ML20045C040

From kanterella
Jump to navigation Jump to search
Insp Repts 50-282/93-08 & 50-306/93-08 on 930330-0531. Violations Noted.Major Areas Inspected:Maint,Surveillance, Engineering & Technical Support,Radiological Controls & Licensee Followup on Previously Identified Items
ML20045C040
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 06/11/1993
From: Jorgensen B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20045C035 List:
References
50-282-93-08, 50-282-93-8, 50-306-93-08, 50-306-93-8, NUDOCS 9306220014
Download: ML20045C040 (28)


See also: IR 05000282/1993008

Text

.-

_m

-

-

,

1

+

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Reports No. 50-282/93008(DRP); 50-306/93008(DRP)

'

Docket Nos. 50-282; 50-306

License Nos. DPR-42; DPR-60

f

Licensee: Northern States Power Company

414 Nicollet Mall

Minneapolis, MN 55401

Facility Name:

Prairie Island Nuclear Generating Plant

Inspection At:

Prairie Island Site, Red Wing, MN ,

Inspection Conducted: March 30 through May 31, 1993

Inspectors:

M. L. Dapas

R. L. Bywater

D. S. Butler

T. J. Kozak

'n

g p3

Approved By:

B. L.

-

en

n, Chief

i-

Reactor Proje ts Section 2A

D~ ate

,

Inspection Summary

Inspection on March 30 through May 31, 1993 (Reports No. 50-282/93008(DRP);

50-306/93008(DRP))

Areas Insnected: Routine, unannounced inspection. by resident and regional

inspectors of plant operational safety including onsite followup of events,

maintenance, surveillance, engineering and technical support, radiological

controls, licensee followup on previously identified items, licensee event

,

report followup, allegation followup, and response to Regional requests.

i

,

l

1

9306220014 930611

PDR

ADOCK 05000282~

G

PDR.

m

,

-

E

p.

Executive Summary

Enforcement

Two cited violations of NRC requirements, one unresolved item, and one

inspection followup item were identified in the areas inspected.

Operations

L

No new strengths or weaknesses were identified. One violation was identified

involving the failure to maintain Technical Specification required

administrative controls for an inoperable containment isolation valve

(paragraph 1.b).

One inspection followup item was identified involving the

effects of temperature on Regulatory Guide 1.97 event monitoring equipment and

the relationship between the safeguards chilled water system and 480 Volt

switchgear operability (paragraph 1.c).

A concern was identified with the-

licensee's implementation of its empowerment philosophy relative to ensuring

that an appropriate level of management is involved in the decision making

process, and that those individuals entrusted with making decisions; keep their

respective supervisors informed (paragraph 1.d).

A concern was also

identified with the-increased incidence of equipment found in an off-normal

condition (paragraphs 1.e and 2.a).

Maintenance and Surveillance

No new strengths were-identified. One violation and associated weakness were

identified involving the improper setting of overtemperature delta temperature

and overpower delta temperature reactor protection system trip setpoints

(paragraph 6.a).

One unresolved item was identified-involving the apparent.

failure to perform required ASME Section XI testing of certain valves -

l

(paragraph 7.c).

1

Enaineerina and Technical Support

,

No new strengths or weaknesses were identified.

Inadequate review of the

design assumptions used to determine the weight of the spent fuel pool covers.

,

resulted in .the licensee qualifying the spent fuel pool crane as single-

failure proof for a maximum critical load less than the actual weight of the

covers (paragraph 4.a).

Radioloaical Controls

!

No new strengths or weaknesses were identified. The licensee implemented the

use of a new thermoluminescent dosimeter on April 1, 1993 (paragraph 5.a).

'

_

s

2

i

t

'

,,

--

. . .

.

.

-

-

,

,.

.

.

. _ - .

_ _ __

_

-

_

l

-l

.a

i

,

REPORT DETAILS

!

l

!

1.

Operational Safety Verification (71707. 93702)

I

,

The inspectors observed control room operations, reviewed applicable

'

logs, conducted discussions with control room operators, and observed

shift turnovers. The inspectors verified operability of selected

,

emergency systems, reviewed equipment control records, verified the

-

l

proper return to service of affected components, conducted tours of the

auxiliary building, turbine building and external areas of the plant to

observe plant equipment conditions, including potential fire hazards,

'

and to verify that maintenance work requests had been initiated for

equipment in need of repairs.

4

a.

General

Both units operated at full power throughout the inspection period

-

except as noted below.

,

Unit I was reduced in power for turbine valve testing on

April 24-25, 1993.

Unit 2 was reduced in power for turbine valve

testing on April 18, 1993.

'

Unit I had a brief reduction in load of'approximately 8 MW on

May 17, 1993.

This occurred when a control room operator was

,

replacing a control panel light bulb for CV-31023 ~(ISA feedwater

'

heater drain to 14A feedwater heater) without a light _ bulb removal

l

tool.

During the bulb removal, a short occurred,'a fuse was

blown, and CV-31023 failed closed. The resulting increase in

feedwater heater level caused CV-31024 (15A feedwater. heater drain

t

to B condenser dump) to open and caused the load reduction due to

reduced feedwater heating.

Replacement of the fuse was prompt and

full power operation was restored shortly thereafter. Although

,

!

this was a minor transient, it could have been avoided by proper

use of the light bulb removal tool .

1

b.

Loss of Administrative Control for a Containment Isolation Valve

"

On April 3,1993, while performing SP 2272, " Quarterly Cycling of

. ;

Pressurizer Relief Tank (PRT) Reactor Makeup Water and Nitrogen

'

Control Valves," containment isolation valve CV-31342 (Reactor

,

Makeup Water to Unit 2 Containment) exceeded its maximum allowable

1

time to close. As a result, CV-31342 was declared inoperable.

l

4

Technical Specification (TS) 3.6.C.3 states that with one or more

valves listed in Table TS 4.4-1 inoperable, within four hours:

-

(a) restore the inoperable valve (s) to operable status, or (b)

deactivate the operable valve in the closed position, or (c) lock

closed at least one valve in each penetration having one _

j

inoperable valve. Table TS 4.4-1 lists containment penetration

a

No. 45, Reactor Makeup to PRT, which includes CV-31342.

To comply

,

3

i

~ l

. - . . - - ,

- . _ , _ .

-

_

_

.

-

~-

. -.

. _ - _

-

.

-

--

.__

-.

.

-

.

with Technical Specification (TS) 3.6.C.3, CV-31342 was shut and'

its air supply was lockwired closed.

Safety tags, which are used

to administratively control equipment status, were placed on both

the control switch. in the control room and the air supply

isolation valve for CV-31342.

On April 5, 1993, No. 45 containment penetration upstream

- i

'

isolation valve 2RM-8-4 (Supply to PRT) was closed and normally

capped vent valve 2RC-9-4 (penetration leak test connection) was

verified closed. This established dual / redundant isolation.

Safety tags were attached to each of these valves. On April 9,

1993, the system engineer requested control room operators to

stroke CV-31342 for troubleshooting purposes.

The Unit 2 shift

supervisor (SS) determined that valves 2RM-8-4 and 2RC-9-4 should

be lockwired closed to ensure compliance with TS 3.6.C.3 before

cycling CV-31342.

2RM-8-4 was lockwired closed, however, 2RC-9-4

'

could not be lockwired because there was no hole in the valve

handwheel to pass the lockwire through.

A maintenance work

request was initiated to drill a hole in the valve handwheel for

2RC-9-4.

,

On April 13, 1993, after maintenance personnel had completed

drilling a hole in the valve handwheel, the system engineer

,

requested that 2RC-9-4 be lockwired so that CV-31342 could be

stroked. The system engineer removed the isolation and

restoration (I&R) sheet that listed valves 2RC-9-4 and 2RM-8-4

from the Unit 2 shift supervisors 1&R record book, circled 2RC-9-

4, and added a note to install lock wire.

The I&R sheet that

contained the air supply isolation valve and control switch for

CV-31342 was also removed from the 1&R record book.- The Unit 2 SS

gave both I&R sheets to the Unit 2 reactor operator (RO) and

provided verbal instructions to install lock wire on 2RC-9-4, to.

remove the safety tag from the air supply' isolation valve for

CV-31342 and then open that valve, and to remove the safety tag on

i

the control switch for CV-31342.

