed and independently verified on 5/1/82.

Pump 22 was neither in pull to lock nor tagged

Later, during a

restored to service on the same day the ta

Investigation

.

was on file in the Tagging Authority's Offic

A

.

Record did not document tag removal and restoration to n

,

up by either the initial or independent checkcr, required by

ne-

i

administrative procedures.

of Calvert Cliffs Instruction ll2C, safety and Safety Ta

regarding the clearing of tags and restoration of equipment to

service is a violation (318/82-07-06),

,

'

d.

_0ther Checks

During plant tours, the inspector observed shift turnovers

pemits, protective clothing and respirators. practices at

, security

i

r

monitors were reviewed. status of personnel monitoring practici

Plant housekeeping and cleanliness was eval

with TS LCOs.

TS LCOs, including RCS Chemistry and Activity, Secondary Ch

Other

Activity, watertight doors, and remote instrumentation were ch

y and

e.

About 2:30 p.m. on 4/15/82, during an alignment of the Unit 1

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Refueling Water Tank (RWT) to the Spent Fuel Pool (SFP) p

cation system, approximately 2500 gallons of borated wate

fed through a malfunctioning 150 psi relief valve

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SFP cooler 11 to the miscellaneous waste receiver tank, 0-RV-1997

was quickly isolated and repaired on the followi

The valve

.

The

nvolved.

were posted beyond their expiration dates.On 4/19/8

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.

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11

SWP No.

Expiration Date

82-286

4/13/82

82-284

4/13/82

82-173

4/14/82

82-176

4/14/82

This was pointed out to the on-duty principle radiation-chemistry

technician. The expired SWPs were removed by 4/20/82.

During a tour of the Unit 2 Charging Pump Room on 4/30/82 the

--

inspector noted that the door to the enclosure for Charging Pump

22 had been blocked open. The enclosures had recently been

installed as part of the fire protection plant upgrade, however,

the door was not labeled as a fire door. The licensee stated that

the door in question was a fire door and that the Charging Pump

enclosure doors would be closed and appropriately labeled. This

item is unresolved (318/82-07-07) pending completion of the licensee's

actions and reinspection by the NRC.

About 9:30 a.m. on 4/20/82 a fire broke out on the second floor of a

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temporary 2-story building under construction east of the South

Service Building. The onsite fire brigade extinguished the fire

within 10 minutes. The local fire department responded within 15

minutes. No safety-related equipment or radioactive materials were

involved.

The inspector observed the actions of the onsite fire brigade and

security measures to allow rapid access for the local fire department

(SolomonsIsland). No unacceptable conditions were identified.

About 1:00 p.m. on 4/14/82 an approximately 1 inch layer of spent

--

resin was found unifonnly spread over the top of a shipping cask liner,

contained by a 2 inch lip around the liner outside circumference.

The spillage occurred during a transfer operation of resin from

the spent resin metering tank at about 3:00 p.m. on 4/13/82. No

resin spread outside of the shipping cask. A small resin sample

measured 4 mrem /hr on contact. The liner top measured 400 mrem /hr

on contact. The outside of the cask measured 15 mrem /hr on contact.

No personnei exposure or contamination problems resulted.

Subsequent invetigation showed that about 150 cubic feet of resin

had been transfeired to the cask liner. The personnel involved

during the event hcd underestimated the amount of resin in the

holding tank and bei'eved they were only transferring about 90

cubic feet. There is a level indicator on the resin metering

tank.

Level is estimateo based on the number and volume of ion

exchangers flushed to the tank. The transfer operation had been

interrupted by a continuous air monitoring system (CAMS) alann at

3:00 p.m. which resulted in a 1 to 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> evacuation of the area.

A followup air sample showed zero MPC iodine and particulate

activity and the following gaseous activity.

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Isotope

~ Activity,uci/cc

Xe 131m

1.72 x 10-8

Xe 133

1.76 x 10-6

Xe 133m

1.72 x 10-8

Xe 135

4.9 x 10-11

The liner may have overfilled during the interruption. The inspector

discussed the event with radiation safety and operations personnel.

