LER-1981-073, /03L-0:on 810920,24 & 1007,diesel Generator 4 Did Not Attain Rated Speed in Required Time When Started.Caused by Intermittent Electrical Connection on Diesel Right Starting Air Bank Dc Solenoid Valve.Connection Repaired |
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| 3241981073R03 - NRC Website |
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NRC FORM h U.S. NUCLEAR REGULATORY COMMISSION (7 77) 4 LICENSEE EVENT REPORT 4
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60 61 DOCKET NUYBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l o l 2 l lWhile performing periodic testing on No. 4 iiesel generator, the diesel started but didl 2
I O 13 l [not attain rated speed. On September 24,'1981 following an auto start of all four l
lo l4 l l diesel generators, it was observed that No. 4 diesel generator required 25 seconds to l
[ O I s i l attain rated speed. ' On October 7,1981, while performing required testing, No. 4 l
10 le I idiesel generator did not attain rated speed in <10 seconds. These events did not 1
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l 0 l 7 l laf fect the health and safety of the public. Technical Specifications 3.8.1.1, l
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CODE TYPE N O.
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40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h lil0llThe principal cause of these events was an intermittent electrical connection on the
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l i j i j l diesel right starting air bank DC solenoid valve, SS-SSV1,.model 2, which prevented thei l timely admission of fuel to the diesel. The electrical connection was repaired anci thel 3 7
- l diesel was successfully tested, started and returned to service. Plant documentation l
, 3 g lshows that this is an isolated event; therefore, no further corrective action'is requirpd.
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% POWER OTHER STATUS DtS OV RY DISCOVERY DESCRIPTION Periodic Test j
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LER ATTACHMENT - RO #2-81-73 Facility: BSEP Unit No. 2 Event Date: September 20, 1981
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- - On September 20, 1981, while performing Service Water and Service Water Lube System Operability Test, PT 24.1, when No. 4 diesel generator was started-to observe the opening of the diesel, Unit No.1 Service Water ' System supply valve,-
the diesel started but did not attain rated speed. The initial investigation of the event determined corrosion buildup in the valve body of the diesel left starting air b nk regulating valve PRV-786, Model 310-32, had prevented the' full admittance of starting air to the diesel, which resulted in the event. The valve was cleaned, reassembled snd tested for' proper operation. The diesel was then successfully test started and returned to normal standby ^ readiness..In addition, a Work Request was then submitte'd to inspect the diesel right starting air bank regulating valve, PRV-789 during the next scheduled maintenance on.No.
4 diesel generator, in order to ensure proper operation of the valve.
Prior to inspecting PRV-789 on September 24, 1981, following a main turbine trip resulting from a main generator load reject, all four diesel generators; auto started, but No. A required 25 seconds to attain rated speed. The initial investigation of this event revealed a corrosion buildup in the 789. valve, and' it was determined tae event had also occurred due to insufficient starting air
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pressure as was encountered during the September 20, 1981 event involving the
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PhV-786 pressure regulating valve. PRV-789 was then cleaned, reassembled and tested for proper operation. The diesel was then successfully started and' returned to normal standby readiness.
On October 7,1981, while performing required testing due to the removal cf No.
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1 diesel generator from service for maintenance, No. 4_ diesel generator started but failed to attain rated speed in the required <10 seconds.
This investigation of this event revealed a broken terminal ring on the solenoid operator to the diesel right starting air bank solenoid valve SV-SSV1.. It is believed the broken terminal ring permitted intermittent operation of the valve and is the fundamental cause of all three events.
During a " start" sequence of a diesel generator the diesel fuel regulating system receives an inithtl opening signal via the diesel right starting air bank.
After the dierel otarts, the normal hydraulic control of the. fuel regulating system is supplied by the pressure developed by the diesel driven-shaft oil pump.
It is believed that in each of the three events, the diesel' received sufficient starting air pressure to crank the diesel, but due to intermittent operation of the SV-SSV1 valve, the diesel fuel regulating system did not operate in a timely n.anner. In each case, the diesel would then start after sufficient engine cranking supplied enough hydraulic pressure to open the diesel fuel regulating system " fuel racks." The reason for the broken solenoid terminal lug which is fastened with a nut and is wrapped in electrical insulation could not be determined.
It is presently under consideration ;to -
evaluate the starting air moisture problems of the diesel generators' starting air systems.