The Unit 2 R0 then contacted the

.

Auxiliary Building Operator and requested that he come to the

control room to perform a valve restoration.

The R0 gave both I&R

.!

sheets to the Auxiliary Building Operator with instructions to

remove the safety tag on the air supply isolation valve and open

the valve and to install lock wire on-2RC-9-4.

At approximately

11:00 a.m., the Auxiliary Building Operator removed the safety tag.

-

and opened the air supply isolation valve for CV-31342.

He then

removed the safety tags for 2RM-8-4 and 2RC-9-4, cut the lock wire

,

off of 2RM-8-4 and opened the valve.

(Note: With 2RM-F-4 open and

l

CV-31342 no longer disabled, action requirements of TS 3.6.C.3

i

came back into effect.)

,

The Auxiliary Building Operator then installed lock wire on 2RC-9-

.

4 as indicated on the I&R sheet.

He then called the control room

!

and system engineer and reported that the reactor makeup

restoration was complete. Apparently, the Auxiliary Building

Operator misunderstood the directions he had received from the R0

,

4

t

1

_

and assumed he was making a routine system restoration after

maintenrnce. At this time the Unit 2 R0, Lead Plant Equipment

Operator (LPED), and SS and the system engineer-thought that both

2RM-8-4 and 2RC-9-4 were lockwired closed with safety tags hung.

j

At approximately noon, SP 2272 was performed and CV-31342 cycled.

The stroke time for this valve was within the specified acceptance

criteria. After completing the surveillance procedure, CV-31342

-i

was left in the open position. However, CV-31342 was not declared

-

operable. At about 5:00 p.m. while preparing for ' shift turnover,

the Unit 2 LPE0 noted that the system engineer had not informed

the control room of the current status of CV-31342.

The Unit 2 SS

i

!

decided to shut the valve.

During shift turnover, the Unit 2 SS,

R0, and LPE0 each reported to their respective reliefs that CV-

31342 was closed and still considered inoperable, that the air

supply isolation valve for CV-31342 was open, and both 2RM-8-4 and

i

2RC-9-4 were lockwired closed.

'

At approximately 12:30 a.m. on April 14, 1993, a control room

operator making a plant tour decided to check the status of the

>

CV-31342 containment penetration. The operator found the air

supply isolation valve for CV-31342 open, 2RM-8-4 open, 2RC-9-4

lockwired closed, and safety tags on 2RM-8-4 and 2RC-9-4 removed.

.

The Unit 2 SS instructed the operator to close and lockwire

2RM-8-4.

This re-established conditions required by TS.

'

Administrative control of containment isolation valve 2RM-8-4 was

lost for approximately 13% hours from 11:00 a.m. on April 13 to

12:30 a.m. on April 14, 1993.

During this 13% hour period

containment integrity was maintained by the redundant containment

isolation valve for containment penetration No. 45, 2RC-3-1

(Reactor Makeup to PRT check valve). The failure to maintain

either 2RM-8-4 locked closed or CV-31342 closed with its

associated air supply isolated is considered a violation of TS 3.6.C.3. (50-306/93008-01(DRP)).

The inspectors reviewed the Error Reduction Task Force (ERTF)

report generated for this event and discussed the apparent causes

for the T.S. violation with the licensee.

Poor communications

between the system engineer, shift supervisor, and control room

operators was one of the primary causes of this event.

The use of

j

safety tags issued by the SS rather than a work request to

maintain administrative control of 2RM-8-4 and 2RC-9-4, caused

{

confusion concerning the status of containment penetration No. 45.

I&R sheets did not contain specific conditions for removing'the

isolations or indicate that the purpose of the isolation was' to

maintain containment integrity. The inspectors reviewed'the

Licensee Event Report (LER) submitted by the licensee for this TS

violation and concluded that the planned corrective action,~as

documented in the LER, does not sufficiently address all of the

apparent causes for this violation. The inspectors requestad the

5

.,

,

--

-.

.

.-

- - - .

i

f

1

.l

licensee to describe its comprehensive corrective action to

prevent recurrence in its response to the associated Notice of

Violation.

c.

Train A Hydroaen Monitor Lockup due to Hiah Ambient Temperature

,

Train A hydrogen monitor is located in 480 Volt safeguards bus

,

room No. 120.

The hydrogen monitor is a Regulatory Guide 1.97

i

Category 1 Type A instrument and as such,.is required to be

j

seismically and environmentally qualified for the environment in

,

which it is expected to operate during a design basis accident.

Bus room 120 contains Unit 1 Train B 480 Volt safeguards buswork,

!

and Train A event monitoring (EM) equipment for both units. Two

unit coolers are installed in bus room 120, one from each train of

the safeguards chilled water system.

Both unit coolers are

i

'

safety-related and each cooler is sized to remove the maximum

postulated heat generation in the room;

i.e., train A cooler

'

(102A) to ensure the EH equipment is operable, and train B cooler

"!

(102) to ensure the switchgear is operable.

On April 5,1993, Panel 134 (power supply to unit cooler 102A) was

deenergized for maintenance on an associated motor control center

!

-

(MCC).

This resulted in removing unit cooler 102A from service.

l

After completing the MCC work on April 6, the licensee reenergized

Panel 134. The licensee expected unit cooler 102A to restart

based on review of electrical schematic and wiring diagrams during

i

preparation of the work request. However, starting'and' stopping

i

of this cooler is controlled by a magnetic starter which was not

i

identified on the drawings. To restart the. cooler after power has

been restored, the start pushbutton must be depressed. Contrary

l

to the licensee's expectation, unit cooler 102A did not restart

i

when power was restored to Panel 134. This was not recognized at

the time.

On April 7,1993, Panel 135 (power supply to unit cooler 102) was

deenergized for MCC work. This removed the only running cooler in

bus room 120 from service. As a result, ambient temperature in

the bus room began to increase. During a routine system walkdown,

,

the EM system engineer discovered the hydrogen monitor locked up

j

and noted that the room temperature was about 95 degrees

!

Fahrenheit. The system engineer notified the control room and a

-

work request was initiated to investigate the instrument failure

and high temperature condition. The connecting door between bus

i

rooms 110 and 120 was opened to reduce ambient temperature and a

l

fire watch was stationed. During the investigation, the reset and

i

start pushbuttons for unit cooler 102A were depressed and the

!

cooler started. The licensee also generated a nonconforming item

.

report (866) for the failure of unit cooler 102A to restart after

i

power was restored to- Panel 134.

'

,

i

6

.

%

.

.-

_

_

_ _ .

.

.

_

_

.

_

.

!

!

!

!

'

t

On April 8,1993, the inspectors noted the reactor log entry for

';

the failed hydrogen monitor. The inspectors questioned the

!

licensee. regarding the environmental- qualification of the EM

j

equipment installed in bus room 120. The licensee initially

stated.that the hydrogen monitor computer is designed to operate

I

in an ambient environment up to 120 degrees Fahrenheit, and that

the maximum ambient room temperature under an accident condition

would be 105 degrees. The inspectors questioned why the hydrogen

monitor had failed at a lower than expected temperature. The

licensee stated that there had been a previous history of the

hydrogen monitor locking up due to high ambient temperature and

i

decided to further investigate the apparent temperature

.'

susceptibility of this instrument.

After further review of the design specifications for the hydrogen

monitor, the licensee stated that the-instrument would operate-in

l

an ambient environment up to 105 degrees versus the prev._iously

i

stated 120 degrees.

Subsequent testing verified that the hydrogen

,

monitor would operate up to a temperature of 105 degrees inside

'l

the instrument rack that houses the hydrogen monitor. However,

-

since the instrument rack is not ventilated, the temperature

inside the instrument rack is 10-15 degrees higher than the

,

ambient room temperature.

