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LER-1982-029, /01T-0:on 820222,steam Line Flow Instruments for a Main Steam Line,Channels 3 & 4, & B Main Steam Line,Channel 3,reported Inoperable During Startup.Caused by Lack of Power Supply Fuses to Transmitters.Fuses Replaced |
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2801982029R01 - NRC Website |
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ATTACIIMENT 1 SURRY POWER STATION, UNIT NO.1 DOCKET NO:
50-280 REPORT NO:
82-029/OlT-0 EVENT DATE:
02-22-82 TITLE OF THE EVENT:
F-474, F-475, and F-484 INOPERABLE 1.
DESCRIPTION OF EVENT
On 2-22-82, during unit startup following a maintenance outage, the instrument technicians reported that the power supply fuses to certain main steamline flow instruments were removed. The unfused condition rendered these steam-line flow transmitters inoperable. Reactor power was approximately 8% and reactor coolant average temperature was approximately 547' at the time of discovery.
The instruments affected were F474 and F475 serving "A" main steamline and F484 serving "B" main steamline.
Inoperability of the main steamline flow instruments with reactor coolant average temperature above 543' is contrary to Technical Specification 3.7.B.
Table 3.7-2.
This event is reportable per Technical Specification 6.6.2.a.(6).
2..
PROBABLE CONSEQUENCES OF OCCURRENCE:
Protection against a steamline break accident is brought about, in part, by actuation of the Safety Injection System which provides emergency cooling and a reduction of reactivity. Diverse instrumentation has been provided to sense accident conditions and to initiate the operation of the Engineered Safety Features.
Signals which provide automatic SIS actuation following steamline break accidents include:
1.
High steamline flow from 1 of 2 channels from 2 of 3 steamline in coinci-l dence with low reactor coolant average temperature.
Page 2 Report No. 82-029/0lT-0 2.2.
High steamline flow from 1 of 2 channels from 2 of 3 steamlines in coincidence with low steanline pressure.
3.
A 120 psig difference between 2 of 3 main steam header pressure channels and 2 of 3 pressure channels of 1 of 3 main steamlines.
4.
Containment pressure of 3 psig (due to the loss of high energy steam inside the containment).
5.
Low pressurizer pressure (due to the increased extraction of reactor coolant system heat).
The high steamline flow signals mentioned above also initiate closure of the main steam trip valves on all 3 main steamlines. Closure of these valves is designed to prevent blowdown of all 3 steam generators in the event of a break of 1 steamline. Should a trip valve fail to close, a degree of redundancy is provided by the angle type non-return valve.
During the 02-22-82 event, both channels of steamflow instrumentation on "C" main steamline remained operable as did the channel 4 instrument, F485, on "B" main steamline. Thus, the ESF actuation from high steamline flow logics was still possible, though in a degraded mode.
The other systems' instrumentation which act to automatically initiate the ESF functions remained operable and therefore provided a backup to the degraded steamline flow logic.
A steamline break is also characterized by system parameter indications in the main control room such as:
1.
Decreasing level in the affected steam generator.
~
Page 3 Report No. 82-029/OlT-0 2.
Decreasing steam pressure in the affected steam generator.
3.
Increased AT within the affected loop due to increased extraction of reactor coolant heat.
It is concluded that at the time of the event, there existed adequate instrumentation to provide protection and alert the control room operator of steamline breaks. For these reasons, the public health and safety were not affected.
3.
CAUSE OF EVENT
This event was the result of both personnel error and inadequate procedures.
The steamline flow transmitters were replaced during the maintenance outage which preceeded the unit startup. No specific instructions were contained in the Design Change Package, the Instrument Department procedures, or Periodic Test procedures to ensure the condensate (sensing) lines of the transmitters were filled following the transmitter replacement and. before unit startup.
Con-sequently, some of tP;se lines contained inadequate fluid and provided
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erroneous flow indication. The transmitters so affected were left in the unfused l
l condition to avoid the KWST cross connect signal initiated by a high steamline
..ow in coincidence with reactor coolant averge temperature less than 543*F.
