LER-1981-062, /03L-0:on 810810,inadvertent Actuation of ECCS Train B Occurred,Resulting in Borated Water Concentration in Injection Tank Dropping Below Tech Spec Limit.Caused by Defective Low Pressurizer Reset & Block Switch |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 3391981062R03 - NRC Website |
|
text
'
U.S. NUCLEAR REGULATORY COMMISSION i
LICENSEE EVENT REPORT CONTROL BLOCK / / / / / / / (1)
(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
/0/1/
/V/A/N/A/S/2/ (2)
/0/0/-/0/0/0/0/0/-/0/0/ (3)
/4/1/1/1/1/ (4)
/ / / (5)
LICENSEE CODE LICENSE NUMBER LICENSE TYPE CAT
/0/1/
E L/ (6)
/0/5/0/0/0/3/3/9/
(7)
/0/8/1/0/8/1/
(8) /o/9/o/7/a/1/ (9)
I DOCKET NUMBER EVENT DATE REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES (10)
/0/2/
/ On August 10, 1981, during Mode-3 operation, an inadvertent actuation of Train B /
/0/3/
/ of the Emergency Core Cooling System occurred.
This actuation caused the borated /
/0/4/
/ water concentration in the Boron Injection Tank to drop below the minimmr re-
/
/0/5/
/ quired by T.S. 3.5.4.1.
Since this was an inadvertent actuation, the health and /
i
/0/6/
/ safety of the public were not affected. This event is reportable pursuant to
/
/0/7/
/ T.S. 6.9.1.9.b. an( the special reporting requirement of T.S. 3.5.2.
/
/0/8/
/
/
i SYSTEM
CAUSE
CAUSE COMr.
VALVE l
CODE CODE SUBCODE COMP 0NFNT CODE SUBCODE SUBCODE
/0/9/
/S/F/ (11) /E/ (12) /A/ (13) /C/K/T/B/K/R/ (14) /E/ (15)
LZ/ (16)
SEQUENTIAL OCCURRENCE REPORT REVISION LER/R0 EVENT YEAR REPORT NO.
CODE TYPE NO.
(17) REPORT NUMBER
/8/1/
L-/ /0/6/2/
/\\/
/0/3/
/L/
/-/
/0/
ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRD-4 PRIME COMP. COMPONENT TAKEN ACTION ON PLANT METHOD HOURS SUBMITTED FORM SUB. SUPPLIER MANUFACTURER g/ (18) LA/ (19) [C/ (20) LZ/ (21) /0/0/0/0/ (22) /Y/ (23) /N/ (24) /N/ (25) /W/1/2/0/ (26) i CAUSE DESCRIPTION AND CORRECTIVE ACTIONS (27)
/1/0/
/ This event was caused by a defective " Low Pressurizer Pressure SI" Reset and
/
/1/1/
/ diock switch. When the switch was released from the " Block" position, it spring /
l
/1/2/
/ returned past the center to the " Reset" position reinstating the Low Pressurizer /
/1/3/
/ Pressure SI function. The detective switch will be replaced when unit conditions /
/1/4/
/ permit.
/
FACILITY METHOD OF DISCOERY DESCRI m 0N (32)
/ (30)DISCOW RY STATUS
% POWER OTHER STATUS LA/ (31)
/ Operator Observation /
L1/5/
[G/ (28)
/0/0/0/ (29) /
N/A ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY (35)
LOCATION OF RELEASE (36)
/1/6/
LZ/ (33)
[Z/ (34) /
NA
/
/
NA
/
PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION (39)
/1/7/ /0/0/0/ (37) /Z/ (38)
/
NA
/
PERSONNEL INJURIES NUMBER DESCRIPTION (41)
/1/8/ /0/0/0/ (40) /
NA
/
LOSS OF OR DAMAGE TO FACILITY (43)
TYPE
DESCRIPTION
/1/9/
/Z/ (42) /
NA
/
PUBLICITY ISSUED DESCRIPTION (45)
NRC USE ONLY
/2/0/
/N/ (44) /
NA
/////////////
8109110240 ggo902 SR W. R. MRTWRIGHT PHONE (703) 894-5151 PDR ADOCK 05000339 S
PDR
0.
