05000364/LER-1981-043-03, /03L-0:on 810918,following Performance of Operability Test,Diesel Generator 1C Found Inoperable When Tripped Under Load.Caused by High Crankcase Pressure Resulting from Cylinder Lining Scoring

From kanterella
(Redirected from ML20011A743)
Jump to navigation Jump to search
/03L-0:on 810918,following Performance of Operability Test,Diesel Generator 1C Found Inoperable When Tripped Under Load.Caused by High Crankcase Pressure Resulting from Cylinder Lining Scoring
ML20011A743
Person / Time
Site: Farley 
Issue date: 10/16/1981
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20011A734 List:
References
LER-81-043-03L-01, LER-81-43-3L-1, NUDOCS 8110290374
Download: ML20011A743 (1)


LER-1981-043, /03L-0:on 810918,following Performance of Operability Test,Diesel Generator 1C Found Inoperable When Tripped Under Load.Caused by High Crankcase Pressure Resulting from Cylinder Lining Scoring
Event date:
Report date:
3641981043R03 - NRC Website

text

LICENSEE EVENT REPORT--

1 CONTROL BLCCX: l l

l l

l l lh (PLEASE PRINT OR TYC'E ALL REQUIRED INFORMATIONI 1

0 o I i l l A l L l J l M l F l 2 l@l 0 l 0 l - l 0 l OI O l 0 l 0.l-l0 l 0 l@l 4 l 1 l 1l Il 1l@l l

l@

F 3 9 UCENSEE CCDE 14 15 LICENSE NUM8ER a5

5 LICENSE TYPE JO 57 CA T 54

[ 9.

3c[3"c l L l@l0 l 5 l 0 l 0. l 0 l 31 6l 4 @l 0 l 9 ll' l8 l 8 l 1 l@l 1 l 0 l 1 l 6 ! 8 I 1 l@

"E 7

i

'O 60 61 COCKET NUMBER 63 63 EVENT CATE 74 75 REPCRT QATE 40 EVENT DESCRIPTICN AND PROBABLE CONSECUENCES h 10 62) l At 0252 on 9/18/81,followino oprfnrmanco nf FNP 1 ATPJA_1 (091C Onnrahilitu Toe + } Diocal I

oi3( l Gener.
Lor 1C was declared inoperable when.it tripped under load. Tech. Spec. 3.8.1.1 in ;
o ;e j lpart, requires DG 1C to be operable. Tech. Spec. 3.8.1.1.b.2 action statement requir.e-l 9oa3l l ments were met.

Health / safety of the public was not affected.

j io 86 I I I

l O 171 l l

l013l l 7

'l 3

60 SYSTEM

CAUSE

CAUSE CCMP.

VALVE CCCE CCCE SUSCCOE COMPCNENT CCCE SUSCCOE SUSCCCE

{019l l E! E l @ lE lh lB l@ lE lN lG lI l N l E l@ lZ l@ lZl@

7 a

9 to 11 12 t3 18 19

C SEQU ENTI AL OCCURRENCE REPCRT REVISION LEBtRO EVENT YEA R REPORT NO.

CCCE TYPE N O.

@ yu l 811l l-l l 01413 l l/l l013l lLl l-l

.l 0 l aE T

7.

22 23 24 26 27 28

3 30 31 32 T

N A C.

CN PL ? T M T HOURS 22 SS FC 1 S.

S PP E M NUFA RER g

.. IA @lZl@

lZ l@

l Z l@

[0 l 010 l 0 l [Njg l N [g l Alg l p l 0 l1 lo

.3 45 a6 37 40 4:

42 43 u-47 CAUSE CEECRIPTION AND CCRRECTIVE ACTIONS 27 l i i o l l The DG 1C trip was due to high crankcase pressure. An investigation revealed that the l3 ;il l number 1 and 11 cylinder liners were scored. The scoring of the liners caused localized ;

ii,,l l heating and exhaust leakage into the oil sump. This, in turn, caused the high crankcase ;_

li63l l pressure. Following the completion of repairs and successful testing, DG IC was returned y

,,,4 l l to service at 1603 on 10/02/81.

7

- 8 9

80

$A agpCWER OTH ER STATUS Cf C h

CISCCVERY OESCRIPTICN -

ii i5 l l El@ l ll 0l Ol@l NA l

lB (@lSurveillanceTest l

a $nviTY cClTENT 7

A AMOuNTCF ACTIVITY @ l aELEASEc or RELEASE LCCAT!CN OF RELEASE l1 66llZl@_lZl@l l

NA l_

NA 7

3 3 to 11 4.*

45 80 PERSONNEL EXPOSURES NUM8ER TYPE DESCRIPT1CN j i I 7 l l 0l 01 O l@l Z l@l NA l

PERSCNNEt'iN2u' dies NUMSER CESCRIPTION [t t a l l 0l' 010 l@l iA l

7 53

.it u

ao

.[

  • ! LCSS OF CA CAMAGE TO FACILITY 43 TYPE CE!CAIPTtON ft,9 lZl@l NA l

7 8 9. PusuC Tv 10 30 8110290374 G11015 NRC USE ONLY 43 i a 101 l Nlh[OESCRIPTtCN iSSuEo PDR ADOCK 05000364

=

i a s to I. IlI!IIIIllIllI NA S

PDR 6s as

. ao 3 -

NAME OF PREPARER: W. G. Hairston, III PHONE: (205)899-5156 o;