The licensee's original statement that the maximum ambient room

t

temperature under an accident condition would be 105 degrees was

based on a calculation that used the design specifications of the

'

cooler. The calculation showed that for a cooler air inlet

temperature of 105 degrees, the temperature of the air leaving the

,

cooler would be 74 degrees. The licensee stated that this

calculation used rather conservative assumptions. The licensee

!

initiated an evaluation 'as part of its configuration management

follow-on item (FOI) assessment program to verify that one unit

i

cooler can maintain ambient temperature in bus room 120 at or

below 90 degrees, to account for the temperature differential

between ambient room temperature and the 105 degree internal

instrument rack limit. A calculation demonstrated this

capability. This calculation was based on a maximum air inlet

.)

temperature of 88.4 degrees assuming that the ambient room

-)

temperature would be between 66 and 88.4 degrees depending on.the

i

location in the room. Based on the results of this calculation,

the licensee cor.cluded that there was no operability concern

associated with the EM equipment installed in bus room 120. The

inspectors reviewed the licensee's calculations and concluded that

the licensee's operability determination was adequately supported.

The licensee noted that there is no specific Technical

Specification applicable to the safeguards chilled water system.

Technical Specification Interpretation (TSI) 3.13-6 regarding

control room cooling, discusses administrative controls for the

chilled water system to prevent temperature excursions relative to

equipment life concerns.

However, TSI 3.13-6 states that the

!

7

!

I

l

_

_

_

l

I

l

safeguards chilled water system is not required to maintain

equipment operability in any of the rooms that it serves.

This

statement appeared invalid, considering the apparent need for at

least one unit cooler in bus roon 120 to satisfy EM equipment

qualification requirements.

Further, during a plant tour, the inspectors noted that the unit

-

cooler for bus room 16 was removed from service. The cooler was

being relocated to another part of the room to support cable

routing for the station blackout / electrical systems upgrade

(SB0/ESU) project.

The inspectors reviewed the work request for

relocating the unit cooler. The work request contained a note

',

stating that removal of the unit cooler from service does not

affect the operability of bus-16 room components.

The inspectors

questioned the licensee regarding the impact of the out-of-service

unit cooler on the operability of 4KV safeguards bus No.16. The

l

licensee responded that a safety evaluation (No. 321) had been

performed to address the event of a loss of integrity of the

.

!

safeguards chilled water system due to a seismic event.

The

licensee stated that this safety evaluation provided a documented

'

justification for continued operation for a loss of the safeguards

chilled water system.

The inspectors reviewed safety evaluation

No. 321, F0I A0617 (Heat Removal Calculations for the Safeguards

Chilled Water System), and associated reference calculations.

.

Thse documents indicated that no equipment thermal limits would

.

be exceeded for equipment located in the 4KV switchgear rooms upon

a loss of the chilled water system.

However, for equipment in the

i

480 Volt switchgear and relay rooms, these same documents

,

indicated that thermal limits would be exceeded,. unless operator

action is taken.

This action would include shedding equipment

loads to minimize heat generation and opening room doors to

,

'

provide supplemental cooling. The inspectors concluded that the

relationship of the chilled water system to switchgear room

equipment operability, as stated in TSI 3.13-6 needs to be

reevaluated.

The licensee informed the inspectors that it would evaluate

i

current guidance in TSI 3.13-6 regarding operability of the

safeguards chilled water system in relation to 480 Volt switchgear

1

and relay room operability. The licensee also concluded that

,

further evaluation of EM equipment capabilities relative to

ambient room temperatures was needed. This is considered an

inspection followup item (50-282/93008-02; 50-306/93008-02)

pending the inspectors review of the results of the licensee's

evaluation.

d.

Defective Anti-Rotation Key in Motor-0perated Valves

The inspectors informed the licensee of a 10 CFR Part 50.72

notification by the licensee for the Kewaunee Nuclear Power Plant

involving a safety injection (SI) system recirculation valve to

the refueling water storage tank (RWST) which failed to close

8

.i

I

,

.

- --

-

-

-

-

. _ . . -

. .

,

,

during' dynamic motor-operated valve (MOV) testing.

The valve

failure was attributed to a broken anti-rotation device which

caused binding of.the valve stem.

The anti-rotation device

>

consists of an approximate 2.25 by 0.90 inch "L" shaped key that

fits into the valve upper yoke bushing and prevents the valve

shaft from rotating while allowing the shaft to traverse up and

down.

The subject valve is a two inch globe valve manufactured by

Vel an. The licensee for Kewaunee identified six broken

'

anti-rotation keys in the nine applications of this Velan globe.

valve in various safety related systems.

-

The licensee reviewed this potential generic problem under.'its

)

operating experience assessment program. The licensee identified ~

12 applications of the Velan globe valve in the SI system and 4

applications in the chemical and volume control system (CVCS).

The licensee noted that valve actuators for all of the SI-valves

were overhauled and then tested both statically and dynamically

during the 1992 dual-unit outage. To address concerns with loss

of thrust due to key interaction with the stem, the keys and

keyslots for each SI valve were inspected, cleaned, and

lubricated.

In addition, rough edges were eliminated.

During

this maintenance activity, the key for Unit 1 MOV SI-32067, SI to

Reactor Vessel, was broken during removal. * The licensee contacted

'

the valve manufacturer, Velan, since no spare part was available.

The vendor informed the licensee that replacement keys were being

i

manufactured from a different material than the original hardened

440 C stainless steel due to brittle fracture concerns. 'Upon

receipt from Velan, a replacement key was installed in SI-32067,

i

This material change was implemented under Alteration 92A257

>

-which was reviewed by the Operations Committee-(onsite safety

i

review).

Following replacement of the broken key in SI-32067, two

,

additional keys were found broken in Unit 2 MOVs SI-32170, SI to

Reactor Vessel, and SI-32204, SI pump recirculation to RWST.

Both

were replaced.

For both keys, the break occurred at the 90 degree-

.

angle that connects the shorter leg to the longer leg.

Based on

r

the location of the break, the length of the key and keyslot, and

the arrangement of the keyslot in' the valve stem and yoke bushing,

,

i

the licensee concluded that the anti-rotation key would still have

performed its intended function. This operability determination

was made by engineering personnel based on discussion with those

individuals involved in the original outage maintenance activity

and did not involve the Operations Committee. While it is likely

that the Operations Committee would have reached a similar

conclusion, the inspectors were concerned that the Operations

Committee was not involved in the operability determination.

The

licensee strongly promotes the philosophy of empowerment in which

i

decision making is forced down to lower levels of management.

The

inspectors discussed with the licensee the need to ensure that an

appropriate level of management is involved in the decision making

.

process and that those individuals entrusted _ with making decisions

keep their respective supervisors informed.

9

!

.

.

._.-

-

- -- .

-

.

.

--

-

>

l

l

As part of its operating experience assessment, the licensee

'

checked the Nuclear Plant Reliability Data System (NPRDS) data

base for other reported failures of Velan globe valves to operate

i

due to a broken anti-rotation key.

No reported failures were

identified.

However, the licensee search of the NPRDS data base

is of limited utility in that sub-component degradation such as a

'

broken anti-rotation key, would not typically be reported unless

the degradation would have obviously prevented the component from

i

functioning.

Based on the fact that 12 of the 16 identified Velan

,

valves had recently been inspected, which involved cleaning and

lubricating the anti-rotation key, and then dynamically tested,

the licensee concluded that the 16 valves were operable.

This

operability determination was conducted by the Operations

Committee.

I

Based on a preliminary evaluation by the licensee for Kewaunee

that the reported anti-rotation key failure may have been caused

by low cycle fatigue, the inspectors expressed a concern that the

dynamic testing conducted during the recent dual-unit outage may

have imposed sufficient stress on the subject valves to cause the

associated anti-rotation key to fail.

The broken key could then

potentially prevent the valve from operating upon demand. As a

result, the licensee decided to visually inspect selected,

normally closed valves for evidence of key failure. The long leg

of any broken "L" shaped key would slide down tiie key slot and

become visible below the yoke bushing.

The licensee conducted at-

power entries into Unit I and Unit 2 containment to verify key

integrity of certain valves in the CVCS and SI system. The

inspectors accompanied the licensee's MOV engineer to' inspect

three valves in Unit 2 containment: MV 32172 - SI to Reactor

Vessel, MV 32170 - SI to Reactor Vessel, and MV 32235 - RHR to

'

Reactor Coolant System- Letdown.

The keys for MV 32170 and MV

32235 appeared intact. The licensee was not able to inspect MV

32172 since it was inaccessible due to high radiation levels.

The

licensee plans on inspecting this valve during the next refueling

outage.

Based upon verification of key integrity for other

valves, the licensee concluded there was a high degree of

,

confidence that MV 32172's key was intact.

