LER-1981-160, Forwards LER 81-160/03L-0.Detailed Event Analysis Encl |
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October-22,-.1981 373..ee3 d
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Re: McGuire Nuclear Station Unit K'et7 Docket No. 50-369 r
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Dear Mr. O'Reilly:
Please find attached Reportable Occurrence Report RO-369/81-160. This
. report concerns T. S. 3.5.1.2, "Each upper head injection accumulator system shall be operable with:... c.
The nitrogen bearing accumulator pressurized to between 1206 and 1264 psig." This incident was considered to be of no significance with respect to the health and safety-of the public.
Very truly yours, d
William O. Parker, Jr.
PBN:1s
. Attachment cc: Director Records Center Office of Management and Program Analysis Institute of Nuclear Power Operations.
U. S. Nuclear Regulatory Commission 1820 Water Place Washington, D. C.
20555 Atlanta, Georgia 30339 Ms.
M.'J. Graham Resident Inspector - NRC McGuire Nuclear Station [h
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8110290279 81102U PDR ADOCK 05000369 o.
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a McGUIRE NUCLEAR STATION REPORTABLE OCCURRENCE REFORT NUMBER:
81-160 REPORT DATE: October 22, 1981 OCCURRENCE DATE:
September 22, 1981 FACILITY: McGuire Unit 1; Cornelius, N. C.
IDENTIFICATION OF OCCURRENCE: The nitrogen over pressure on the upper head injection (UHI) accumulator dropped below 1206 psig.
CONDITIONS PRIOR TO OCCURRENCE: Mode 1, 31% power DESCRIPTION OF OCCURRENCE:
On September 22, 1981, the "UHI Surge Tank Hi/Lo Pressure" alarm was received in the control room.
When an unsuccessful attempt to pressurize the UHI nitrogen accumulator using the nitrogen bulk storage cylinders was made, it was discovered that the nitrogen cylinders' pressures were between 1200 and 1250 psig. Repressurization of the nitrogen cylinders was begun using the liquid nitrogen storage unit, and power was reduced to comply with the action statement in Technical Specification 3.5.1.2 since the UHI nitrogen accumulator had not been repressurized. A Safety Injection pump was operated to add water to the water accumulator. After the nitrogen header had been repressurized to between 1300 and 1350 psig and the UHI low pressure alarm had cleared, the turbine-generator load was increased back to about 260 FNe. This incident was reportable pursuant to the above Technical Specification.
APPARENT CAUSE OF OCCURRENCE: A design inadequacy resulted in the nitrogen low header pressure alarro in the control room being energized continuously. Thus, the operators were not aware that the header pressure was low and that they would not be able to repressurize the UHI nitrogen accumulator. A drain valve on the UHI nitrogen accumu-lator was found to be " weeping".
Packing leakoffs on the UHI hydraulic block valves also contribute to water and eventually pressure decreases in the UHI system.
ANALYSIS OF OCCURRENCE: A nitrogen heater is installed on the 1550 psig header because of the high flowrate required for pressurizing the UHI nitrogen accumulator. A vendor supplied relief valve is attached to the nitrogen heater and is set for 1450 psig. A pressure switch on the nitrogen header feeds a "N2 System Distribution Header Low Pr ssure" alarm in the control room.
The pressure switch is set to alarm at 1450 psig, which is the same serpoint as the relief valve on the nitrogen heater.
The switch also has a reset band of normally 200 psig (alarm clears at 1650 psig). To prevent lif ting the relief valve which discharges at the heater in the auxiliary building, the header has been maintained at 1300-1350 psig. Thus, the nitrogen low header pressure alarm light has been energized continuously.
Nitrogen had been used in various plant systems during the previous twenty-four hours and the nitrogen cylinders' pressures had decreased to 1200-1250 psig.
Thus, when the UHI low surge tank pressure alarm was received, the operators were unable to immediately repressurize the UHI nitrogen accumulator and clear the alarm. After the cylinders were repressurized from the liquid nitrogen storage unit the UHI low pressure alarm was cleared by adding nitrogen to the accumulator.
Was,r was also added to the UHI water accumulator to increase the surge tank level. A 3/4 inch Kerotest drain valve on the nitrogen accumulator was found to be " weeping".
The valve handwheel was tightened down and joint sealing compound applied to the pipe cap.
Packing leakoffs on the four UHI hydraulic block valves also contribute to water and eventually pressure decreases in the UHI system.
t Report Number 81-160
,Page Two s
SA5ETY ANALYSIS:
The UHI system is passive and is only used if a large reactor coolant system break occurs. Even though the UHI pressure decreased to the Technical Specification limit of 1206 psig, the system would have functioned properly if it had been needed.
Thus, safe plant operation and the health and safety of the public were not affected by this incident.
CORRECTIVE ACTION
Plant power was reduced to comply with the Technical Specification action statement until the UHI low pressure alarm cleared. The alarm setpoint on the pressure switch has been reduced to 1250 psig (minimum required for repressurizing the UHI nitrogen accumulator), and the reset band to about 130 psig.
The resulting reset (low header pressure alarm clears) pressure of 1380-1400 psig is still considered to be too close to the 1450 psig relief valve setpoint for personnel safety. Duke Power Company is trying to obtain a suitable pressure switch which has an adjustable reset band of approximately 50 psig.
This would allow the low header pressure alarm to clear with 1300-1350 psig header pressure. The " weeping" drain valve was tightened and its pipe cap sealed with joint compound. Two of the nitrogen cylinders have been White Tagged with the stubs held by the Shift Supervisor and will be used for emergency purposes.
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| 05000369/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000369/LER-1981-001-03, /03L-0:on 810129-0212,several Fire Detection Instruments Were Inoperable for Periods Exceeding 1-h. Caused by Const in Area.Fire Watches & Patrols Established | /03L-0:on 810129-0212,several Fire Detection Instruments Were Inoperable for Periods Exceeding 1-h. 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Linkage Repositioned & Nut Tightened | | | 05000369/LER-1981-009, Forwards LER 81-009/03L-0.Detailed Event Analysis Encl | Forwards LER 81-009/03L-0.Detailed Event Analysis Encl | | | 05000369/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000369/LER-1981-010-03, /03L-0:on 810207,total RHR Flow Exceeded Tech Specs.Caused by Air Line Supplying Actuator on RHR Valve Breaking,Allowing Valve to Fail Open.Rhr Flow Reset.Rigid Air Supply Lines to Be Replaced W/Flexible Lines | /03L-0:on 810207,total RHR Flow Exceeded Tech Specs.Caused by Air Line Supplying Actuator on RHR Valve Breaking,Allowing Valve to Fail Open.Rhr Flow Reset.Rigid Air Supply Lines to Be Replaced W/Flexible Lines | | | 05000369/LER-1981-011-03, /03T-0:on 810210,both Pressure Seals on Inner Door of Lower Personnel Air Lock Failed.Caused by Hole in One Seal & Bubble in Other Seal.Seals Replaced & Returned to Manufacturer | /03T-0:on 810210,both Pressure Seals on Inner Door of Lower Personnel Air Lock Failed.Caused by Hole in One Seal & Bubble in Other Seal.Seals Replaced & Returned to Manufacturer | | | 05000369/LER-1981-011, Forwards LER 81-011/03T-0 | Forwards LER 81-011/03T-0 | | | 05000369/LER-1981-012-03, /03T-0:on 801211,isolation Valve NV-250 Found Not Verified Closed Under Administrative Control Per Tech Spec. 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