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| 05000325/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000325/LER-1981-001-01, /01T-0:on 810103,feed Pump Tripped on High Vessel Level Due to safety-relief Valve B21-F013G,Model 67F,lift. Caused by High Second Stage & Pilot Leakage in Valve.Pilot Valve Temporarily Replaced Until Next Scheduled Outage | /01T-0:on 810103,feed Pump Tripped on High Vessel Level Due to safety-relief Valve B21-F013G,Model 67F,lift. Caused by High Second Stage & Pilot Leakage in Valve.Pilot Valve Temporarily Replaced Until Next Scheduled Outage | | | 05000324/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000324/LER-1981-001-03, /03L-0:on 810129,during Surveillance Testing, HPCI Sys Initiation Reactor Level Switch Actuated at Simulated Level Above Tech Spec.Caused by Components Slipping Due to Loose Set Screws on Actuator Pointers | /03L-0:on 810129,during Surveillance Testing, HPCI Sys Initiation Reactor Level Switch Actuated at Simulated Level Above Tech Spec.Caused by Components Slipping Due to Loose Set Screws on Actuator Pointers | | | 05000325/LER-1981-002-03, /03L-0:on 810114 & 0212,reactor Protection Sys Logic relays,C71-K3D & K3E,did Not de-energize When MSIV 1-B21-F028B Was Closed.Caused by Sticking Valve Position Limit Switch Actuator Arm Cam.Switch Replaced | /03L-0:on 810114 & 0212,reactor Protection Sys Logic relays,C71-K3D & K3E,did Not de-energize When MSIV 1-B21-F028B Was Closed.Caused by Sticking Valve Position Limit Switch Actuator Arm Cam.Switch Replaced | | | 05000325/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000324/LER-1981-002-03, /03L-0:on 810104,vacuum Breaker X-18A Had Dual open-close Position Indication While in Open Position. Probably Caused by Problem W/Vacuum Breaker Position Limit Switches.Problem Will Be Resolved During Next Outage | /03L-0:on 810104,vacuum Breaker X-18A Had Dual open-close Position Indication While in Open Position. Probably Caused by Problem W/Vacuum Breaker Position Limit Switches.Problem Will Be Resolved During Next Outage | | | 05000324/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000324/LER-1981-003-03, /03L-0:on 810108,suppression Pool Level Exceeded Specs.Caused by Valve Operator Torque Switch Out of Adjustment Allowing Leakage Into Suppression Pool.Switch Repaired | /03L-0:on 810108,suppression Pool Level Exceeded Specs.Caused by Valve Operator Torque Switch Out of Adjustment Allowing Leakage Into Suppression Pool.Switch Repaired | | | 05000324/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000325/LER-1981-003-03, /03L-0:control Rod 26-35 on 810103,18-51 on 810113,38-31 & 22-15 on 810114 Showed Inaccurate Position Indications.Caused by Buffer Card Failure on 26-35;defective Reed Switches in Others.Card Replaced,Switches Repaired | /03L-0:control Rod 26-35 on 810103,18-51 on 810113,38-31 & 22-15 on 810114 Showed Inaccurate Position Indications.Caused by Buffer Card Failure on 26-35;defective Reed Switches in Others.Card Replaced,Switches Repaired | | | 05000325/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000324/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000324/LER-1981-004-03, /03L-0:on 810110,during Startup,Intermediate Range Monitor a Did Not Respond to Changes in Input Signal.Monitor C Indicated Downscale When on Range 7.On 810111 Monitor E Indicated Downscale While Monitor C Still Inoperable | /03L-0:on 810110,during Startup,Intermediate Range Monitor a Did Not Respond to Changes in Input Signal.Monitor C Indicated Downscale When on Range 7.On 810111 Monitor E Indicated Downscale While Monitor C Still Inoperable | | | 05000325/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000325/LER-1981-004-03, /03L-0:on 810118,during Control Rod Operability Check,Pt 14.1,rod 26-07 Would Not Select.Caused by Loose Solder Joint in Rod Select Switch Due to Frequent Use of Switch.New Solder Joint Made | /03L-0:on 810118,during Control Rod Operability Check,Pt 14.1,rod 26-07 Would Not Select.Caused by Loose Solder Joint in Rod Select Switch Due to Frequent Use of Switch.New Solder Joint Made | | | 05000325/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000325/LER-1981-005-03, /03L-0:on 810101,during