ML20010E546

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Notice of Violation from Insp on 810701-0803
ML20010E546
Person / Time
Site: Oyster Creek
Issue date: 08/21/1981
From: Brunner E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20010E545 List:
References
50-219-81-14, NUDOCS 8109040242
Download: ML20010E546 (2)


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APPEllDIX A i

it0TICE OF VIOLATI0tl 4

Jersey Central Power and Light Company Docket flo. 50-219 Oyster Creek fluclear Generating Station l

License flo. DPR 16 As a result of the inspection conducted on July 1 - August 3,1981 and in i

accordance with the Interim Enforcement Policy, 45 FR 66754 (October 7,1980),

i the following violations were identified:

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A.

Technical Specification 3.5.3.1 states in part, " Secondary containment integrity shall be maintained at all times unless all of the following conditions are met..."

f Technical Specification 1.14 states in part, " Secondary containment integrity means that the reactor buildfrg is closed and the following j

conditions are net..."

c.

All reactor building ventilation system automatic isolation valves are operable or are secured in the closed position."

i Contrary to the above, secondary containment integrity was not maintained i

from about 7:00 p.m., July 14, 1981 until about 10:15 a.m., July 15, 1981, i

during which time secondary containment integrity was required, in that i

a reactor building ventilation system automatic isolation valve, V-28-22, was inoperable and not secured in the closed position.

l This is a Severity Level IV violation (Supphment I.D.)

B.

/cendment 54 to Provi.iional Operating License DPR-16, dated May 8,1981 j

modified Technical Specifications by incorporating section 4.13.A.

J Technical Specification 4.13.A requires that each accident mcnitoring instrument channel shall be demonstrated operable by perfonnance of a i

j channel check at least once per 31 days.

Contrary to the above, no channel checks of the accident monitoring l

instrument channels were perfonned from flay 8,1981 until July 13, 1981, a ceriod of greater than 31 days.

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This is a Severity Level IV violation (Supplement I.D.)

l C.

Technical Specification 3.4.E states in part, "The core spray and contain-ment spray pump compartments doors shall be closed at all times except detring passage...".

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2 8109040242 810621 PDR-ADOCK 05000219 S. _ -, -. l ?. =., -, _,,.-,.

Appendix A 2

Contrary to the above, on July 31, 1981, at abuut 5:30 p.m., the south-east containment spray pump compartrant door was found open and not being used for passage. This is a recurrence of three similar events that were reported in Licensee Event Reports 79-36, 80-32, and 81-07.

This is a Severity Level IV violation (Supplement I.D.)

Pursuant to the provisions of 10 CFR 2.201, Jersey Central Power and Light Company, Incorporated is hereby required to submit to this office within thirty days of the date of this Hotice a written statenent or explanation in reply incit:,ina the corrective steps which have been taken and results achieved; corrective steps which will be taken to avoid further violations; and the date when full compliance will be achieved. Under the authority of Section 182 of the Atanic Energy Act of 1954, as amended, this response shall be submitted under oath or affirmation. Where good cause is shown, consideration will be given to extending your response time.

The responses directed by this Notice are not subject to the clearance procedures of the Office of itanagement and Budget as required by the Paperwurk Reduction Act of 1980, PL 96-511.

(., $u~wo N

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Dated

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Eldon J. Brunner, Acting Director Divisien of Resident and Project Inspection l

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