ML20028A059
| ML20028A059 | |
| Person / Time | |
|---|---|
| Site: | Robinson |
| Issue date: | 09/02/1982 |
| From: | Norris H CAROLINA POWER & LIGHT CO. |
| To: | |
| Shared Package | |
| ML20028A055 | List: |
| References | |
| NUDOCS 8211160357 | |
| Download: ML20028A059 (2) | |
Text
,
OPERATING DATA. REPORT DOCKET NO:
50-261 DATE:
820902 COMPLETED BY:
H. Ray Norris TELEP110NE:
(803) 383-4524 OPERATING STATUS Notes:
- 1. Unit Name:
H. B. Robinson Unit No. 2 There are presently 157 spent
- 2. Reporting Period: 820801.0000/820831.2400 fuel assemblies in the ' pent s
- 3. Licensed Thermal Power (MWt):
2300 fuel pool.
- 4. Nameplate Ra. ting (Gross tale):
739
- 5. Design Electrical Rating (Net }Me):700
- 6. tbximum Dependable Capacity (Gross FMe):
700
- 7. Maximum Dependable Capacity (Net FMe):
665
- 8. If Changes Occur in Capacity Ratings (Item Number 3 through 7) Since Last Report, Give Reasons:
No change
- 9. Power Level to Which Restricted, If Any (Not Mile):
1955 MWT Reactor Power
- 10. Reasons For Restrictions, If Any: Although the Unit is not restricted by any outside agency, the power level is presently reduced due to steam generator considerations.
This Month' Yr.-to-Date Cumulative
- 11. Hours in Reporting Period 744 5,831 100,757
- 12. Number of Hours Reactor Was Critical 304.73 1,671.83 74,017.25
- 13. Reactor Reserve Shutdown llours 0
0 1.085.30
- 14. Hours Generator On-Line 215.10 1,582.20 72.137.51
.15. Unit Reserve Shutdowa Hours 0
0 23.20
- 16. Gross Thermal Energy Generated (IMI)
- 245157
- 2746467
'*145841841
- 17. Gross Electrical Energy Generated (FMH) 72.952
.871.282 46.'949.252
- 18. Net Electrical Energy Generated (FMH)
- 54837
- 788696
- 44408947
- 19. Unit Service Factor 28.91 27.13 7 L. 59 '
- 20. Unit Availability Factor 28.91 27.13 71.61
- 21. Unit Capacity Factor (Using MDC N'et) 11.08 20.33 66.27
- 22. Unit Capacity Factor (Using DER Net) 10.53
_19.32 62.96
- 23. Unit Forced Outage Rate
- 40.37
- 8.43
- 14.46
- 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
l, Type-2, 2/26/83, Four week steam generator inspection outage.
25 If Chut Down At End of Report Period, Estimated Date of Startup:
On line
- 26. Units In Test Status (Prior to Commercial Operation):
Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION 8211160357 821110 PDR ADOCK 05000261 R
- Corrected on 821102 (9/77)
Cg
J 50-261 DOCKET NO.
H. B. Robinson UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT N AME 820902 DATE COMPLETED BY H. Ray Norris REPORT MONTil Augus t TELEPHONE (803) 383-4524 i
e.
E E
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3
$Y5 Lisensec 5 r, "g t Cause & Correesive -
r v
No.
Date y,
3g s
ji5 Event g,7 9-3 Action to mO E'
Prevent Recurrence
~ 5 =!!
Report
- E A
H s
v
.e 5
ZZ ZZZZZZ Shuutdown for maintenance / refueling 2-01 820801 S
350.08 B/C 3
outage HB HTEXCH While bringing the unit off line 08-02 82'0815 F
131.59 B
3 due to, faulty MW* indication, the unit tripped.
Cause-low icvel S/G resulting in low level trip.
HH VALVEX High level S/G. Cause-trip due to 08-03 820821 F
6.00 A
3 feedwater reg. valve malfunction.
HH VALVEX High level S/G. Cause-trip due to 08-04 820821 F
8.01 A
3 feedwate'r reg. valve malfunction.
HA TURBIN Required turbine over speed trip 08-05 820822
- S 32.27 B
1 test following refueling /maintenanc a outage.
~
HA TURBIN Required turbine test-adjusted over-
~
08-06 820825
'
- S.,
0.23 B y
speed trip.
4 3
I
. 2 Method:
Exhibit G Instructions for Preparation of Data F: For(cd Reaw n; I. Manual S: Scheduled A l'iluipment Failure (Explain) 2-Manual Scram.
Entr> Sheets for Licensee 3 Autmnatic Scram.
Event Repor (LER) File (NUREG-n Maintenance of Test C. Refueling 4-Other'(Explain) 0161)
D Regulatory Restriction 1:.-Operator Training & License Examination 5
F-Admmisirative Exhibit ! Same Sourec G. Operational Error (Explain)
(9/77)
Il-Other (Explain) o Corrected on 821102 t
........ - -.