The licensee for Kewaunee submitted a 10 CFR Part 21 report for

the anti-rotation device failure in the Velan globe valves. The

inspectors did not have any further questions regarding this

issue.

e.

Pressurizer Heater Control Power Selector Switch Mispositioned

j

Unit 1 pressurizer heater group B can be powered from either bus

120 (safeguards power supply) or bus 180 (non-safeguards power

supply).

Heater group B receives power from 480 Volt motor

control center (MCC) 1RI.

A transfer switch is used to power MCC

1R1 from either bus 120 through breaker 124 or from bus 180

through breaker 181.

Control power to breakers 124 and 181 is

10

'l

-

-

, .

, ..-

.

- . .

. .

.

.

$

- provided through selector switch CS-19328, located in the control

rod drive room.

Pressurizer heater group B is normally aligned to -

!

,

bus 180 with CS-19328 and the 1R1 transfer switch-each in the bus

180 position.

In this coniiguration, breaker 181 would be shut

!

'

and breaker 124 would be open.

1

On April 28, 1993, the Unit 1 Plant Attendant entered the Unit I

control rod drive room and noticed both bus 120 and bus 180

indicating lights on CS-19328 lit.

The operator found CS-19328

selected to the bus 120 position and the IR1 power supply transfer

switch selected to the bus 180 position. The operator notified

the control' room and was instructed to place CS-19328 in the bus

180 position. After switching CS-19328 to'the bus 180 position,

the operator noticed that both indicating lights on CS-19328 were

still lit. He then checked the position of breakers 124 and 181'

and noted that they were both closed. The operator notified the

control room of the breaker positions and was instructed to open

breaker 124. After opening this breaker, the operator noted that

only the bus 180 indicating light remained lit.

-

On April 29, 1993, the inspectors noted a reactor log entry for

.

the abnormal pressurizer heater control power selector switch

(CS-19328) and 1R1 power supply transfer switch lineup.

The

inspectors questioned the control room operators on the effect

this abnormal switch lineup would have on control of the

pressurizer heaters. The licensee determined that with this

'

switch lineup, all manual and automatic controls for the group B

pressurizer heater were disabled. The heaters would not have

deenergized on a low pressurizer level, resulting in potential

',

damage to the uncovered heaters. No indication of the

-

micpositioned centrol power selector switch was available in the

control room.

Control room operators would likely not have become

aware of this condition until an attempt was made to deenergize

the heaters. The licensee conducted an ERTF review of this event

but was unable to determine how or when the abnormal switch lineup

occurred. The inspectors reviewed the ERTF report and discussed

-

the results of this review with the licensee.

There are five groups of pressurizer heaters; one group of

,

variable heaters (C) and four groups of backup (A,B,D, and E)

heaters. The backup heaters cycle between 2210 and 2218 psig.

If

a transient occurred res'11 ting in a reactor coolant system (RCS)

pressure increase and pressurizer heater group B did not

deenergize at 2218 psig, the pressurizer spray valve would begin

i

to ramp open at 2260 psig to reduce RCS pressure.

If a

loss-of-offsite power occurred pressurizer heater group A

(safeguards) and pressurizer spray would both be available. - If

heater group B was needed to control pressure, operators would

have to align CS-19328 and the IRI power supply transfer switch to

the bus 120 position.

This same action would be required if the-

original switch lineup had been correct. The inspectors concluded

that the abnormal switch lineup for the B group of pressurizer

11

p

y

v

---

,

_

_

_ _

.

heaters had minimal safety Significance. However, the inspectors

expressed a concern for the apparent lack of a questioning

attitude regarding the potential operatioral impact of this

off-normal condition.

The inspectors discussed this issue with

the licensee. The inspectors noted that the licensee has taken

-

action to communicate to the operations staff the need for a

questioning attitude when an off-normal condition is discovered.

The inspectors will evaluate the effectiveness of this action

during their ongoing inspection activities.

One violation and one inspection followup item were identified. No

deviations or unreselved items were identified.

2.

Maintenance Observation (71707. 37700. 62703)

Routine preventive and corrective maintenance activities were observed

)

to ascertain that they were conducted in accordance with approved

procedures, regulatory guides, industry codes or standards, and in

conformance with Technical Specifications. The following items were

considered during this review:

adherence to Limiting Conditions for

Operation while components or systems were removdd from service,

approvals were obtained prior to initiating the work, activities were

accomplished using approved procedures and were inspected as applicable,

functional testing and/or calibrations were performed prior to returning

components or systems to service, quality control records were

,

maintained, activities were accomplished by qualified personnel,

!

radiological controls were implemented, and fire prevention controls

were implemented.

!

Portions of the following maintenance activities were observed or

'

reviewed during the inspection period:

a.

Bus 16 CT-11 Source Breaker Relay Gl"

Scement. On May 19,

1993, the licensee identified that th g us. cover plate for the C

'

phase time overcurrent relay on the C1 1] cf1 ite power source

breaker for Unit I safeguards bus 16 was .

.

Bus .16 can also

receive offsite power from the IRY transformer and via 'a manual

bus-tie from Unit 2 bus 26 (alternate AC source).

.

Once identified, the licensee promptly-began'an investigation to

i

evaluate operational consequences of the cracked glass, the cause,

,

and possible time of occurrence. The licensee examined and tested'

'

the relay to determine if, when the glass broke, if there were any

shards of glass interfering with relay operation or if the relay

was damaged in any other way. The relay was clean and intact, and'

was tested satisfactorily.

The licensee's investigation of how the glass was broken or

exactly when it was broken was inconclusive.

Scaffolding was

present in the vicinity of the bus to support SB0/ESU modification

activities in the bus room, but no particular incident was

identified as the possible cause for the broken cover glass.

12

4

l

,, _ , _

.-

,

.

-

- -

. .

.

.- J

. _ .

1

.

,

b.

Non-Safeguards Chilled Water System Modification.

+

c.

Repair of No. 12 Charging Pump suction stabilizer and desurger.

,

No violations, deviations, unresolved items or inspection followup items

were identified.

3.

Surveillance (37700. 61726. 71707)

The inspectors reviewed Technical Specification required surveillance

testing as described below, and verified that testing was performed in

accordance with adequate procedures, test instrumentation was

calibrated, and Limiting Conditions for Operation were met.

The

inspectors further verified that the removal and restoration of affected

.

components were properly accomplished, test results conformed with

Technical Specifications and procedure requirements, test results were

reviewed by personnel other than the individual directing the test, and

deficiencies identified during the testing were properly reviewed and

,

resolved by appropriate management personnel.

Portions of the following test activities were observed or reviewed:

a.

SP 1106C, "121 Cooling Water Pump Test." At a meeting of the

Operations Committee (onsite safety review), a member of the

i

engineering staff presented an issue regarding the apparent

degradation of No. 121 CW pump performance.

As part of the

SB0/ESU project, No. 121 CW pump was provided with a Class IE

power supply and it was designated a safeguards pump and included

in TS.

This occurred following completion of the 1992 dual-unit

outage.

Following the completion of CW header and annubar

!

replacement work after the 1992 dual-unit outage, SP 1106C, "121

,

Cooling Water Pump Test," was performed.

During the performance

i

of this test, the licensee observed that the pump was operating

about 11 percent below its pump performance curve (10 percent.

degradation defines the " alert" threshold).

Flow measurement

instrumentation was recalibrated and when SP 1106C was

!

subsequently performed, pump performance was in the acceptable

range.

However, the licensee believes that it will not take much

additional pump wear before No. 121 CW pump is degraded to the

point where it can no longer be considered a safeguards pump.

This pump was last replaced in 1989 and there is a spare pump

available onsite which could be installed. in about 5-7 days. The

timetable for pump replacement is dependent upon temperature

considerations (affecting demand for CU flow) and ASME Code.

testing requirements.

If the pump is not operable from a safeguards point of view, it

may still be available for normal operation.

However, TS state

that four out of the five CW pumps are required to be operable

except that two of the five pumps may be inoperable for 7. days.

The decision of whether or when to replace the pump had not yet

been made at the conclusion of the inspection period.

j

13

)

i

l

!

b.

SP 1106B, "No. 22 Diesel Cooling Water Pump Test."

c.