Virginia Electric and Pcwer Company North Anna Power Station, Unit 2 Attachment: Page 1 of 2-Docket No. 50-339 Report No. LER 81-062/03L-0
Description of Event
On August 10, 1981, at 1851 while in Mode 3, the ECCS Train B actuated when the Low Pressurizer Pressure SI Block / Reset switch spring returned past the center (neutral) position to the " Reset" position.
This caused an inadvertent reinstating of the "Lo Pzr Press" SI function.
'Since system pressure at that time was below the activation setpoint of 1765 psig, (cctual pressure was 1494 psig), the ECCS actuated.
The actions of 2-EP-5 were completed and the signal was reset at 1854 when it was determined to be an inadvertent actuation.
As a result of the Safety Injection, the contents of the Boron Injection Tank (BIT) were flushed to the Reactor Coolant System which caused the boron concentration in the BIT to fall below the minimum Technical Specification limit of 20,000 ppm of borated wa.er.
The BIT did perform it's intended function.
2 All of the Train B SI equipment operated as required. This was the third actuation of ECCS reportable as per T.S. 6.9.2.
The usage factor for the affected SI injection nozzles has not exceeded 0.70.
The ECCS actuation is reportable as per T.S. 3.5.2 which requires a Special Report in accordance with T.S. 6.9.2 within 90 days. This Licensee Event Report is intended to satisfy the T.S. 6.9.2 requirements.
Probable Consequences of Occurrence The purpose of the Emergency Core Cooling System is to ensure adequate cooling of the reactor in the event of a loss of coolant accident.
Although the safety injection system performed its intended function to inject borated water into the Reactor Coolant System, an actual accident condition did not exist and therefore the SI was not required. As a result, the health and safety of the general public were not affected.
Cause of Event
The "Lo Pzr Preas" Block switch has three positions; Block, Reset and Center. Both the Block and Reset positions spring return 'to the center position.
When the switch was moved to the " Block" position and released, it returned past the center to the " Reset" position on the Train B switch which unblocked the Train B Low Pressure SI function.
Since system pressure was below the Lo Pzr Pressure SI setpoint of 1765 psig the ECCS inadvertently actuated.
a.
Immediate Corrective Action
The unit was stabilized and the equipment returned to normal.
Using an approved procedure, the defect in the switch was demonstrated several times confirming the cause of the event. This was done without actually injecting water into the RCS. All Control Room Operators were made aware of the defect in the switch.
Scheduled Corrective Action When a replacement switch can be obtained and when unit conditiors allow, the switches will be replaced.
Actions Taken to Prevent Reccurrence All control room operators have been made aware of the deiect in the switch and have been instructed not to release the switch from the unblocked position but to return it to center prior to releasing the switch.
No further actions are necessary at this time. The SI blocked status lights provida positive indication of when the SI function is blocked or when it is reset.
Generic Implications There are no generic implications associated with this event.
