05000280/LER-1981-057-03, /03L-0:on 810827,circuit Breaker for Motor Operated Valve Found Open.Caused by Accidental Bumping. Breaker Reclosed & Appropriate Valve Indication Ack

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/03L-0:on 810827,circuit Breaker for Motor Operated Valve Found Open.Caused by Accidental Bumping. Breaker Reclosed & Appropriate Valve Indication Ack
ML20010H727
Person / Time
Site: Surry  
Issue date: 09/22/1981
From: Joshua Wilson
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20010H722 List:
References
LER-81-057-03L-02, LER-81-57-3L-2, NUDOCS 8109290218
Download: ML20010H727 (2)


LER-1981-057, /03L-0:on 810827,circuit Breaker for Motor Operated Valve Found Open.Caused by Accidental Bumping. Breaker Reclosed & Appropriate Valve Indication Ack
Event date:
Report date:
2801981057R03 - NRC Website

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o ATTACHMEKI 1 SURRY POWER STATION. UNIT 2 DOCKET NO:

50-261 REPORT NO:

El-O',7 / 03L-0 EVENT PATE:

GE-27 -81 MOV-2867B BREAKER OPEN 1.

EVENT DESCRIPTION

With the unit at 100% power, a routine walkdown of the control board revealed the circuit breaker for MOV-2867B (Beron Injection Tank Inlet) to be oper..

These breakers had been verified closed 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> earlier while performing the control board indicating light walk-down. The redundan flow path was checked to ensure it was energized.

This event is contrary to T.S.3.3.A.7 and reportable in accordance with T.S.6.6. 2.b (2).

2.

PROBABLE CONSEQUENCES AND STATUS OF REDUNDANT EQUIPME'iT:

Upon receipt of a safety injection, signal, the BIT valves are automatically opened and the BIT contents are pumped into the RCS by the High Head Safety Injection Pumps. The redundant BIT flow path, MOV-2867A, was operable through-out this event; therefore, the health and safety of the public were not affected.

3.

CAUSE

The breaker is located in an area where extensive design change activity was unuerway.

It is likely that the breaker was accidentally bumped, causing it to open.

4.

IMMEDIATE CORRECTIVE ACTION

The breaker was closed and the valve responded properly.

5.

SUBSEQUENT CORRECTIVE ACTION:

None required.

6.

ACTIONS TAKEN TO PREVENT RECURRENCE:

The number of construction personnel authorized access to the switchgear room has been reduced.

7.

GENZPIC IMPLICATIONS:

None.

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