SP 2272, " Quarterly Cycling of PRT Reactcr Makeup Water and

Nitrogen Control Valves."

No violations, deviations, unresolved items or inspection followup items

'

were identified.

4.

Enaineerina' and Technical Support (377001

a.

Spent Fuel Pool Covers and Spent Fuel Crane

The spent fuel storage pool at Prairie Island is a two compartment

(interconnected) pool.

Pool No.1 is located in a position that

is in the load path of the auxiliary building crane (125-ton rated .

!

load).

Pool No.1 is provided with three, sectional protective

covers which allow loads up to 24,800 pounds to be transported (at

,

a maximum height of 6 inches) through the spent fuel enclosure

j

when fuel is stored in pool No.1, to preclude damage to the fuel

if tnere is a crane failure.. The covers also provide protection

for fuel. in pool No. I when maintenance is being performed on pool

No. 2.

In 1992, the licensee installed a new spent fuel crane in the

spent fuel pool enclosure. This crane has two hoists, designated

the East hoist and the West Hoist. The East hoist is a 2-ton

capacity hoist, used for general fuel handling and Unit I

refuelings.

The West hoist is a redundant, 3-ton design-rated

load, 3700-pound maximum critical load (MCL) hoist, intended to be

i

used for general fuel handling, Unit 2. refuelings, and lifting

heavy loads.

The crane with its West hoist is single-failure-

i

'

proof, meeting the criteria described in NUREG-0554, " Single-

Failure P oof Cranes for Nuclear Power Plants," and NUREG-0612~,

" Control of Heavy Loads at Nuclear Power Plants," for a load of up

to 3700 pounds.

Prior to installation of the new crane, the licensee used a non-

single-failure proof crane consisting of two 3-ton capacity hoists

i

for movement of heavy loads such as the pool covers.

The NRC

'I

approved this crane as acceptable for use for movement of the pool

covers in correspondence relating to Generic Letter 81-07,

" Control of Heavy Loads," if procedures were-in place such that

the covers were not raised to a height greater than 6 inches and

such that the ends of the covers were maintained over the edge of

the fuel pool and over the floor at all times'.

During a maintenance activity'on April 13, 1993, which required

ac ass to Pool No.1, the licensee discovered that the actual

weight of each spent fuel pool cover, as measured by a load cell,

was approximately 4550 pounds (not including approximately 250

)

pounds of rigging). This was in excess of the historically

assumed weight of 3700 pounds.

The assumed weight of 3700 pounds

14

<

-

-

_

..

_

_

__.

_ . _ _

_

_

_

_ -_

,

k

was a calculated value based on the drawing details of a 1977

construction drawing. The licensee, therefore, procured its

single-failure proof crane based on an erroneous value for the

-

weight of the MCL.

Before this. discrepancy was discovered, the

single-failure proof crane (with a MCL rating of about 1100 pounds

less than the actual weight of the covers plus rigging) had been

'

used on four occasions. However, because the actual weight of the

covers plus rigging was still less than the normal capacity of the .

hoist (3 ton), and the other administrative controls on load path

of the covers was maintained, the probability of dropping the

covers on the fuel was low.

Following its review of this event, the licensee has revised its

procedure 058, " Control of Heavy Loads," to again require two,

3-ton hoists when moving the pool covers over fuel. Also,

,

controls on the lift height and overlap are still required. This

method is consistent with the licensee's original NRC-approved

method of transporting heavy loads in the spent fuel . pool

enclosure with the exception that the actual weight lifted is

about 1100 pounds greater than that originally evaluated. This

'

increased weight, however, is still within the dual-hoist

arrangement capacity of 6 tons.

The inspectors concluded that an inadequate review of the design

assumptions used to determine the weight of the spent fuel pool

covers resulted in the licensee qualifying the spent fuel crane as

,

single-failure proof for an MCL less than the actual weight of the

covers.

b.

Primary Water Stress Corrosion Crackina (PWSCC) of Control Rod

Drive (CRD) Penetrations

,

In November 1991, the licensee was notified that cracks had been

I

found on a CRD penetration on the reactor vessel head at a plant

located in France (reference NRC Inspection Report 50-

282/91024(DRP);.50-306/91024(DRP)).

The mechanism of degradation

was determined to be PWSCC. This issue received prompt attention

by the NRC and groups within the U.S. nuclear industry represented

l

by the Nuclear Utilities Management and Resources Council

(NUMARC), Electric Power Research Institute (EPRI)', the

i

pressurized water reactors (PWR) Owners Group, and the

'

Westinghouse Owners Group, in order to ascertain whether there was

an immediate safety concern for nuclear. reactors in this country.

Several meetings have been conducted between the NRC and these

groups and safety evaluations (SEs) have been performed with the

conclusion that this issue does not present an immediate safety

hazard. Northern States Power has used:an SE. performed by

-

Westinghouse, .which envelops the Prairie Island reactor . vessels,

in performing its own SE (SE No. 343) to provide justification for

continued safe plant operation.

15

j

-

-

-

..

-

.--, , -.

.

..

. - .

- - ..-

.

_

.-

-. . - . - -

h

Additional meetings are planned between the NRC and the industry

groups. Also, plans for performing inspections of CRD

penetrations using non-destructive examination techniques are

being developed and scheduled, and techniques are being studied

for the mitigation of PWSCC. Although the NRC agrees.that CRD

penetration cracking is not a significant safety issue at this

-

time, the NRC considers this a serious matter and additional

information or future events could cause a reassessment of the

safety significance of the cracking.

No violations, deviations, unresolved or inspection followup items were

identified.

5.

Radioloaical Controls (83750)

Radiological control practices were observed.to ascertain if they were

performed in accordance with regulatory _ requirements.

No problems were

'

noted in this area during the inspection.

Controls on the radiological

condition of the plant remained essentially unchanged from previous

inspection periods and were excellent. The dose expended for the year

,

through the end of the inspection period was under the licensee's

estimate and vary low at approximately 11 person-rem.

The following specific items were observed during the inspection period:

.

a.

As of April 1,1993, the licensee changed vendors for

thermoluminescent dosimeter (TLD) processing. The vendor will

report doses at 7, 300, and 1,000 milligrams per square

centimeter, which conforms to_ dose reporting requirements of 10 CFR Part 20, Revision 1.

TLDs will now be processed quarterly

instead of monthly. The licensee's TLD quality assurance program

will consist of verifying the vendor's ability to produce accurate

and precise results for TLDs exposed to known gamma, beta, and

neutron sources. The inspectors verified that the new TLD vendor

held current personnel accreditation from the National Voluntary.

Laboratory Accreditation Program of the National Bureau of

Standards for each type of radiation for which personnel are to be

monitored.

No problems were noted.

b.

The inspectors reviewed an audit report (AG 92-38) conducted by

the licensee's power supply quality assurance organization. The

audit reviewed the licensee's performance during the dual-unit

outage which was completed in early 1993.

Specific to radiation

protection, one finding was issued with regards to. contamination

control (FG 92-42), which discussed problems encountered during a

letdown system modification and the observance of some personnel

not frisking upon exit from the radiologically controlled area.

The problems identified during the letdown modification were

discussed in a previous NRC Inspection Report (50-282/92028(DRSS);

50-306/92028(DRSS)), and the licensee's assessment of the event

was similar to the NRC's assessment.

16

.

y..

-

y,,-_

, . . -

,.

,.

. . . - . . . . -

w.

.-

No violations, deviations, unresolved items or inspection followup items

were identified.

6.

Licensee Followup on Previousiv Identified Items (92701. 92702)

a.

(Closed) Unresolved item 50-282/93002-02:

Ali four Nuclear

Instrumentation System (NIS) bottom detector flux (Q bottom)

isolation amplifiers were miscalibrated.

The top and bottom detector flux signals are used to calculate the

overtemperature delta temperature (OTAT) and overpower delta

temperature (0 PAT) reactor protection system trip setpoints.

The

Prairie Island FSAR/USAR, Chapter 14, Design Basis Events, uses

these setpoints as primary trip functions for uncontrolled rod

cluster control assembly withdrawal at power (slow rate) and a

chemical and volume control system malfunction at power.