He expressed concern to the General Supervisor of Operations (GS0) on

4/20/82 that the exact cause needed to be identified and corrective

action taken to prevent recurrence. The GS0 stated that a radiation

safety engineer had been assigned to investicate the inchient to

determine appropriate corrective actions. This item is unresolved

pending licensee action to identify and correct associated problems

and subsequent NRC review (317/82-07-07).

10.

Containment Leakage Testing

During the week of March 8, 1982 the inspector discussed clarification of

10CFR50 Appendix J requirements with the licensee. A copy of an internal NRC

memorandum from the Director, Division of Systems Integration, NRR to the

Director, Division of Resident and Regional Inspection, I&E dated January 11,

1982 was handed to the licensee. The position of the memorandum was basically

that improvements in pathway leakages performed on paths testable in Type B

and C testing completed during the outage time preceeding a periodic integrated

containment leakage test must be added to the as found integrated results.

This would allow leakage information obtained fron the "as is" Type A (integrated)

test to be used to assess the containment condition and its integrity following

a period of plant operation. The licensee disagreed with the NRC position,

however, the inspector stated that this was the position which would be enforced.

On April 13, 1982 the licensee sent a letter to the Operating Reactors Project

Manager formally stating their disagreement with the NRC position in the

January 11, 1982 memorandum.

About 4/27/82 the inspector was informed by the licensee thet 9 penetrations,

including electrical (4) and piping (5) penetrations had been repaired or

removed on Unit 1 following the refueling shutdown which commenced on April 17,

1982 without testing for the "as found" leakage. The inspector held a meeting

with the licensee on April 28 to discuss this issue. The inspector expressed

concern that the licensee had decided to repair the penetrations without prior

testing. This decision had not been discussed with the NRC nor was the April 13,

1982 letter disagreeing with the NRC position distributed to the Resident

Inspector. The inspector informed the licensee that failure to make prior

measurements of pathway leakage meant that it was impossible to detemine

improvement for the purpose of calculating the "as found" integrated contain-

ment leakage and that the 1982 Integrated Test would be considered to be a

failure. The inspector also querted the licensee concerning whether any

additional repairs were anticipated prior to Type B and C testing. The licensee

stated that none were planned, but if any repairs were indicated they would test

for the "as found" condition.

_ . _ - _

.

.

___

_ , . _ _

_ _ _ _ .

_-

_ _ _ _ _ _ _ _ - . _ _ _ .

13

The licensee stated that a review could be made of the 9 repairs in question

in order to establish an upper boundary of leakage for those paths which had

1 valve or barrier still intact.

In addition, they stated that data was

available from the previous Type B and C tests which could be used as the basis

for improvement, notwithstanding any unquantified increase during Cycle 5

operation. The inspector stated that this area was unresolved (317/82-07-08)

and would be examined by a Specialist NRC Inspector during the review of the

integrated test results. The inspector further noted that the point regarding

integrated test failure became moot following discovery by the licensee

(paragraph 11) that Unit I had been operated throughout Cycle 5 with contain-

ment leakage above allowable.

11.

a.

Review of Licensee Event Reports (LERs)

LERs submitted to NRC:RI were reviewed to verify that the details were

clearly reported, including accuracy of the description of cause and

adequacy of corrective action. The inspector determined whether further

information was required from the licensee, whether generic implications

were indicated, and whether the event warranted onsite followup. The

following LERs were reviewed.

LER No.

Date of Event

Date of Report

Subject

Unit 1

82-09/3L

3/14/82

4/14/82

RPS CHANNEL B HI POWER, THERMAL

'