Intradepartmental correspondence prior to startup cautioned that the unfused instruments were to be fused when the sensing lines were filled and before reactor coolant average temperature reached 543*F. As a result of ad_
ministrative oversight, tha instrument fuses were neglected and the mistake was not realized until the reactor power was approximately 8% and the reactor l
coolant average temperature was 547*F.
l l
Page 4 Report No.
'!-029 /01T-0 4.
IMMEDi.\\TE CORRECTIVE ACTIONS :
The immediate actions were to install power supply fuses in the affected instruments.
5.
SUBSEQUENT CORRECTIVE ACTIONS:
The "B" main steamline channel 3 instrument, F484, continued to produce an erroneous signal. This channel was placed in the trip mode and the transmitter was subsequently replaced.
6.
ACTIONS TAKEN TO PREVENT RECURRENCE:
More definitive guidance and checks will be implemented to ensure the operability of engineered Safeguards and reactor protection instrumentation. Appropriate personnel have been re-instructed in the use of existing. Jministrative controls for maintenance and other related activities.
7.
GENERIC IMPLICATIONS:
The possibility of unit startup without the full-protection from process instrumentation is increased when on scale indications from the instruments are not achieved before the protection function is required.
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05000280/LER-1982-001, Forwards LER 82-001/03L-0 | Forwards LER 82-001/03L-0 | | 05000280/LER-1982-001-03, /03L-0:on 820106,spurious Safety Injection Caused Phase 1 Containment Isolation.Trip Valve TV-CC-109B Failed to Close.Caused by Teflon Tape Preventing Operation of 3-way SOV That Controls TV-CC-109B | /03L-0:on 820106,spurious Safety Injection Caused Phase 1 Containment Isolation.Trip Valve TV-CC-109B Failed to Close.Caused by Teflon Tape Preventing Operation of 3-way SOV That Controls TV-CC-109B | | 05000281/LER-1982-001-03, /03L-0:on 820105,loss of Accurate Control of Boric Acid Concentrations of Unit 2 Bit & C Bast Occurred on 820105,08,15 & 18.Caused by Inleakage to Bit Via MOV-2867 A&B.Boron Concentration Returned to Tech Spec Limit | /03L-0:on 820105,loss of Accurate Control of Boric Acid Concentrations of Unit 2 Bit & C Bast Occurred on 820105,08,15 & 18.Caused by Inleakage to Bit Via MOV-2867 A&B.Boron Concentration Returned to Tech Spec Limit | | 05000281/LER-1982-001, Forwards LER 82-001/03L-0 | Forwards LER 82-001/03L-0 | | 05000280/LER-1982-002-03, /03L-0:on 820109,discharge Checkvalve of Charging Svc Water Pump 2-SW-P-10A Found Stuck Open.Caused by Failure of Valve Disk to Reseat Properly | /03L-0:on 820109,discharge Checkvalve of Charging Svc Water Pump 2-SW-P-10A Found Stuck Open.Caused by Failure of Valve Disk to Reseat Properly | | 05000280/LER-1982-003-03, /03L-0:on 820122,loss of Boric Acid Flow to Blender Observed.Caused by Inadequate Insulation on FT-1113 & Adjacent Piping.Blockages Removed or Freed & Addl Insulation Added to Prevent Recurrence | /03L-0:on 820122,loss of Boric Acid Flow to Blender Observed.Caused by Inadequate Insulation on FT-1113 & Adjacent Piping.Blockages Removed or Freed & Addl Insulation Added to Prevent Recurrence | | 05000281/LER-1982-003-03, /03L-0:on 820108,PT-27 