i f
I e
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000339/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000339/LER-1981-001-03, /03L-0:on 810101,average RCS Temp Outside Tech Specs on Two Occasions.First Caused by Vol Control Tank Being Overborated;Second by Overcooling Primary.Steam Generator Blowdown Secured,Rods Withdrawn & RCS Diluted | /03L-0:on 810101,average RCS Temp Outside Tech Specs on Two Occasions.First Caused by Vol Control Tank Being Overborated;Second by Overcooling Primary.Steam Generator Blowdown Secured,Rods Withdrawn & RCS Diluted | | | 05000338/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000338/LER-1981-001-03, /03L:on 810318 & 19,nitrogen Supply Tank Pressure for Associated Pressure Operated Relief Valves Dropped Below Min Required to Operate Valves for Low Temp RCS Overpressurization Protection.Caused by Leaks in Tanks | /03L:on 810318 & 19,nitrogen Supply Tank Pressure for Associated Pressure Operated Relief Valves Dropped Below Min Required to Operate Valves for Low Temp RCS Overpressurization Protection.Caused by Leaks in Tanks | | | 05000338/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000338/LER-1981-002-03, /03L-0:on 801231,pressurizer Power Operated Relief Valve Declared Inoperable Because of Low Nitrogen Gas Supply Tank Pressure in 1-GN-TK-1A.Caused by Excessive Usage of Nitrogen to Cycle Relief Valves to Reduce RCS Pressure | /03L-0:on 801231,pressurizer Power Operated Relief Valve Declared Inoperable Because of Low Nitrogen Gas Supply Tank Pressure in 1-GN-TK-1A.Caused by Excessive Usage of Nitrogen to Cycle Relief Valves to Reduce RCS Pressure | | | 05000339/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000339/LER-1981-002-03, /03L-0:on 801230,w/unit in Mode 1,steam Flow Channel III Became Erratic W/O Any Annunciators or Computer Alarms.Cause Unknown.Channel Placed in Trip Condition, Calibr & Returned to Svc | /03L-0:on 801230,w/unit in Mode 1,steam Flow Channel III Became Erratic W/O Any Annunciators or Computer Alarms.Cause Unknown.Channel Placed in Trip Condition, Calibr & Returned to Svc | | | 05000338/LER-1981-003-03, /03L-0:on 810104,loop 3 Reactor Coolant Flow Protection Channel II,F-1435,found Out of Tolerance High. Caused by Voltage Drift in Flow Transmitter Serving Loop. Channel Recalibr | /03L-0:on 810104,loop 3 Reactor Coolant Flow Protection Channel II,F-1435,found Out of Tolerance High. Caused by Voltage Drift in Flow Transmitter Serving Loop. Channel Recalibr | | | 05000338/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000339/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000339/LER-1981-003-03, /03L-0:on 810104,casing Cool Tank Level Indication LI-RS-203B Failed High.Caused by Frozen Transmitter Due to Heat Tracing Failure.Transmitter Was Thawed Out & Redundant Heat Tracing Turned on | /03L-0:on 810104,casing Cool Tank Level Indication LI-RS-203B Failed High.Caused by Frozen Transmitter Due to Heat Tracing Failure.Transmitter Was Thawed Out & Redundant Heat Tracing Turned on | | | 05000338/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000338/LER-1981-004-03, /03L-0:on 801229,three Motor Operated Valves Failed to Actuate During Containment Depressurization Actuation Functional Test.Caused by Loose Lead on Breaker/ Controller & Water in Motor.Valves Repaired | /03L-0:on 801229,three Motor Operated Valves Failed to Actuate During Containment Depressurization Actuation Functional Test.Caused by Loose Lead on Breaker/ Controller & Water in Motor.Valves Repaired | | | 05000339/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000339/LER-1981-004-03, /03L-0:on 810104,during Mode 1 Operation,Flux Penalty Summing Amplifier Found Failed During Loop Calibr Check.Caused by Faulty NSA Card.Card Replaced & Calibr | /03L-0:on 810104,during Mode 1 Operation,Flux Penalty Summing Amplifier Found Failed During Loop Calibr Check.Caused by Faulty NSA Card.Card Replaced & Calibr | | | 05000338/LER-1981-005-03, /03L-0:on 810105,discovered That Control Room Floor Sleeve 1FC00108 Was Never Resealed After Being Previously Breached for Cable Installation.Caused by Failure