MARGIN / LOW PRESSURE & AXIAL SHAPE

INDEX TUS BYPASSED; TH INPUT

FAILING LOW

82-10/3L

3/19/82

4/12/82

CEA PULSE COUNTING SYSTEM &

INCORE DETECTION SYSTEM INOPERABLE

82-11/3L

3/21/82

4/16/82

CEA 21 DROPPED INTO CORE

82-12/3L

3/16/82

4/15/82

11 and 12 CHARGING PUMPS INOPERABLE

82-13/3L

3/16/82

4/15/82

12 CHARGING PUMP OUT-OF-SERVICE

FOR MAINTENANCE & 13 CHARGING

PUMP INOPERABLE

82-15/3L

4/07/82

4/23/82

PRESSURIZER LEVEL EXCEEDED 5%

PROGRAM BAND

82-16/3L

4/01/82

4/27/82

ECCS EXHAUST FILTER TRAIN INOPERABLE

82-17/3L

3/22/82

4/21/82

12 CONTROL ROOM A/C UNIT INOPERABLE

82-18/3L

4/06/82

5/04/82

12 ECCS PUMP ROOM EXHAUST FAN

REMOVED FROM SERVICE FOR SHAFT

BEARING REPLACEMENT

82-19/3L* 4/15/82

4/29/82

HYDROGEN ANALYZER INOPERABLE

_ _ _ _

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_

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14

LER No. Date of Event

_Date of Report

' Subject'

Unit 1

82-22/3L*

5/03/82

5/04/82

UNIT 1 OPERATIONS IN EXCESS OF

200 DEGREES PERFORMED WITH COM-

BINED LEAKAGE RATE OF GREATER

THAN 0.60 La FOR ALL PENETRATIONS

AND VALVES SUBJECT TO TYPE B &

C TESTS DURING CYCLE 5

Unit 2

82-15/3L

3/20/82

4/19/82

NEGATIVE LIMIT SET POINT FOR

CHANNEL A 0F RPS AXIAL SHAPE

INDEX TU OUT OF SPECIFICATION

82-16/3L

4/02/82

4/30/82

PLANT COMPUTER FAILED CAUSING

LOSS OF CEA PULSE COUNT SYSTEM

& INCORE DETECTION SYSTEM

82-17/3L

4/07/82

5/04/82

23 CHARGING PUMP REMOVED FROM

SERVICE WHILE 22 CHARGING PUMP

OUT-OF-SERVICE

82-19/3L

3/28/82

4/27/82

CEA 38 REED SWITCH POSITION

INDICATOR CHANNEL GIVING ERR 0NE0US

INDICATION

b.

For the LERs selected for onsite review (denoted by asterisks aLove) the

inspector verified that appropriate corrective action was taken or

responsibility assigned and that continued operation of the facility was

conducted in accordance with Technical Specifications and did not con-

stitute an unreviewed safety question as defined in 10CFR50.59. Report

accuracy, compliance with current reporting requirements and applicability

to other sf:s systems and components were also reviewed.

LER 82-08/3L (NRC Inspection Report 317/82-05, 318/82-05) - In

--

reviewing this incident the inspector learned that the plant

operators incorrectly believed Component Cooling Water Heat

Exchanger (CCHX) 11 was back in service when 1 of 2 posted sets

of equipment tags had been cleared. The licensee principally

attributed the cause to the failure to enter the CCHX 11 inlet

valves in the Locked Valve Deviation Log, which is reviewed by

operators during shift turnover and poor coninunications during

l

shift turnover.

The inspector discussed this event with the General Supervisor

of Operations (GS0) on 4/15/82 and stated that the NRC felt this

event was significant in that it represented a failure of the

operators on duty to carry out their basic responsibility of

being cognizant of plant status. The GS0 agreed and stated that

he would further discuss the event with his operators and remind

them of their responsibilities in this area. This item is un-

resolved pending licensee action and subsequent NRC review

(317/82-07-09).

.

-__-_ _

_ _

.-.

. _ _ _

.

15

c.

LER 317/82-19. On April 15, 1982 the licensee discovered that the flow

path from the containment to the hydrogen analyzers was isolated. This

was discovered during flow testing of the sample lines to hydrogen analyzer

cabinet IJ222, which was inoperable due to modifications to satisfy TMI TAP

Item II.F.1.6.

The licensee discovered that the test pressure would not

bleed off after the containment isolation valves were opened. A similar

test at 6:10 p.m. on the lines to the cabinet IJ220, the redundant

analyzer, which was being relied upon as the required analyzer (T.S.3.6.5.1),

showed a similar problem. The analyzer was declared inoperable, personnel

entered the containment, discovered that the three manual stop valves to

the cabinet were shut, and reopened the valves at 6:30 p.m., terminating

the event. Subsequent investigation showed that the manual stops to the

redundant analyzer were closed, and a flow test on Unit 2 was successfully

performed.

