05000296/LER-1981-051-03, /03L-0:on 810925,during Normal Operation,Coupling Came Apart on 3EA Reactor Motor Operated Valve Board Motor Generator Set.Caused by Slippage of Retainer Ring.Ring Replaced

From kanterella
(Redirected from ML20011A611)
Jump to navigation Jump to search
/03L-0:on 810925,during Normal Operation,Coupling Came Apart on 3EA Reactor Motor Operated Valve Board Motor Generator Set.Caused by Slippage of Retainer Ring.Ring Replaced
ML20011A611
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 10/23/1981
From: Holder G
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20011A604 List:
References
LER-81-051-03L-02, LER-81-51-3L-2, NUDOCS 8110290179
Download: ML20011A611 (2)


LER-1981-051, /03L-0:on 810925,during Normal Operation,Coupling Came Apart on 3EA Reactor Motor Operated Valve Board Motor Generator Set.Caused by Slippage of Retainer Ring.Ring Replaced
Event date:
Report date:
2961981051R03 - NRC Website

text

NRC FORM 3G6 U. S. WUCLE AR REGULATORV COMMISSION (7-77)

LICENSEE EVENT REPORT CONTROL BLOCK:

l l

l l

l lh (PLE ASE PRINT OR TYPE ALL REQUIRED INFORMATION) lo lil l A lL lB lR lF l 3 l@l 0l 0l -l 0l 0l 0l 0l 0l -l 0l 0l@l 4l 1l 1l 1l 1l@l l

lg 7

8 >

LICENSE E CODE 14 lb LICE NSE NUP.*BE R 16 26 LICENSE TYPE JO 57 C A T $8 CON'T loli!

s]'l L@)l 0 l 5 l 0 l 0 l0 l 2 l 9 l 6 @,0 'l 9 l 2 l5 l 8 l1 l@ll ] 0 l 2 l 3 l 8l 1l@

y 7

8 60 61 DOCKE T NUUBE R 68 fPJ E.VEN T DATE 14 IS REPOR T D ATE 83 EVENT DESCRIPTION AND PROBADLE CONSEQUENCES h l~oT2] l During normal operation, coupling came apart on 3EA reactor MOV board MG set lolal [due to slippage of retainer ring. (T.S. 3.9.A.4f and 3.9.B.ll), rendering the MG l

9 ;4 j l set inoperable. There was no danger to the health or safety of the public.

g Io ist i Redundant systems were availabic and operable. Previous similar event: BFRO-50-296/

Io is i l 81050.

lolill I

fTITI L I

7 8 3 80 SYSTEM

CAUSE

CAUSE COYP.

VALVE CODE CCDE SUBCODE COMPONENT COOE SUECODE SUBCODE 10191 i c l B jg gg l Blg l Ml El C[ Fl Uj Nl@ l Z lg ]g 1

8 9

10 11 12 13 18 1)

?O SEQUEN Ti AL OCCUR h E NCE PEPORT REVISION LER AO Ek EN T YE AR R EPOR T NO.

CODE TYPE NO.

O g,2;V Ialil I-I I 01 sl 11 l/l 1013I It I l-J UU

_ 21 2J 23 24 26

?!

23 TJ 3J 31 32 ACT!O'J FUTUDE E F ; 1CT SuuTDOWN ATTACHMENT NP R D-4 PRIVE CCMP.

COYPCNENT TAKEN ACTION O'

iANT YETHOD HOURS SUB VIT T ED FORM SUB.

St,PP LI E R IUANUFACTURER lA l@l Zlh IZ lh l Zlh l 0l 0l 0l 0l l Yl@

[NJ@

[Lj@

l Wl 0 l 1 l 6l@

33 34 f5 Jfi 3/

40 41 42 43 44 47 CAuSE oESCRIPTION ANC CORRECTIVE ACT!ONS h gi;o l Coupling came apart due to slippage of retainer ring. The old retainer ring was l3 ;,, l replaced by a new one, and the Waldron size +1g Powerline, part 148683 coupling gwas reassembled and inbricated. This is considered a randon failure due to a slightly,

,,,3; jdeformed retainer ring, and no further recurrence control is required.

g l i 141 I i

7 8 3 80 ST N P'TA E H OTHE H ST A TUS ts OV DISCaVEHY OESCRIPTION lt l5 l l E l@ [0l 9l 7l@l NA l

l Algl operator observed.

l ASTiviTY Cc"} T e. T

".mNi or Amn v (E) toc Anum or nEttuE h nrty,SE o nP nE tr a U

e li 16I U @ l Zl/@ l l

l l

,A

,7 8 3 10 11 44 45 80 PER$g.p,[L [wPCtyq(5 5

I i i i l L I o'REqI.J@l Z l@l NU' Tm og s;riipiiry 4

"^

l d '

PE n.;ov.E th s; )n?

ES o. _ :n;P ore.(41) wmn

{ i 1 a l l 0 l 0 l 0 l@l l

NA r

a,

n a

es Lov r)F UH f, A* *ar;E T O r z.cr t# t v [^

rii OLSchtPT '

{ i l 9 l l <- l@l l

NA 8110290179 el1023

., 3 iu DR ADOCK 05000296 Nac usE ONtv 33

[" %'{nm.,@

s j / [ o l h@l PDR

,m j

lilllllllllll;

.3 m

o n9 80 a Gene Holder (205) 729-6134 o

NAvs Or puEoARsn enna:E

3.

j, 7.4 Tennessee Valley Authority :

Browns: Ferry Nuclear Plant =.

Form BFA17

? BF 15.2 -

6/04/81-LER SUPPLDIENTAL INFORMATION-I DFRO 296 ~ / 81051 _ Technical Specification Involved -

3 9 B ll

. Reported -Under Technical Specificationf 6.7.2.b(2)*nate due Nnc:_ 10/25/81-

~

q-

. Date of. Occurrence 9/25/81 Time of Occurrence.

1729

-: Unit 3

.I I'ientification and Description ~of Occurrence:

Coupling came apart on 3EA reactor MOV board MG set due to slippage' of. retainer ring.

c r

.I Conditions Prior to Occurrence:

i

[

Unit 1 in refueling outage.

Unit 2 at 98%.

r.

l J

Unit 3 at 97%.

n i

I -

Action specified in the Technical Specification Surveillance Requirements met

_due to inoperabic equipment.

Describe.

None l

I Apparent Cause of Occurrence:

.[

Coupling came apart due to slippage of the retainer ring. The retainer ring

. was apparently deformed during installation.

.i

. r--

i -

1

_ Analysis of Occurrence:

There was no danger to the health or safety of the public, no. release of activity,-

{

no damage to the plant or equipment, and no resulting significant. chain of events.

}_-t:

l I

J 1

_ Corrective Action:

The old retainer-ring was replaced by a new one, and the coupling reassembled and lubricated. This is considered a random failure due to a slightly' deformed retainer ring, and no further recurrence control is required.-

Failure Data:

BFRO-50-296/81050.

'~

  • Retention:

Perio'd - Lifetime;' Responsibility - Document Control Supervisor

  • Revision :

7 c'