Normal Surveillance, Discovered Secondary Containment 20 Ft Elevation Inner Air Lock Door Inoperable Due to Missing Gasket Sealing Matl. Caused by High Personnel Traffic.Gasket Replaced | /03L-0:on 810101,during Normal Surveillance, Discovered Secondary Containment 20 Ft Elevation Inner Air Lock Door Inoperable Due to Missing Gasket Sealing Matl. Caused by High Personnel Traffic.Gasket Replaced | | | 05000324/LER-1981-005-03, /03L-0:on 810113,during Normal Surveillance, Secondary Containment 20-ft Elevation Outer Air Lock Personnel Door Found Not Sealing.Caused by Heavy Personnel Traffic Through Door.Gasket Repaired | /03L-0:on 810113,during Normal Surveillance, Secondary Containment 20-ft Elevation Outer Air Lock Personnel Door Found Not Sealing.Caused by Heavy Personnel Traffic Through Door.Gasket Repaired | | | 05000324/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000324/LER-1981-006-03, /03L-0:on 810115,when Main Steam Line Isolation Valve F028C Reopened During Test P.T.1.3.1P-2,main Steam Line C Indicated Min Flow.Cause Undetermined.Investigation Will Be Performed During Future Outage | /03L-0:on 810115,when Main Steam Line Isolation Valve F028C Reopened During Test P.T.1.3.1P-2,main Steam Line C Indicated Min Flow.Cause Undetermined.Investigation Will Be Performed During Future Outage | | | 05000324/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000325/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000325/LER-1981-006-03, /03L-0:on 810101,containment Atmospheric Monitor, 1-CAC-ATH-1259-2 Found Out of Calibr.Caused by Instrument Drift.Monitor Recalibr & Returned to Svc | /03L-0:on 810101,containment Atmospheric Monitor, 1-CAC-ATH-1259-2 Found Out of Calibr.Caused by Instrument Drift.Monitor Recalibr & Returned to Svc | | | 05000324/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000325/LER-1981-007-03, /03L-0:on 810220,observed 2-inch Discrepancy Between Level Indicators of Suppression Pool Level Transmitters 1-CAC-LT-2601 & 2602.Caused by Insufficient Venting of 2602 Transmitter High Side Sensing Line | /03L-0:on 810220,observed 2-inch Discrepancy Between Level Indicators of Suppression Pool Level Transmitters 1-CAC-LT-2601 & 2602.Caused by Insufficient Venting of 2602 Transmitter High Side Sensing Line | | | 05000325/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000324/LER-1981-007-03, /03L-0:on 810115,Group 1 Isolation Signal Received on Reactor Protection Sys Trip Channel B.Caused by Failure of Relay Coil,Model P/N 12HFAS1A49F Due to Insulation Breakdown.Coil Replaced | /03L-0:on 810115,Group 1 Isolation Signal Received on Reactor Protection Sys Trip Channel B.Caused by Failure of Relay Coil,Model P/N 12HFAS1A49F Due to Insulation Breakdown.Coil Replaced | | | 05000325/LER-1981-008-03, /03L-0:on 810106,while Performing Primary Containment Leak Rate Testing of Personnel Airlock Doors, Discovered That Drywell Exterior Airlock Door Leakage Rate Exceeded Limits.Caused by Tubing Fitting Lodged in Door | /03L-0:on 810106,while Performing Primary Containment Leak Rate Testing of Personnel Airlock Doors, Discovered That Drywell Exterior Airlock Door Leakage Rate Exceeded Limits.Caused by Tubing Fitting Lodged in Door | | | 05000325/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000324/LER-1981-009-04, /04T-0:on 810128,radwaste Sys Liquid Effluent Discharge High Range Indicator/Recorder Found to Have Recorded Release Rate Less than Actual,Causing Tech Spec Limit to Be Exceeded.Caused by Loose Mechanical Linkage | /04T-0:on 810128,radwaste Sys Liquid Effluent Discharge High Range Indicator/Recorder Found to Have Recorded Release Rate Less than Actual,Causing Tech Spec Limit to Be Exceeded.Caused by Loose Mechanical Linkage | | | 05000325/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000325/LER-1981-009-03, /03L-0:on 810115,sys Oil Cooler Inlet Isolation Valve 1-E51-F046 Would Not Open from RTGB Resulting in Reactor Core Isolation Cooling Inoperability.Caused by Incorrect Motor Control Ctr Key Lock Switch Position | /03L-0:on 810115,sys Oil Cooler Inlet Isolation Valve 1-E51-F046 Would Not Open from RTGB Resulting in Reactor Core Isolation Cooling Inoperability.Caused by Incorrect Motor Control