Technical Specifications (TS) 2.3.A.2.d (OTAT) and 2.3.A.2.e

(0 PAT), " Limiting Safety System Settings, Protective

Instrumentation," specifies a delta flux [F(4I)] penalty be

applied for each percent that the magnitude of Al (Q top - Q

bottom) exceeds +9 percent.

The AT trip setpoints are

automatically reduced by an equivalent 2.5 percent of rated

thermal power at this point.

Based on the miscalibration, the AT trip setpoints would not begin

automatic f(41) reduction until +15 percent.

The 4T trip

functions (channel dependent) would remain nonconservative until

the penalty ramp intersected the TS trip function at a worst case

f(AI) of +38 percent (see Figure 1 below).

The licensee identified the miscalibration on February 4, 1993,

during the periormance of surveillance test SP 1007, " Nuclear

Power Range Functional Test."

Subsequent root cause investigation

identified that the four Q bottom isolation amplifiers were

miscalibrated on January 22, 1993, during the performance of

surveillance test SP 1006B, "NIS Power Range Axial Offset

Cal i brati on . "

The inspectors concluded the following conditions contributed to

the miscalibration:

(1)

Permanently installed test lead NIS-3 was used during the

calibration and was not labeled as having an internal surge

suppression network.

The network caused each Q bottom

amplifier's output to read approximately 10 percent high.

The instrument technician was unaware that NIS-3 contained a

suppression network and followed existing procedure steps in

adjusting each Q bottom amplifier within its required output

value.

(2)

The instrument technician adjusted each Q bottom amplifier

without questioning the adjustment range.

Typically, no

17

T

,

[

?

I

g

adjustment is required.

In addition, the technician did not

notify plant supervision that a significant adjustment had

been made to all four Q bottom amplifiers.

(3)

Even though procedure SP 1006B was used successfully for

approximately 18 years, the procedure permitted an internal

adjustment to be made with only a signoff that the step had

been completed satisfactorily.

The_ licensee implemented the following corrective actions: (a) the

test leads were properly labeled for both units; (b) procedure SP

1006B was revised to notify the system engineer or plant

supervision prior to making any internal NIS adjustments; and (c)

the event was discussed with the instrument technicians

emphasizing the need for self-checking and the need for

-

questioning a calibration shift outside of the acceptance

criteria.

The inspectors concluded the licensee's actions were

satisfactory.

The inspectors concluded that the miscalibration had minimal

safety significance. Diverse backup trip functions, such as high

neutron flux overpower, high pressurizer pressure, and high

pressurizer level, were operable.

During the out of calibration

period, the largest f(AI) experienced was 7.67 percent. The

operators attempt to maintain the target flux difference between

3.31 percent i 5 percent when operating above 50 percent power.

The licensee modeled the two Chapter 14 events by applying the

f(AI) penalty at +20 percent (see figure).

In both design basis

events, no core safety limits were exceeded.

,

>

r

18

__

Figure 1

QL Signal Miscalibration - Prairio Island

120.000

Msca!!bration

k,'.-

100.000 -@

50%,,', %

~

-

a

Y'S'

.

80'000 I

T.S.

/

1,50 %

-

1.10 %

60.000 -

%s

.'

"

k

'

-

%

~,-

,

E 2.60%

'

'

40.000

.-

, . -

g-

,','

20.000

,'

,

. . _

.

- W.Vvw

-

i

e

50

-40

-30

-20

-10

0

10 T 20 \\ 30

40

50

15%

Ar'Mysis PCht

ddta41%)

i

19

,

.

Technical Specification 2.3. A.2.d (OTAT) and TS 2.3. A.2.e (0 PAT)

require that for each percent that the magnitude of *I (Q top - Q

bottom) exceeds +9 percent, the AT trip setpoints be automatically

reduced by an equivalent 2.5 percent of rated thermal power. The

i

licensee operated in a condition where the OTAT and OPAT reactor

trip setpoints would not have been automatically- reduced when al

exceeded +9 percent.

Failure to meet the requirements of TS 2.3.A.2.d and 2.3.A.2.e is considered a violation

(50-282/93008-03(DRP)). The inspectors were particularly

concerned with this violation because one individual adjusted four

redundant reactor trip channels out-of-specification without

questioning the magnitude of adjustment or informing appropriate

licensee staff and without any management oversight or review.

The inspectors discussed this issue with the licensee emphasizing

,

the need for broadly focused and comprehensive corrective action

'

to identify any potential similar situations.

b.

(Closed) Inspection Followuo Item (50-282/93002-01:

50-306/93002-01):

NRC Inspection Report 50-282/93002(DRP);

50-306/93002(DRP) discusses the quality assurance (QA)

classification of valve stem bushings in flow control valves. of

the residual heat removal (RHR) system.

The licensee has

classified the RHR system as ASME Code Class 2, and has designated

RHR system flow control valves as safety-related, QA level 1.

However, the subject bushings are considered non-safety related,

QA level III. The inspectors questioned the licensee regarding

the apparent QA classification of these bushings.

The licensee

f

stated that RHR system flow control valves are considered safety

related, pressure retaining valves, and as such, in accordance

with ASME Code Case N-62-2, " Internal and External Valve Items",

various internal valve components that are not related to the

pressure retaining function of the valve, can be considered

non-safety related, QA level III. As documented in NRC Inspection

Report 50-282/93002(DRP); 50-306/93002(DRP), the inspectors

concluded that since the RHR system flow control valve bushings

are not related to the pressure retaining function of the parent

valve, classification of these bushings as QA-level III appears

justified. However, based on administrative controls referenced

in Corporate Nuclear Administrative Control Directive NIACD 1.3,

and Operations Manual procedure H1-A, all internal valve

,

components for Q-listed valves are by definition QA-level 1,

absent a documented review stating otherwise.

The licensee stated that although a specific technical evaluation

had not been performed per HlACD 1.3 and procedure H1-A in

determining the quality classification of the RHR system flow

control valve bushings, safety evaluation No. 257, dated January

20, 1991, adequately documented a basis for considering these

bushings as QA level III.

The inspectors reviewed safety

evaluation No. 257 which was prepared to clarify procurement

requirements.for various internal valve and pump parts such as

flexitallic gaskets, packing, and mechanical seals.

The safety

l

20

i

I

)

.

-

- .

-

- - -

- - - - -

_,

.

-

.-

.-

_.

..

,

i

'

evaluation references subsections NB, NC, and ND of the ASME Code

'

(1980 Edition) and associated articles NB-2000, NC-2000, and

ND-2000 that define material requirements for Code Class 1, 2, and

3 components, respectively.

In discussing material requirements

for pressure retaining components, the subject safety evaluation

,

references the following statements common to each of the NB-2000,

!

NC-2000, and NC-2000 articles.

"The term pressure retaining

material as used in this subsection applies to items such as

'

vessel shells, heads, and nozzles; pipes, tubes, and fittings;

valve bodies, bonnets, and disks; pump casings and covers; and

bolting which joins pressure retaining items. The requirements of

l

this article do not apply to items not associated with the

pressure retaining function of a component, such as shafts, stems,

trim, spray nozzles, bearings, bushings,_ springs, and wear plates,

nor to seals, packing, gaskets, valve seats, and ceramic

insulating material and special alloys used as seal material in

electrical penetration assemblies."

'

Safety Evaluation No. 257 also references ASME Code Case N-62-2

q

which discusses rules for construction of internal and external

valve items other than valve bodies and bonnets.

The inspectors

-

reviewed this code case. The code case classifies valve

components into eight categories and states that material

manufacturers or material suppliers for Category 4 through 8 valve

,

items are not required to comply with Section III Part NCA-3800,

" Metallic Material Manufacturer's and Material Suppliers Quality

.

System Program," of the ASME Code. The code case lists shaft

bearings (bushings) as a Category 7 item and therefore, these

bushings are not subject to Code requirements for material

i

traceability.

Based on review of safety evaluation No. 257 and

'

ASME Code Case N-62-2, the inspectors concluded that

classification of the RHR system flow control valve bushings as QA

level III is justified.

l

The licensee stated that Operations Manual procedure H1-A would be

-

revised to reference ASME Code Cases N-119-4, " Pump Internal

Items," and N-62-2 in determining the quality classification of

'

internal components for pumps and valves, respectively, that

perform a pressure retaining function. The inspectors did not

have any_further questions regarding this issue.

This item is~

t

closed.

One violation was identified.

