05000327/LER-1981-076-03, /03L-0:on 810627,during Mode 2,1A-A Safety Injection Pump Declared Inoperable When Water Found in Lube Oil.Caused by Condensation Buildup.Oil Changed & Lube Oil Cooler Checked for Leaks

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/03L-0:on 810627,during Mode 2,1A-A Safety Injection Pump Declared Inoperable When Water Found in Lube Oil.Caused by Condensation Buildup.Oil Changed & Lube Oil Cooler Checked for Leaks
ML20009G459
Person / Time
Site: Sequoyah Tennessee Valley Authority icon.png
Issue date: 07/24/1981
From: Harding M, Kirk G
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009G452 List:
References
LER-81-076-03L, LER-81-76-3L, NUDOCS 8108040281
Download: ML20009G459 (1)


LER-1981-076, /03L-0:on 810627,during Mode 2,1A-A Safety Injection Pump Declared Inoperable When Water Found in Lube Oil.Caused by Condensation Buildup.Oil Changed & Lube Oil Cooler Checked for Leaks
Event date:
Report date:
3271981076R03 - NRC Website

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