The licensee detennined that the valves had apparently not been returned

to service following local leak rate testirig (between November 21-28, 1980)

consequently all Unit 1 operations in Modes 1 and 2 during Cycle 5 were

without the required hydrogen analyzers. Licensee review of this event

revealed the following principal causes and planned corrective actions.

(1) The valves did not appear in the NSSS Sampling Operating

Instructions' valve list and consequently no verification

of the valves' position prior to entering Mode 4 on January 8,

1981 was performed.

(2) The tagging procedure used at the time of this event did not

provide for returning valves to a specified position when tags

were cleared nor did it provide for a second individual verifying

that the valve is returned to its proper position after a tagout.

A task force reporting directly to the Plant Superintendent had been

established in February,1982 to walk down all piping systems within

Calvert Cliffs with the following objectives:

(1) Verify the correct arrangement of valves on the piping and instru-

ment diagrams (P& ids) and to add or delete valves from the P& ids

and the operating instructions' valve lists to reflect as-built

conditions.

(2) Ensure that the numbering, descriptions, and operating positions

of all valves listed in the Operating Instructions' valve lists

are correct.

(3) Attach metal identification tags to each valve.

Every process system valve in the plant is to be physically checked regard-

ing its location, function and operating position at the conclusion of this

effort. The Operating Instructions' valve list for each system will be

checked to ensure that all valves are included along with their correct

number, description, location, and operating positions after each system

is walked down to ensure completeness and accuracy of the valve lists.

All valves in the facility will have metal identification tags attached

for facilitating valve lineup checks, restoration of equipment to service

and to minimize system transients due to misoperation of valves. All

.

._

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16

walkdowns and updated valve lists will be complete for all safety

related systems for both units by December 31, 1982.

Further, the licensee stated that Calvert Cliffs Instruction ll2C

Safety and Safety Tagging was revised in June,1981 to incorporate a

l

system by which 2 operators are used to return equipment to service

and to verify that the equipment is returned to service correctly.

The procedure provides for documentation of this verification and of

the repositioning of valves and other components after maintenance or

testing.

If the Senior Control Room Operator directs valves to be

repositioned differently from the nomal operating position after

testing due to operating conditions, this is also documented. With

j

the revision of this instruction, additional verification is being

perfomed by qualified operators of the position of equipment restored

to operability after testing or maintenance consequently minimizing

the possibility of a recurrence of this event.

.

The inspector reviewed the circumstances surrouding this event including

discussions with personnel and review of documents and the report.

The following procedures and drawing were reviewed.

0131B, NSSS Sampling System, revision 4 approved 1/20/82.

--

Coment: This procedure describes the operation of the H2

analyzing system. As noted by the licensee, the valve check-

list appended to the procedure did not include the stop valves

inside the containment. This procedure also provided the path,

through the H2 analyzers, to obtain post-accident containment

radioactivity samples pending installation of the Post-Accident

Sampling System.

0141 A, Hydrogen Recombiners, revision 1 approved 3/2/77.

--

Comment: This procedure does not address use of the hydrogen

analyzer readings.

01 41B, Hydrogen Purge System Operation, revision 2 approved

--

3/20/79. Comment: System operations did not rely on readings

from the hydrogen analyzers.

E0P5, Loss of Reactor Coolant, revision 12 approved 3/6/81.

'

--

Comment: This procedure requires placing the hydrogen recombiners

in service prior to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after the start of the incident, with-

cut reliance on H2 readings. The safety analysis presented in

Section 14.19 of the FSAR, concludes that the recombiner would be

started when hydrogen concentration reaches 3% or approximately

9.55 days after the start of the LOCA.

OM 463, Piping and Instrument Drawing for the Gas Analyzing System,

--

Units 1 and 2, revision 3 dated 5/26/81. Coment: This drawing

shows the valves in question and lists their position as locked open.

(Containment No.1 North Shield, Containment No.1 Elevation 135,

Containment No. 1 Elevation 189.)

--

.

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17

STP M-571-1, Local Leak Rate Tests, revision 3 approved 9/24/80.