of Personnel to Follow Procedures.Sleeve Resealed | /03L-0:on 810105,discovered That Control Room Floor Sleeve 1FC00108 Was Never Resealed After Being Previously Breached for Cable Installation.Caused by Failure of Personnel to Follow Procedures.Sleeve Resealed | | | 05000338/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000339/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000339/LER-1981-005-03, /03L-0:on 810106,greater than 12-step Disagreement Noted Between Individual Rod Position for Rod B08 in Control Bank D & Group Demand Position.Caused by Voltage Drift in Signal Conditioning Card.Indicator Channel Recalibr | /03L-0:on 810106,greater than 12-step Disagreement Noted Between Individual Rod Position for Rod B08 in Control Bank D & Group Demand Position.Caused by Voltage Drift in Signal Conditioning Card.Indicator Channel Recalibr | | | 05000338/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000338/LER-1981-006-03, /03L-0:on 810113,pressurizer Pressure Transmitter PT 1457 Found Out of Calibr.Caused by Instrument Drift. Channel Recalibr | /03L-0:on 810113,pressurizer Pressure Transmitter PT 1457 Found Out of Calibr.Caused by Instrument Drift. Channel Recalibr | | | 05000339/LER-1981-006-03, /03L-0:on 810107,w/unit at 1% Power,Average RCS Temp Less than 541 F on Two Occasions.Caused by Overfeeding Steam Generators Due to Feedwater Control Problems.Condenser Steam Dumps Closed & Reactor Temp Increased | /03L-0:on 810107,w/unit at 1% Power,Average RCS Temp Less than 541 F on Two Occasions.Caused by Overfeeding Steam Generators Due to Feedwater Control Problems.Condenser Steam Dumps Closed & Reactor Temp Increased | | | 05000338/LER-1981-007-99, Plug Found Missing from Tube at Row 1,column 12.On 810202,two More Plugs Found Missing.Caused by Bad Seals.One Tube Was Replugged on 810124.Other Two Tubes Replugged on 810303 | Plug Found Missing from Tube at Row 1,column 12.On 810202,two More Plugs Found Missing.Caused by Bad Seals.One Tube Was Replugged on 810124.Other Two Tubes Replugged on 810303 | | | 05000339/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000339/LER-1981-007-03, /03L-0:on 801230,boron Concentration in Boron Acid Storage Tank C & Boron Injection Tank Below Tech Spec. Probably Caused by Inleakage of Unknown Source.Boric Acid Transferred to Tank C.Investigation of Leak Underway | /03L-0:on 801230,boron Concentration in Boron Acid Storage Tank C & Boron Injection Tank Below Tech Spec. Probably Caused by Inleakage of Unknown Source.Boric Acid Transferred to Tank C.Investigation of Leak Underway | | | 05000338/LER-1981-007, Forwards Updated LER 81-007/99X-1 | Forwards Updated LER 81-007/99X-1 | | | 05000339/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000338/LER-1981-008-03, /03L-0:on 810117,steam Generator a Protection Channel 2 Narrow Range Level Transmitter LT-1475 Found Out of Calibr.Caused by Voltage Drift in Level Transmitter Serving Instrument Loop.Recalibr & Returned to Svc | /03L-0:on 810117,steam Generator a Protection Channel 2 Narrow Range Level Transmitter LT-1475 Found Out of Calibr.Caused by Voltage Drift in Level Transmitter Serving Instrument Loop.Recalibr & Returned to Svc | | | 05000338/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000339/LER-1981-008-03, /03L-0:on 810107,primary Coolant Iodine Isotopic Analysis Not Made within 2-6 Hour Per Tech Spec Re Power Changes Exceeding 15% Per Hour.Caused by Failure of Operations Personnel to Follow Procedures.Sample Analyzed | /03L-0:on 810107,primary Coolant Iodine Isotopic Analysis Not Made within 2-6 Hour Per Tech Spec Re Power Changes Exceeding 15% Per Hour.Caused by Failure of Operations Personnel to Follow Procedures.Sample Analyzed | | | 05000339/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000339/LER-1981-009-03, /03L-0:on 810107,during Leak Test Containment Personnel Hatch Outer Door Leaked Air Past Seals.Caused by Improper Fitup of Door Seals to Frame.Door Adjusted | /03L-0:on 810107,during Leak Test Containment Personnel Hatch Outer Door Leaked Air Past Seals.Caused by Improper Fitup of Door Seals to Frame.Door Adjusted | | | 