05000364/LER-1981-030-03, /03L-0:on 810727,steam Generator 2B Steam Flow Transmitter FT-485 Declared Inoperable.Caused by Kerotest Valve Plug Remaining Closed When Valve Handwheel Was Fully Open.Valve Exercised & Valve Plug Opened

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/03L-0:on 810727,steam Generator 2B Steam Flow Transmitter FT-485 Declared Inoperable.Caused by Kerotest Valve Plug Remaining Closed When Valve Handwheel Was Fully Open.Valve Exercised & Valve Plug Opened
ML20010D220
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 08/17/1981
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20010D207 List:
References
LER-81-030-03L-01, LER-81-30-3L-1, NUDOCS 8108240108
Download: ML20010D220 (1)


LER-1981-030, /03L-0:on 810727,steam Generator 2B Steam Flow Transmitter FT-485 Declared Inoperable.Caused by Kerotest Valve Plug Remaining Closed When Valve Handwheel Was Fully Open.Valve Exercised & Valve Plug Opened
Event date:
Report date:
3641981030R03 - NRC Website

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