--

Coment: This procedure isolates the hydrogen analyzer flow

path but does not include restoration lineups. The inspector

questioned various operators concerning tagging for the purpose

of local leak rate testing (not required by the procedure). They

stated that the penetrations may or may not be tagged, depending

on the particular circumstances. The inspector questioned the

licensee regarding this aspect in light of the statement that

revised tagging requirements would minimize the potential for

recurrence. The licensee stated that the STP would be revised

to require tagging.

The inspector also questioned the licensee concerning short-tenn corrective

action in case another, similar system was misaligned as a result of

local leak rate testing without subsequent proper lineup on startup or

as otherwise necessary.

Because Unit 1 shutdown the next day following

the event no further action was necessary (all local leak rate testing

is to be controlled by tags). The licensee stated that Unit 2 penetra-

tions which were isolated during local leak rate testing would be

investigated.

Technical Specification 3.6.5.1 requires that two independent containment

hydrogen analyzers shall be operable in Modes 1 and 2.

Continued

operation in a degraded mode is allowed for a period of time with one

analyzer out-cf-service. Unit 1 operation during Cycle 5 without an

operable hydrogen analyzer is a violation (317/82-07-10) of Technical Specification 3.6.5.1.

d.

LER 317/82-22. At 2:00 p.m. on May 3,1982 the licensee confinned that

from 12/18/80 until 4/18/82 all Unit 1 operations in excess of 200 degrees

had been perfonned with a combined leakage rate greater than allowed by

Technical Specifications. This was discovered during a review of the

latest Containment Local Leak Rate Test Procedure (STP M-571-1, revision

3 approved 9/24/80) and the latest test results completed December 18,

1980.

Technical Specification 3.6.1.2.b requires that containment combined

leakage rate shall be less than 0.60 La (La)= 0.2 percent by weight of

the containment air per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> at 50 p(La

sig for all penetrations and

valves subject to Type B and C tests.

,T

Pa are defined in 10CFR Part 50, Appendix J.)ype A, B, and C tests and

The results of the test

completed on December 18, 1980 were found to be 0.773 La, however, the

required action of restoring the leakage to within limit prior to

exceeding 200 degrees was not taken.

One contributing factor which led to operation above allowable containment

leakage limits was an error introduced into STP M-571-2 during a general

revision on 9/24/80. At that time, the limit, previously stated simply

as the maximum allowable leakage - 207,600 sccm (standard cubic centimeters

per minute), was changed to list 207,600 scem as the administrative limit

and 346,247 as the Technical Specification limit. The engineer changing the

procedure apparently confused La (346,247 sccm), the maximum allowable

, - , - ,

'

18

leakage rate (10CFR50, Appendix J definition) with the Technical

Specification limit (0.6 La).

The inspector independently calculated the required leakage rates using

a Containment Free Volume (FSAR Section 5.1.2.1) of 2,000,000 ft3 and

,

Pa of 50 psig with a resultant leakage rate of 207,700 secm. This

l

rough calculation confirmed the licensee's conclusion that the administra-

tive limit specified in STP M-571 was in reality the Technical Specification

limit (0.6La)-

The inspector reviewed the following procedures.

STP M-471-1, Air Locks Door Operability and Leak Rate Test,

--

revision 2 approved 9/3/80. Coment: This was a general revision

for format and content. An administrative limit of 207,600 seem

was added and a TS limit of 346,247. The Plant Operations and Safety

Review Comittee (POSRC) approved the revision in meeting 80-120 on

9/3/80.

-- STP M-571-1, Local Leak Rate Tests, revision 3, approved 9/24/80.

Comment: The POSRC approved the revision in meeting 80-130 on

9/24/80. This procedure change was also a general revision and

changed the administrative and TS limit.

Results of STP M-571-1, Local Leak Rate Tests, completed 12/18/80.

--

Coment: The remarks section contained the following note:

"The Administrative leakage limit (running total of all

test, including data from the previous performed LLRT

on penetrations not tested yet this outage) of 207,600

sccm was exceeded, running total is 267,615.21 scem

with 232,051.34 due to the leakage of penetrations ZWB8,

ZWC3, ZEC2, and ZEC7.

MR issued for corrective action.

Follow up Action MR's issued to Electric Shop for pene-

trations, further FCR pending. Final leakage 267,709.75

sCCm."

The POSRC approved the completed test results in meeting 81-22 on

2/2/82.

