ML20010G859

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LER 81-036/03L-0:on 810812,svc Water Dilution Flow Recorder Had Been Inoperable Since 810708 Due to Broken Annubar. Caused by Personnel Not Recognizing This as Limiting Condition of Operation Event
ML20010G859
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 09/10/1981
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20010G841 List:
References
LER-81-036-03L-01, LER-81-36-3L-1, NUDOCS 8109220596
Download: ML20010G859 (2)


Text

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AE8CRT C ATE EVENT OESCBIPTICN AND PRCEAaLE CONSEOUENCES h o!: ; i At 1430 on 8/12/81, it was determined that the service water dilution flow recorder had  ;

o i fj l been inoperable since 8/7/81 due to a broken annubar. Tech. Spec. 3.3.3.10, in part, l aeai l requires the flow recorder to be operable. Tech. Spec. 3.3.3.10 action statement require-l ai3i j ments were met. Health / safety of the public was not affected.  ;

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i i2, l the Tech. Spec. action statement requirement of estimating the discharge canal dilution ,

ii7i i line flov rate every 4 ruurs was not met. However,aninvestigationrevealedthatadequatg ii iai l dilution flow did exist for the 5 days from 8/7/81 to 8/12/81. Upon discovery of the ,

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NAME_0E_ PREPARER: W. G. Hairston, III P110NE: (205) 899-5156 ,

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.-e LER 81-036/03L-0 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS (cont'd) condition, the action requirements were. initiated and following necessary repairs and functional tests, the service water dilution f. low recorder was returned to service at 1310 on 8/21/81.. Personnel-involved have been counseled concerning

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