No deviations, unresolved or inspection

.

followup items were identified.

'

7.

Licensee Event Renort (LER) Followun (92700. 92701. 37700)

a.

(Closed) LER 50-282/92007: Design basis reconstitution effort

!

identified a condition outside the plant design basis.

The licensee identified.in a 1992 Design Basis Reconstitution

Effort finding that emergency diesel generator (EDG).D1 was

t

'

21

\\

1

1

.

.

-

-

-

, - -

-.

.

-

.

-

. . -

-

- _ .

,

potentially vulnerable to damage due to a tornado-driven missile.

Incapacitation of EDG D1 due to a tornado and an assumed single

failure of EDG D2 could have resulted in a loss of all AC power.

-As discussed in NRC Inspection Report 50-282/92011(DRP);

50-306/920ll(DRP), the licensee installed an interim missile

barrier, pending the completion of a detailed analysis of the

as-built configuration.

The inspectors reviewed the licensee's safety evaluation,

No. 328 - Addendum 1, "D1 Generator Tornado Missile Protection,"

u

and Calculation Gen-PI-002, Rev.1, "Probabilistic Risk Assessment

'

of D1 EDG Room Door Vulnerability to Tornado Missiles," and the

NRC's Standard Review Plan. The Standard Review Plan identifies

that 10 CFR Part 100 requirements are met if the probability of

site proximity missiles impacting the plant and causing

radiological consequences greater than 10 CFR Part 100 exposure

guidelines is less than about 10" per year. The results of the

licensee's probabilistic risk analysis indicated that the

probability of incapacitation of D1 due to a tornado missile and

the simultaneous failure of D2 is about 10-* per year, a result

which indicates that the as-built configuration is acceptable.

The Operations Committee reviewed the safety evaluation and

requested that EDG availability be considered in addition to

reliability. This review, however, was not complete at the

conclusion of the report period.

Based upon the inspectors'

,

review of the LER, the safety evaluation, analyses, and

discussions with engineering staff, this LER is closed.

b.

(0 pen) LER 50-282/93006:

Automatic start of No. 121 Cooling Water

Pump on low header pressure while aligned for safeguards

'

operation.

At 3:24 p.m. (CST) on March 25,1993, No.121 motor-driven cooling

water (CW) pump started automatically on low header pressure while

aligned for safeguards operation.

The licensee was performing

surveillance test SP 1106B, "No. 22 Diesel Cooling Water Pump

Test," to satisfy post-maintenance testing requirements for No. 22

diesel-driven CW pump.

This event is further discussed in NRC

Inspection Report 50-282/93002(DRP); 50-306/93002(DRP).

The licensee's corrective action to prevent recurrence for this

event, as described in the LER, was to discuss the event with

those individuals involved in the weekly work planning meeting.

In addition, the licensee vill revise the surveillance procedures

j

for testing the diesel-driven CW pumps to. clarify the instructions

,

for disposition of the pump discharge header valves. The

j

inspectors will evaluate the adequacy of the licensee's corrective

actions during a future inspection.

c.

IClosed) LER 50-282/93007: Discovery that certain valves should

be subject to ASME Section XI testing.

22

'

-

_

,

,

.

-

-

-.

.. .- -

- - -

During a review of the feedwater system as part of the design

basis reconstitution program, the licensee identified that four

feedwater system valves required to mitigate the consequences of

an accident were not included in the ASME Section XI inservice

inspection and testing program.

Subsequent to this discovery

while developing the inservice inspection and testing program for

the third ten-year interval, the licensee identified.40 additional

valves that had not been included in the original program.

The

subject valves were originally classified as ASME Code Class MC

(metal containment) and were therefore not included in the

licensee's original inservice testing (IST) program implemented.in

1976. These valves should have been classified as ASME Code Class

2 valves. The licensee performed an evaluation, referenced = in the

LER, to determine if the failure to perform required Section'XI

testing for these valves constituted an operability issue. This

evaluation included valve position verification and a review of

historical data, testing and inspection results. The licensee

concluded that there was no operability concern with the missed

testing,

The licensee's corrective action for this event, as addressed in

the LER, will be to test the subject valves in accordance with

'

Section XI requirements during the next cold shutdown for the

respective units for 32 of the 44 valves.

The remaining 12 valves

will be tested by August 1,1993.

In addition, all 44 valves will

be included in the third ten-year IST program.

The failure to perform required ASME Section XI IST is an apparent

violation of Technical Specification 4.2.A.2 which states that IST

of ASME Code Class 1, 2, and 3 pumps and valves shall be performed

in accordance with Section XI of the ASME Boiler and Pressure

!

Vessel Code and applicable Addenda as required by 10 CFR Part 50,-

Section 50.55(g), except where specific written relief has been

granted by the NRC.

This issue will be reviewed by an NRC Region

,

III IST specialist during the next scheduled IST inspection. This

is considered an unresolved item 50-282/93008-04 pending an

evaluation of the safety significance and adequacy of the

corrective action addressed in the LER.

This LER is therefore

closed.

d.

(Closed) LER 50-306/93002:

Loss of administrative control of an

inoperable containment isolation valve due to personnel error.

This event is discussed in paragraph 1.b.

The inspectors will

evaluate the adequacy of the licensee's corrective action for this

event, as described in the licensee's response to the Notice of

Violation during a future inspection.

This LER is closed.

.

One unresolved item was identified.

No violations, deviations or

inspection followup items were identified.

23

-

-

.

-

.

.

.

-

. .

.

.. .

.

.

-

. -

- -

. -

8.

Contacts With Members of the Public (94703)

A management meeting was conducted at the Prairie Island Training Center

on April 23, 1993, to present the NRC's Systematic Assessment of

Licensee Performance (SALP) Report for Prairie Island.

Following the

meeting, the inspectors met wit l1 members of the public who were in

attendance. Two individuals requested information regarding issues

affecting the nuclear industry and their specific relevance to Prairie

Island.

These issues included the use of Thermo-Lag Fire Barrier

Material and primary water stress corrosion cracking of control rod

drive penetrations.

Copies of materials available in the NRC Public

-

Document Room such as NRC Bulletins, Information Notices, licensee

correspondence, inspection reports, and SALP reports were provided under

separate cover to the individuals.

The issue of PWSCC of CRD

penetrations is discussed further in paragraph 4.b.

B

9.

(Closed) AMS No. RIII-93-A-0009

The inspectors performed a review in response to concerns regarding the

inability to perform inspections of encapsulated welds in the main. steam

system and possible design deficiencies in the auxiliary building

ventilation system. The concerns were not substantiated.

,

a.

Encapsulated Main Steam System Welds

Section XI of the ASME Boiler and Pressure Vessel Code provides

rules that nuclear plant owners must follow for the inservice

inspection of plant components.

10 CFR 50.55a requires nuclear

plant licensees to adhere to the ASME Code.

However, in cases

,

where a licer,see has determined that it is impractical to conform

with a code requirement at its facility, it may request NRC-

approval for relief from the requirement.

The licensee requested relief from performing code-required;

inspections of certain welds in the main steam piping at Prairie

Island Units 1 and 2 that are inaccessible due to their-

encapsulation within sections of guard piping.

The NRC staff

reviewed this request for relief from inspection of these~ welds

,

and documented approval of the relief request, with certain

contingencies, in Safety Evaluations (SEs) dated

November 14, 1980, and December-28, 1984. -These SEs documented

NRC approval of the licensee's inservice inspection program per

the requirements of 10 CFR 50.55a.

The contingency imposed by the NRC in approval of the request for

.

'

relief from inspecting these encapsulated welds, was that the

licensee must perform a visual-inspection of the' surrounding area

to look for leaks during a main steam pressure test, to be '

,

conducted-at 3 1/3 year intervals.

The inspectors verified that

-

,

'

this inspection had been completed for both units within the

24

.

,m4

+

r

<y

g---

<

ver

i -- ' < - - -

,y

+ +-- er a

e-

required time interval. This visual inspection of the area,

combined with the routine code-required inspection of other welds,

provides reasonable assurance of continued safe plant operation.

b.

Auxiliary Buildina Ventilation System

The ventilation of the auxiliary building is provided by the

normal ventilation system and the auxiliary building special

ventilation system (ABSVS), a safeguards system.