Revealed Ampere Readings for Heat Tracing Panel 10 Circuits 1B,2A & 5B & Panel 11 Circuit 2A,4C & 5B Found Below Acceptance Criteria.Caused by Excessive Heat.Defective Heat Tracing Replaced & Tested | /03L-0:on 820108,PT-27 Revealed Ampere Readings for Heat Tracing Panel 10 Circuits 1B,2A & 5B & Panel 11 Circuit 2A,4C & 5B Found Below Acceptance Criteria.Caused by Excessive Heat.Defective Heat Tracing Replaced & Tested | | 05000281/LER-1982-004-03, /03L-0:on 820112,at 85% Power,Boron Injection Tank Recirculation Lost Due to Failure of Pump 1-CH-P-2D Leaving Only Two Boric Acid Transfer Pumps Serviceable.Caused by Failure of Mechanical Seal.Pump Repaired | /03L-0:on 820112,at 85% Power,Boron Injection Tank Recirculation Lost Due to Failure of Pump 1-CH-P-2D Leaving Only Two Boric Acid Transfer Pumps Serviceable.Caused by Failure of Mechanical Seal.Pump Repaired | | 05000280/LER-1982-004-03, /03L-0:on 820112,fire Hydrants 1-FP-89,1-FP-63, 1-FP-73 & 1-FP-98 Would Not Open.Caused by Freezing of Stagnant Water in Body of Hydrant Due to Unusually Low Temp. Frequency of Insps to Be Increased During Winter Months | /03L-0:on 820112,fire Hydrants 1-FP-89,1-FP-63, 1-FP-73 & 1-FP-98 Would Not Open.Caused by Freezing of Stagnant Water in Body of Hydrant Due to Unusually Low Temp. Frequency of Insps to Be Increased During Winter Months | | 05000281/LER-1982-004, Forwards LER 82-004/03L-0 | Forwards LER 82-004/03L-0 | | 05000280/LER-1982-005-03, /03L-0:on 820207,trip Valve TV-SS-204B Was Discovered Open & Would Not Close W/O Operator Intervention. Caused by Misalignment of Actuation Disk.Actuation Disk Adjusted | /03L-0:on 820207,trip Valve TV-SS-204B Was Discovered Open & Would Not Close W/O Operator Intervention. Caused by Misalignment of Actuation Disk.Actuation Disk Adjusted | | 05000280/LER-1982-006-03, /03L-0:on 820211,w/unit at 100% power,PT-27 Revealed That Amp Readings for Heat Tracing Panel 11,circuit 6A Was Below Acceptance Criteria.Caused by Excessive Heat. Defective Heat Tracing Replaced & Tested | /03L-0:on 820211,w/unit at 100% power,PT-27 Revealed That Amp Readings for Heat Tracing Panel 11,circuit 6A Was Below Acceptance Criteria.Caused by Excessive Heat. Defective Heat Tracing Replaced & Tested | | 05000280/LER-1982-007-03, /03L-0:on 820119,PT-27C Revealed Amp Reading for Heat Tracing Panel 9,circuit 20B Below Acceptance Criteria. Caused by Excessive Heat.Defective Heat Tracing Replaced & Tested | /03L-0:on 820119,PT-27C Revealed Amp Reading for Heat Tracing Panel 9,circuit 20B Below Acceptance Criteria. Caused by Excessive Heat.Defective Heat Tracing Replaced & Tested | | 05000280/LER-1982-007, Forwards LER 82-007/03L-0 | Forwards LER 82-007/03L-0 | | 05000281/LER-1982-007-03, /03L-0:on 820118,periodic Test 10 Revealed Unidentified Leak Rate Greater than 1 Gallon Per Minute. Caused by Inlet Flange Leak on Relief Valve.Flange Gasket Replaced | /03L-0:on 820118,periodic Test 10 Revealed Unidentified Leak Rate Greater than 1 Gallon Per Minute. Caused by Inlet Flange Leak on Relief Valve.Flange Gasket Replaced | | 05000280/LER-1982-008-03, /03L-0:on 820121,instrument Malfunction Resulted in Loss of All Pressurized Heaters.Caused by Short in One Pressurized Level Comparator.Short Repaired & Pressurizer Control Sys Returned to Normal Condition | /03L-0:on 820121,instrument Malfunction Resulted in Loss of All Pressurized Heaters.Caused by Short in One Pressurized Level Comparator.Short Repaired & Pressurizer Control Sys Returned to Normal Condition | | 05000281/LER-1982-008-03, /03L-0:on 820118,fault Occurred on Feeder Cables to B Reserve Station Svc Transformer.Isolation of Fault de-energized Emergency Bus.Caused by Flashover to Ground & to Adjacent Phase Due to Spraying of Insulators | /03L-0:on 820118,fault Occurred on Feeder Cables to B Reserve Station Svc Transformer.Isolation of Fault de-energized Emergency Bus.Caused by Flashover to Ground & to Adjacent Phase Due to Spraying of Insulators | | 05000280/LER-1982-009-03, /03L-0,on 820128,inadequate Svc Water Flow Resulted in Higher 2-CH-P-1C Lubricating Oil Temp.Pump Declared Inoperable.Caused by Foreign Object in Svc Water Temp Control Valve Body.Object Removed | /03L-0,on 820128,inadequate Svc Water Flow Resulted in Higher 2-CH-P-1C Lubricating Oil Temp.Pump Declared Inoperable.Caused by Foreign Object in Svc Water Temp Control Valve Body.Object Removed | | 05000280/LER-1982-010-03, /03L-0:on 820105,while Removing Unit from Svc, Spurious Safety Injection Signal Generated & Trip Valve Failed to Close.Cause Not Found.Investigation Continuing | /03L-0:on 820105,while Removing Unit from Svc, Spurious Safety Injection Signal Generated & Trip Valve Failed to Close.Cause Not Found.Investigation Continuing | | 05000280/LER-1982-011-03, /03L-0:on 820126,three Incidents of Unsampled Release from Subsurface Drains to Discharge Canal Occurred. Caused by Operator Error.Administrative Controls Established to Notify Health Physics Prior to Pumping of Drains | /03L-0:on 820126,three Incidents of Unsampled Release from Subsurface Drains to Discharge Canal Occurred. Caused by Operator Error.Administrative Controls Established to Notify Health Physics Prior to Pumping of Drains | | 05000280/LER-1982-012-03, /03L-0:on 820126,block Valve MOV-1536 Isolated Electrically While in Closed Position Due to Failure to Close Completely W/O Assistance.Cause Not Known.New Torque Switch Assembly Installed in Limitorque Operator | /03L-0:on 820126,block Valve MOV-1536 Isolated Electrically While in Closed Position Due to Failure to Close Completely W/O Assistance.Cause Not Known.New Torque Switch Assembly Installed in Limitorque Operator | | 05000281/LER-1982-013, Forwards LER 82-013/03L-0 | Forwards LER 82-013/03L-0 | | 05000281/LER-1982-013-03, /03L-0:on 820124,radioiodine Sample Taken 6-h & 28 Minutes Following Thermal Power Increase,Exceeded Tech Spec Time Limit.Caused by Delayed Oncoming Shift Chemists Due to Traffic Problems | /03L-0:on 820124,radioiodine Sample Taken 6-h & 28 Minutes Following Thermal Power Increase,Exceeded Tech Spec Time Limit.Caused by Delayed Oncoming Shift Chemists Due to Traffic Problems | | 05000280/LER-1982-013-03, /03L-0:on 820126,dropped Control Rod Resulted in Quadrant to Average Power Tilt of Greater than 2%.Caused by Corroded Conductors in Power Supply Due to Break in Cable Admitting Moisture.Cable Repaired & Control Rod Realigned | /03L-0:on 820126,dropped Control Rod Resulted in Quadrant to Average Power Tilt of Greater than 