05000220/LER-1981-032-03, /03L-0:on 810705,during Normal Operation,Automatic Reactor Scram Occurred on Low Reactor Water Level.Caused by Time Delay Due to Malfunctioning HPCI Controller.Controller Replaced & New Controller Tested Properly

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/03L-0:on 810705,during Normal Operation,Automatic Reactor Scram Occurred on Low Reactor Water Level.Caused by Time Delay Due to Malfunctioning HPCI Controller.Controller Replaced & New Controller Tested Properly
ML20010A627
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 08/04/1981
From: Neild R
NIAGARA MOHAWK POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20010A620 List:
References
LER-81-032-03L, LER-81-32-3L, NUDOCS 8108110617
Download: ML20010A627 (1)


LER-1981-032, /03L-0:on 810705,during Normal Operation,Automatic Reactor Scram Occurred on Low Reactor Water Level.Caused by Time Delay Due to Malfunctioning HPCI Controller.Controller Replaced & New Controller Tested Properly
Event date:
Report date:
2201981032R03 - NRC Website

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