05000338/LER-1981-009-03, Combined Leakage in Excess of Allowable Limits Noted from 14 Electrical Penetrations & 23 Valves.Valve Leakage Caused by Valve Seat Deterioration or Limit Switch Drift | Combined Leakage in Excess of Allowable Limits Noted from 14 Electrical Penetrations & 23 Valves.Valve Leakage Caused by Valve Seat Deterioration or Limit Switch Drift | | | 05000338/LER-1981-009, Forwards Updated LER 81-009/03X-1 | Forwards Updated LER 81-009/03X-1 | | | 05000338/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000338/LER-1981-010-03, /03L-0:on 810211,w/unit in Mode 6,containment Purge & Exhaust Isolation Sys Was Rendered Inoperable When Power to MOV-HV-100B,D Was Lost.Caused by Fault on High Resistance Connection.Defective Parts Replaced | /03L-0:on 810211,w/unit in Mode 6,containment Purge & Exhaust Isolation Sys Was Rendered Inoperable When Power to MOV-HV-100B,D Was Lost.Caused by Fault on High Resistance Connection.Defective Parts Replaced | | | 05000339/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000339/LER-1981-010-03, /03L-0:on 810113,w/unit at 100% Power,Overspeed Trip of Turbine Driven Auxiliary Feedwater Pump Occurred During Surveillance Testing.Caused by Failure of Turbine Governor to Control Speed.Governor Was Replaced | /03L-0:on 810113,w/unit at 100% Power,Overspeed Trip of Turbine Driven Auxiliary Feedwater Pump Occurred During Surveillance Testing.Caused by Failure of Turbine Governor to Control Speed.Governor Was Replaced | | | 05000338/LER-1981-011-03, /03L-0:on 810117,w/unit in Mode 6,loss of Power to Radiation Monitor Common Alarms Panel Was Experienced for Less than 5 Minutes.Caused by Failure of Electrician to Switch Power to Unit 2 During Unit 1 Trip | /03L-0:on 810117,w/unit in Mode 6,loss of Power to Radiation Monitor Common Alarms Panel Was Experienced for Less than 5 Minutes.Caused by Failure of Electrician to Switch Power to Unit 2 During Unit 1 Trip | | | 05000338/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000339/LER-1981-011-03, /03L-0:on 810114,w/unit at 100% Power,Breaker for 2-QS-P-1A Spray Pump Racked Out & Suction Valve MOV-QS-200A Closed & de-energized.Caused by Dirty Seat on Vent Valve. Valve Seat Cleaned & Disc Lapped | /03L-0:on 810114,w/unit at 100% Power,Breaker for 2-QS-P-1A Spray Pump Racked Out & Suction Valve MOV-QS-200A Closed & de-energized.Caused by Dirty Seat on Vent Valve. Valve Seat Cleaned & Disc Lapped | | | 05000339/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000338/LER-1981-012-03, /03L-0:on 810118,fuel Bldg Supply & Exhaust Fan Suction Dampers Switched to Failed Position,Bypassing Iodine Filter Bank When Control Bank Was Isolated.Caused by Low Outdoor Temp.Dampers Positioned to Exhaust Through Filter | /03L-0:on 810118,fuel Bldg Supply & Exhaust Fan Suction Dampers Switched to Failed Position,Bypassing Iodine Filter Bank When Control Bank Was Isolated.Caused by Low Outdoor Temp.Dampers Positioned to Exhaust Through Filter | | | 05000338/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000339/LER-1981-012-03, /03L-0:on 810121,containment Pressure Protection Channel 3 Failed Low.Caused by Blown Transistor on Loop Power Supply Card,Resulting in Power Loss to Each Comparator in Loop.Failed Card Replaced W/Calibr Card | /03L-0:on 810121,containment Pressure Protection Channel 3 Failed Low.Caused by Blown Transistor on Loop Power Supply Card,Resulting in Power Loss to Each Comparator in Loop.Failed Card Replaced W/Calibr Card | | | 05000339/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000339/LER-1981-013-03, /03L-0:on 810126,containment Hi & hi-hi Pressure Channel III Annunciator Energized.Caused by Instrument Drift in Nonisolated Power Supply Card S/N 5088,increasing Output Voltage.Card Replaced & Channel Calibr | /03L-0:on 810126,containment Hi & hi-hi Pressure Channel III Annunciator Energized.Caused by Instrument Drift in Nonisolated Power Supply Card S/N 5088,increasing Output Voltage.Card Replaced & Channel Calibr | | | 05000338/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000339/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | |
|