Ctr Key Lock Switch Position | | | 05000324/LER-1981-009, Forwards LER 81-009/04T-0 | Forwards LER 81-009/04T-0 | | | 05000325/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000325/LER-1981-010-03, /03L-0:on 810120,upon Auto Initiation After Reactor Scram,Rcic Turbine Failed to Accelerate to Idle Speed,Making RCIC Inoperable.Caused by Dirty Contacts in Turbine Steam Inlet Supply Valve 1-E51-F045.Contacts Cleaned | /03L-0:on 810120,upon Auto Initiation After Reactor Scram,Rcic Turbine Failed to Accelerate to Idle Speed,Making RCIC Inoperable.Caused by Dirty Contacts in Turbine Steam Inlet Supply Valve 1-E51-F045.Contacts Cleaned | | | 05000324/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000324/LER-1981-010-03, /03L-0:on 810120,RHR Svc Water Subsys a Suction valve,2-SW-V101,would Not Open Fully.Caused by Two Hex Nuts on Input Shaft of Valve Motor Operator,Model H3BC-SMB-00, Freezing to Shaft.Nuts & Shaft Reworked & Lubricated | /03L-0:on 810120,RHR Svc Water Subsys a Suction valve,2-SW-V101,would Not Open Fully.Caused by Two Hex Nuts on Input Shaft of Valve Motor Operator,Model H3BC-SMB-00, Freezing to Shaft.Nuts & Shaft Reworked & Lubricated | | | 05000324/LER-1981-011-03, /03L-0:on 810120 & 0123,actual Pool Level Determined in Excess of Upper Tech Spec Limit.Caused by Improper Calibr Data & Calibr Procedure Inadequacy.Procedure Revision Underway & Indicators Correctly Calibr | /03L-0:on 810120 & 0123,actual Pool Level Determined in Excess of Upper Tech Spec Limit.Caused by Improper Calibr Data & Calibr Procedure Inadequacy.Procedure Revision Underway & Indicators Correctly Calibr | | | 05000324/LER-1981-011, Forewards LER 81-011/03L-0 | Forewards LER 81-011/03L-0 | | | 05000325/LER-1981-011-03, /03L-0:on 810121,during Routine Shutdown Operation,Seat Leakage Discovered on Reactor Recirculation Sample Inboard Isolation Valve 1-B32-F019.Cause Unknown. Valve Will Be Inspected & Repaired During Next Outage | /03L-0:on 810121,during Routine Shutdown Operation,Seat Leakage Discovered on Reactor Recirculation Sample Inboard Isolation Valve 1-B32-F019.Cause Unknown. Valve Will Be Inspected & Repaired During Next Outage | | | 05000325/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000324/LER-1981-012-03, /03L-0:on 810320,wiring Deficiency Associated W/ Actuation Switch Discovered That Prevented Switch Operation. Caused by Improper Writing of Field Revision to Plant Mods Requiring Installation of Switches | /03L-0:on 810320,wiring Deficiency Associated W/ Actuation Switch Discovered That Prevented Switch Operation. Caused by Improper Writing of Field Revision to Plant Mods Requiring Installation of Switches | | | 05000325/LER-1981-012-03, /03L-0:on 810122,rod 26-35 Did Not Have Position Indication at Position 03 & Rod 34-35 Did Not Have Position Indication at Position 02.Caused by Defective Rod Position Indication Reed Switches.Corrective Maint Will Be Comple | /03L-0:on 810122,rod 26-35 Did Not Have Position Indication at Position 03 & Rod 34-35 Did Not Have Position Indication at Position 02.Caused by Defective Rod Position Indication Reed Switches.Corrective Maint Will Be Completed | | | 05000325/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000324/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000324/LER-1981-013-03, /03L-0:on 810119,HPCI Sys Component Test Tp 9.3.a Could Not Be Completed.Caused by Failed Motor on CST Suction Valve F004.Motor Sent to Svc Contractor to Be Repaired | /03L-0:on 810119,HPCI Sys Component Test Tp 9.3.a Could Not Be Completed.Caused by Failed Motor on CST Suction Valve F004.Motor Sent to Svc Contractor to Be Repaired | | | 05000324/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000325/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000325/LER-1981-013-03, /03L-0:on 810122,rod Worth Minimizer Sys Rod Blocks Were Received W/Proper Adherence to Control Rod Pattern Pull Sheet.Caused by Inadequate Procedures.Rods Pulled to Correct Position | /03L-0:on 810122,rod Worth Minimizer Sys Rod Blocks Were Received W/Proper Adherence to Control Rod Pattern Pull Sheet.Caused by Inadequate Procedures.Rods Pulled to Correct Position | |
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