The inspector reviewed the POSRC meeting minutes listed above and noted

that all items reviewed were approved without comment. Several members

present were questioned regarding the content of the review but they

indicated that it was too far in the past to recall. The POSRC Chaiman

indicated that the STP results were probably approved because the procedure

stated that the results were between the administrative and TS limits and

ccrrective actions had been initiated.

The inspector noted that the test failure was caused principally by four

electrical penetrations (total leakage 0.67 La). The penetrations involved

were all Type 2E Electrical Penetrations made by Amphenol, Sams Division.

The inspector reviewed historical test results for the four penetrations

and noted the following progressive deterioration:

_.

,

_ _ _ _ _ _____

_ _ _ _

.

.

Penetration

Preop

5/76

3/77

3/78

~7 /79

10/80

ZWB8

10

0.4

7

1393

23043(1419)

(28772)

ZWC3

4

0

0

22

1810(2917)

(46408)

ZEC2

5

0

240

4790(4464)

(76777)

-

ZEC7

3

0

-

94

3380(1310)

~(80112)

Total

22

0.4

1749

(10,110)

(232,069)

-

Parenthetical values are as-left condition. Other values are listed

as-found. All numbers in sccm.

The inspector asked the licensee about individual limits (both administrative

and absolute) for the results of individual penetrations. Although valves

(Type C tests) contained such limits,none were specified for the electrical

penetrations. The licensee stated that the valve values were obtained from

codes and standards, however, these were not available for electrical

penetrations. As a result the licensee started up with 39% of the allowable

combined leakage coming from a single (ZEC7) penetration, without successful

repair. This was another contributing factor to the event.

The inspector questioned the licensee concerning the as-found condition of

the penetrations following Cycle 5 operation in light of the noted progressive

deterioration. This information would allow quantification of the leakage

to detemine how much above the limit the leakage was at the end of the

cycle. The inspector was infomed that these penetrations were included

in those which had been imediately removed from the containment without

prior testing upon shutdown on April 17,1982 (see paragraph 10). This

action was contrary to the NRC position on Type B and C leakage testing

and resulted in an inability to establish how bad the leakage was at the

time of shutdown. The penetrations are bein

type (Conax Type 2E Electrical Penetrations)g replaced with an improved

The penetrations will be

.

welded to the containment liner versus the previous design which incorporated

a bolted joint with two concentric 0-rings.

In addition, the cable passages

have been changed to include an improved mechanical joint and better epoxy

material. A Type A (integrated) test will be perfomed after the current

refueling outage. The inspector stated that operation of the facility

between 12/18/80 until 4/18/82 with a combined containment leakage rate

greater than allowed was a violation (317/82-07-11).

The licensee stated that although similar procedural errors existed in the

Unit 2 procedures, the actual results of Unit 2 combined leakage tests were

always within required limits.

12. Review of Periodic and Special Reports

Upon receipt, periodic and special reports submitted pursuant to Technical Specification 6.9.1 and 6.9.2 were reviewed. That review included the following:

Inclusion of infomation required by the NRC, test results and/or supporting

infomation consistency with design predictions and perfomance specifications,

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20

planr.ed corrective action adequacy for resolution of problems, determination

whether any information should be classified as an abnormal occurrence, and

validity of reported information. The following periodic report was reviewed.

'

March,1982 Operations Status Reports for Calvert Cliffs No.1 Unit

--

and Calvert Cliffs No. 2 Unit, dated April 15, 1982.

During the review of the March,1982 Operations Status Report the

inspector noted that the report distribution was not according to

1

the latest Technical Specification change (issued March 9,1982).

The licensee stated that a copy of the March report would be sent

to the correct addressee and that the distribution would be cor-

rected for future reports. A subsequent revised report was sent

on May 5,1982 to the correct distribution.

13. Unresolved Items

Unresolved items are matters about which more information is required to

determine whether they are acceptable. Unresolved items are discussed in

paragraphs 2, 8, 9,10,11, and 12 of this report.

14.

Exit Interview

Meetings were held with senior facility management periodically during the

course of this inspection to discuss the inspection scope and findings. A

summary of findings was also provided to the licensee at the conclusion of

the report period.

_

>

,