2%.Caused by Corroded Conductors in Power Supply Due to Break in Cable Admitting Moisture.Cable Repaired & Control Rod Realigned | | 05000280/LER-1982-014-03, /03L-0:on 820211,w/unit at 100% Power,Nuclear Power Range Instrument 41 (N 41) Failed.Caused by Shorted (Wetted) High Voltage Connector.Shorted Connector Replaced, Junction Box Dryed Out & N-41 Returned to Svc | /03L-0:on 820211,w/unit at 100% Power,Nuclear Power Range Instrument 41 (N 41) Failed.Caused by Shorted (Wetted) High Voltage Connector.Shorted Connector Replaced, Junction Box Dryed Out & N-41 Returned to Svc | | 05000280/LER-1982-015-03, /03L-0:on 820215,component Cooling to RHR Trip Valve TV-CC-209B Would Not Close on Control Room Signal. Caused by Faulty Pilot Valve,Controlling Air Flow to Valve Actuator.Valve Replaced & Tested | /03L-0:on 820215,component Cooling to RHR Trip Valve TV-CC-209B Would Not Close on Control Room Signal. Caused by Faulty Pilot Valve,Controlling Air Flow to Valve Actuator.Valve Replaced & Tested | | 05000280/LER-1982-016-03, /03L-0:on 820131,loss of Boric Acid Flow to Blender Observed While Attempting Blend to Vol Control Tank. Caused by Loss of Heat Tracing & Damaged Insulation Upstream of Flow Transmitter.Tracing Replaced | /03L-0:on 820131,loss of Boric Acid Flow to Blender Observed While Attempting Blend to Vol Control Tank. Caused by Loss of Heat Tracing & Damaged Insulation Upstream of Flow Transmitter.Tracing Replaced | | 05000280/LER-1982-017-03, /03L-0:on 820131,PR-27 Revealed Ampere Readings for Heat Tracing Panels 8 & 9,circuits 24A & C Below Acceptance Criteria.Caused by Loss of Heat Tracing Due to Excessive Heat.Tracing Replaced.Design Change Initiated | /03L-0:on 820131,PR-27 Revealed Ampere Readings for Heat Tracing Panels 8 & 9,circuits 24A & C Below Acceptance Criteria.Caused by Loss of Heat Tracing Due to Excessive Heat.Tracing Replaced.Design Change Initiated | | 05000280/LER-1982-018, Forwards LER 82-018/03L-0 | Forwards LER 82-018/03L-0 | | 05000280/LER-1982-018-03, /03L-0:on 820121,PT-27 Revealed Amp Readings for Heat Tracing Panels 8 & 9,circuit 13A,below Acceptable Criteria.Caused by Excessive Heat.Defective Heat Tracing Replaced & Tested | /03L-0:on 820121,PT-27 Revealed Amp Readings for Heat Tracing Panels 8 & 9,circuit 13A,below Acceptable Criteria.Caused by Excessive Heat.Defective Heat Tracing Replaced & Tested | | 05000280/LER-1982-019-03, /03L-0:on 820202,PT-27 Revealed Ampere Readings for Heat Tracing Circuits 24C,25A,panel 2 & Circuit 24D, Panels 1 & 2 (Boron Injection Tank Recirculation Line) Below Acceptance Criteria.Caused by Loss of Heat Tracing | /03L-0:on 820202,PT-27 Revealed Ampere Readings for Heat Tracing Circuits 24C,25A,panel 2 & Circuit 24D, Panels 1 & 2 (Boron Injection Tank Recirculation Line) Below Acceptance Criteria.Caused by Loss of Heat Tracing | | 05000280/LER-1982-020-03, /03L-0:on 820205,w/unit at 100% Power,Loss of Boric Acid Flow to Blender Was Observed.Caused by Operating Mechanism Failure on Valve 1-CH-88.Valve Mechanism Repaired | /03L-0:on 820205,w/unit at 100% Power,Loss of Boric Acid Flow to Blender Was Observed.Caused by Operating Mechanism Failure on Valve 1-CH-88.Valve Mechanism Repaired | | 05000280/LER-1982-021-03, /03L-0:on 