The ABSVS serves

to collect and filter any potential post-accident coniainmr '

leakage before reaching the environment.

The normal venti.s ,i

system uses a fresh air supply and no filtration before ext.aust to

the environment.

If there is an accident, receipt of a high

radiation signal or a safety injection signal actuates the ABSVS,

trips normal ventilation system supply and exhaust -fans, and -

closes normal ventilation system supply and exhaust dampers. This

design provides for the collection and filtration, by the ABSVS,

of air in the auxiliary building before it is exhausted to the

environment.

No violations, deviations, unresolved or inspection followup items were

identified.

10.

Followup on Reaional Reouests

a.

Inadvertent Reactivity Insertion from Reactor Coolant Pump (RCP)

Restart

The NRC has recently issued NUREG/CR-5822, " Analysis of Thermal

Mixing and Boron Dilution in a PWR." This document identifies a

scenario which could result in an unintended positive reactivity

transient.

The scenario described a plant in the beginning of its

fuel cycle, in_ hot standby with RCPs running, and with a boron

dilution in progress. The analysis evaluated the amount of

thermal mixing and boron mixing that would occur if the RCPs

tripped and boron dilution continued via seal injection.

The

results indicated that boron mixing in the reactor coolant system

(RCS) would be minimal in these conditions because there would be

little flow due to natural circulation. An unborated slug of

coolant could develop and upon RCP restart, a significant positive

reactivity insertion could occur.

The inspectors reviewed licensee controls for precluding a similar

event from occurring at Prairie Island. The_ licensee's nuclear

analysis department has not performed a detailed analysis

regarding this'particular transient.

However, NRC Information

.

Notice (IN) 91-54, " Foreign Experience Regarding Boron Dilution,"

which was received by the licensee, discusses a scenario similar

to the one addressed in_NUREG/CR-5822. After reviewing the IN,

the licensee implemented procedural and administrative controls Lto-

preclude a similar event from occurring. These measures include:

25

I

1.

A precaution in the RCP operating procedure and a limitation-

in the unit startup procedure stating, "Do not restart a

tripped RCP if the trip occurred while dilution was in

progress, until sufficient time has elapsed to ensure

thorough mixing of the RCS."

2.

A precaution in the reactor makeup control system operating

i

procedure stating, "A minimum of one RCP or RHR pump.must be

operating during any boron dilution step."

3.

An initial action in the alarm response guide for RCS low

flow to "stop any dilution, if in progress."

Based upon review of the licensee's administrative controls, the

inspectors concluded that the licensee had implemented measures to

prevent this inadvertent positive reactivity insertion transient,

b.

Low Temperature Overoressure Protection (LTOP)

'

An issue was identified at another nuclear power plant involving

calculations to determine the setpoints for LTOP which did not

compensate for pressure drops due to piping and other components

between' the reactor pressure vessel and the pressure transmitters.

This issue had potential generic applications.for all Westinghouse-

PWRs.

The presence of improper /non-conservative LTOP setpoint

settings could allow an overpressure condition to exist which

could potentially cause brittle fracture of the reactor pressure

vessel.

The inspectors reviewed the licensee's engineering evaluation of

the applicability of this issue to the Prairie Island units. At

the plant at which this issue was identified, RCS pressure

transmitters are located in the intermediate leg of the RCS.

In

addition to accounting for instrument error and the pressure drop

associated with the hot leg and intermediate leg piping, this

location necessitates compensation for the significant pressure

drop across a steam generator. The pressure transmitters for the

Prairie Island units are located on the hot leg of the RCS.

'

Compensation for a steam generator pressure drop is therefore not

required.

The licensee's reactor vessel heatup and cooldown limit curves

contain a margin of 60 psig, intended to allow for instrumentation-

error. The actual pressure transmitter error value ' calculated by

the licensee is +/- 29.1 psig. The calculated pressure drop due

to the reactor vessel itself was determined to be about 20 psig,

and.the pressure drop from the hot leg piping to the transmitters

was considered negligible.

The combination of the instrumentation

error and pressure drops is still less than the margin inherent'in

the limit curves. Therefore, the licensee concluded the LTOP

settings are adequate. The inspectors concluded that the

licensee's review of this issue was adequate.

t

26

,

-_

_-

.-

.-- -.

.

. - - - - .

!

'

No violations, deviations, unresolved or inspection followup items were

identified.

11.

Safety Audit Committee Meetina (40500)

<

The inspectors attended portions of the licensee's Safety Audit

Committee (SAC) meeting on April 1, 1993. The SAC is the licensee's

offsite safety review committee and meets quarterly to discuss plant

events, organizational changes, iicense amendment requests and other

regulatory correspondence, quality assurance audits, and other various

.

items of interest.

During the April 1 meeting, the inspectors observed

!

discussions on the review of selected plant events for closecut, the

status of the station blackout / electrical systems upgrade project, the

response to Notices of Violation concerning security of safeguards

i

information, an investigation summary of fitness-for-duty concerns at

'

Prairie Island, and the annual security audit.

!

The inspectors noted that the meeting was characterized by an open

exchange of information, discussions were detailed and accurate, and

,

that the committee exhibited an appropriate safety perspective as

reflected in the nature of questions to the licensee's staff.

No violations, deviations, unresolved or inspection followup items were

identified.

I

12.

Independent Spent Fuel Storace Installation (ISFSI) (37700)

The inspectors reviewed activities associated with the construction and

planned operation of the licensee's ISFSI.

Review of the licensee's

application to operate an ISFSI under the regulations contained in

10 CFR Part 72 is the responsibility of the NRC's Office of Nuclear

l

Material Safety and Safeguards (NMSS) and is in progress. The

inspectors' activities included a review of the proposed technical

specifications for the ISFSI, (comments were forwarded to NRC personnel

,

in HMSS), and tours of the ISFSI construction site, including

,

observations of the construction of the earthen berm surrounding the

concrete ISFSI storage pads.

13.

Unresolved Items

Unresolved items are matters about which more inforriation is required in

order to ascertain whether they are acceptable items, violations, or

deviations. An unresolved item is discussed in paragraph 7.c.

14.

Inspection Followup Items

Inspection followup items involve activities which were not completed

within the inspection period, where additional inspection is necessary

and planned.

An inspection followup item is discussed in paragraph 1.c.

1

'

27

.

-

-

-

. - . - - - -

-

.

- - 0

,

i

)

,

15.

Manaaement Interview (71707)

The inspectors met with the licensee representatives denoted in

paragraph 16 after the conclusion of the report period on June 4, 1993.

The inspectors discussed the purpose and scope of the inspection and the

findings. The inspectors also discussed the likely information content.

of the inspection report with regard to documents or processes. reviewed

>

by the inspectors during the inspection. The licensee did not identify

,

any documents or processes as proprietary.

16.

Persons Contacted

E. Watzl, General Manager, Prairie Island

,

  1. M. Wadley, Plant Manager

K. Albrecht, General Superintendent, Engineering

  1. G. Lenertz, General Superintendent, Maintenance

R. Lindsey, Assistant to the Plant Manager

D. Schuelke,. General Superintendent, Radiation Protection

and Chemistry

J. Sorenson, General Superintendent of Plant Operations

G. Miller, Superintendent, Technical Support

  1. M. Reddemann, General Superintendent, Electrical and

Instrumentation Systems

  1. G. Rolfson, General Superintendent, Nuclear Projects Department
  1. J. Mcdonald, Superintendent, Site Quality Assurance
  1. A. Hunstad, Staff Engineer
  1. J. Hill, Superintendent, Instrumentation and Controls

Systems

  1. P. Ryan, Operations Shift Manager

M. Klee, Superintendent,. Quality Services

  1. J. Maki, Superintendent, Electrical Systems

.

E. Eckholt, Nuclear Support Services

  1. J. Leveille, Nuclear Support Services
  1. G. Aandahl, Superintendent Design Standards

C. Mundt, Production Engineer

J. Donatell, Production Engineer

S. Schaefer, Production Engineer

R. Waterman, Nuclear Engineer

  1. M. Dapas, NRC Senior Resident Inspector
  1. R. Bywater, NRC Resident Inspector

,

  1. Denotes those present at the management interview of June 4,1993.

I

L

v

28

,

_

__

_ _ . _ ,

1 --- -