LER-1981-051, /03L-0:on 810925,during Normal Operation,Coupling Came Apart on 3EA Reactor Motor Operated Valve Board Motor Generator Set.Caused by Slippage of Retainer Ring.Ring Replaced |
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NRC FORM 3G6 U. S. WUCLE AR REGULATORV COMMISSION (7-77)
LICENSEE EVENT REPORT CONTROL BLOCK:
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8 60 61 DOCKE T NUUBE R 68 fPJ E.VEN T DATE 14 IS REPOR T D ATE 83 EVENT DESCRIPTION AND PROBADLE CONSEQUENCES h l~oT2] l During normal operation, coupling came apart on 3EA reactor MOV board MG set lolal [due to slippage of retainer ring. (T.S. 3.9.A.4f and 3.9.B.ll), rendering the MG l
9 ;4 j l set inoperable. There was no danger to the health or safety of the public.
g Io ist i Redundant systems were availabic and operable. Previous similar event: BFRO-50-296/
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40 41 42 43 44 47 CAuSE oESCRIPTION ANC CORRECTIVE ACT!ONS h gi;o l Coupling came apart due to slippage of retainer ring. The old retainer ring was l3 ;,, l replaced by a new one, and the Waldron size +1g Powerline, part 148683 coupling gwas reassembled and inbricated. This is considered a randon failure due to a slightly,
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Form BFA17
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6/04/81-LER SUPPLDIENTAL INFORMATION-I DFRO 296 ~ / 81051 _ Technical Specification Involved -
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. Reported -Under Technical Specificationf 6.7.2.b(2)*nate due Nnc:_ 10/25/81-
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. Date of. Occurrence 9/25/81 Time of Occurrence.
1729
-: Unit 3
.I I'ientification and Description ~of Occurrence:
Coupling came apart on 3EA reactor MOV board MG set due to slippage' of. retainer ring.
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.I Conditions Prior to Occurrence:
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Unit 1 in refueling outage.
Unit 2 at 98%.
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Unit 3 at 97%.
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Action specified in the Technical Specification Surveillance Requirements met
_due to inoperabic equipment.
Describe.
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I Apparent Cause of Occurrence:
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Coupling came apart due to slippage of the retainer ring. The retainer ring
. was apparently deformed during installation.
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_ Analysis of Occurrence:
There was no danger to the health or safety of the public, no. release of activity,-
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no damage to the plant or equipment, and no resulting significant. chain of events.
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_ Corrective Action:
- The old retainer-ring was replaced by a new one, and the coupling reassembled and lubricated. This is considered a random failure due to a slightly' deformed retainer ring, and no further recurrence control is required.-
Failure Data:
BFRO-50-296/81050.
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Perio'd - Lifetime;' Responsibility - Document Control Supervisor
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