820415,w/unit Operating at Steady State 96% power,2 Emergency Diesel Generator Found Stuck in Lower Position.Caused by Speed Control Governor Being Physically Stuck in Lower Position | /03L-0:on 820415,w/unit Operating at Steady State 96% power,2 Emergency Diesel Generator Found Stuck in Lower Position.Caused by Speed Control Governor Being Physically Stuck in Lower Position | | 05000280/LER-1982-022, Forwards Updated LER 82-022/03X-1 & LER 82-047/01T-0 | Forwards Updated LER 82-022/03X-1 & LER 82-047/01T-0 | | 05000280/LER-1982-022-03, /02L-0:on 820209,relief Valve RV-GW-103 Opened Causing Pressure Transient in Process Vent Sys & Damaging Process Vent Flow Transmitter.Caused by Momentary Pressure Spike That Overranged Flow Transmitter.Transmitter Replaced | /02L-0:on 820209,relief Valve RV-GW-103 Opened Causing Pressure Transient in Process Vent Sys & Damaging Process Vent Flow Transmitter.Caused by Momentary Pressure Spike That Overranged Flow Transmitter.Transmitter Replaced | | 05000281/LER-1982-023, Forwards LER 82-023/03L-0 | Forwards LER 82-023/03L-0 | | 05000281/LER-1982-023-03, /03L-0:on 820420 W/Boric Acid Transfer Pump 1-CH-P-2D Tagged for Maint,Boron Injection Tank Recirculation Lost Due to Failure of 1-CH-P-2C.Caused by Reversal of Slow Speed Motor Leads.Pump Repaired | /03L-0:on 820420 W/Boric Acid Transfer Pump 1-CH-P-2D Tagged for Maint,Boron Injection Tank Recirculation Lost Due to Failure of 1-CH-P-2C.Caused by Reversal of Slow Speed Motor Leads.Pump Repaired | | 05000280/LER-1982-023-03, /03L-0:on 820212,PT-39B.2 & PT-39B.1 Revealed That Snubbers 1-RC-HSS-131,1-WFPD-HSS-15 & 1-SHP-HSS-35B Were Inoperable Due to Low Oil Reservoir Level.Caused by Seal Leakage.Snubbers Replaced &/Or Repaired | /03L-0:on 820212,PT-39B.2 & PT-39B.1 Revealed That Snubbers 1-RC-HSS-131,1-WFPD-HSS-15 & 1-SHP-HSS-35B Were Inoperable Due to Low Oil Reservoir Level.Caused by Seal Leakage.Snubbers Replaced &/Or Repaired | | 05000280/LER-1982-024-01, /01T-0:on 820524,weld Leak on a Steam Generator Channel Head Drain Piping at 2-RC-159 Identified During RCS Integrity Test PT-11.Caused by Random Defect in Root Weld, Possibly Due to Split Pass | /01T-0:on 820524,weld Leak on a Steam Generator Channel Head Drain Piping at 2-RC-159 Identified During RCS Integrity Test PT-11.Caused by Random Defect in Root Weld, Possibly Due to Split Pass | | 05000280/LER-1982-025-03, /03L-0:on 820215,smoke Detector Panel Found W/All Alarms Illuminated & Silenced,Rendering Panel Inoperable. Caused by Personnel Error & Inadequate Procedural Guidance. Switches Returned to Proper Position | /03L-0:on 820215,smoke Detector Panel Found W/All Alarms Illuminated & Silenced,Rendering Panel Inoperable. Caused by Personnel Error & Inadequate Procedural Guidance. Switches Returned to Proper Position | | 05000280/LER-1982-026-03, /03L-0:on 820218,approx 135 Gallons of Unsampled Contaminated Water Discharged from Contaminated Drain Tank.Caused by Personnel Failure to Follow Approved Procedure | /03L-0:on 820218,approx 135 Gallons of Unsampled Contaminated Water Discharged from Contaminated Drain Tank.Caused by Personnel Failure to Follow Approved Procedure | | 05000280/LER-1982-027-03, /03L-0:on 820208,spurious Safety Injection Signal Generated & Trip Valve TV-CC-109B Failed to Close.No Mechanical or Electrical Malfunction Found.Investigation Continuing | /03L-0:on 820208,spurious Safety Injection Signal Generated & Trip Valve TV-CC-109B Failed to Close.No Mechanical or Electrical Malfunction Found.Investigation Continuing | | 05000280/LER-1982-028-03, /03L-0:on 820219,radiation Alarm Setpoints for Component Cooling Sys Found Greater than Twice Background. Caused by Reduced Background Due to Plant Shutdown.Setpoints Reset | /03L-0:on 820219,radiation Alarm Setpoints for Component Cooling Sys Found Greater than Twice Background. Caused by Reduced Background Due to Plant Shutdown.Setpoints Reset | | 05000280/LER-1982-029, Forwards LER 82-029/01T-0 | Forwards LER 82-029/01T-0 | | 05000280/LER-1982-029-01, /01T-0:on 820222,steam Line Flow Instruments for a Main Steam Line,Channels 3 & 4, & B Main Steam Line,Channel 3,reported Inoperable During Startup.Caused by Lack of Power Supply Fuses to Transmitters.Fuses Replaced | /01T-0:on 820222,steam Line Flow Instruments for a Main Steam Line,Channels 3 & 4, & B Main Steam Line,Channel 3,reported Inoperable During Startup.Caused by Lack of Power Supply Fuses to Transmitters.Fuses Replaced | | 05000280/LER-1982-030-03, /03L-0:on 820222,alarm Setpoint for Component Cooling Water Radiation Monitor (RM-CC-105) Found to Be Greater than Twice Background.Caused by Instrument Drift. Monitor Reset | /03L-0:on 820222,alarm Setpoint for Component Cooling Water Radiation Monitor (RM-CC-105) Found to Be Greater than Twice Background.Caused by Instrument Drift. Monitor Reset | | 05000280/LER-1982-031-03, /03L-0:on 820222,RHR Sample Sys Containing Isolation Trip valve,TV-SS-103A,opened W/O Operator Action & Could Not Be Closed from Control Room.Cause Not Yet Identified.Redundant Trip Valve Closed | /03L-0:on 820222,RHR Sample Sys Containing Isolation Trip valve,TV-SS-103A,opened W/O Operator Action & Could Not Be Closed from Control Room.Cause Not Yet Identified.Redundant Trip Valve Closed | | 05000280/LER-1982-032-03, /03L-0:on 820314,accumulator Levels Increased to Maintain Tech Spec Level Limits.Caused by Operator Failure to Close Containment Isolation Valve 1-SI-32 Per OP-7.7 | /03L-0:on 820314,accumulator Levels Increased to Maintain Tech Spec Level Limits.Caused by Operator Failure to Close Containment Isolation Valve 1-SI-32 Per OP-7.7 | | 05000280/LER-1982-033-03, /03L-0:on 820530,w/unit at 96% Power,Charging Pump Svc Water Pump 2-SW-P-10B Failed to Develop Sufficient Discharge Pressure.Caused by Insufficient Npsh.Svc Water to Chillers Throttled | /03L-0:on 820530,w/unit at 96% Power,Charging Pump Svc Water Pump 2-SW-P-10B Failed to Develop Sufficient Discharge Pressure.Caused by Insufficient Npsh.Svc Water to Chillers Throttled | | 05000280/LER-1982-034-03, /03L-0:on 820625,cabinet 2AC Control Rods Would Not Respond to Demand Signal.Caused by Blown Fuse & Failed Phase Control Rod in Power Cabinet.Failed Components Replaced & Rods Succesfully Tested | /03L-0:on 820625,cabinet 2AC Control Rods Would Not Respond to Demand Signal.Caused by Blown Fuse & Failed Phase Control Rod in Power Cabinet.Failed Components Replaced & Rods Succesfully Tested | |
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