05000327/LER-1981-062-03, /03L-0:on 810531,following Reactor trip,turbine- Driven Auxiliary Feedwater Pump Failed to Deliver Full Flow. Caused by Speed Control Setpoint Drift.Trimpot Adjusted. Locking Nut Tightened & Locking Putty Applied

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/03L-0:on 810531,following Reactor trip,turbine- Driven Auxiliary Feedwater Pump Failed to Deliver Full Flow. Caused by Speed Control Setpoint Drift.Trimpot Adjusted. Locking Nut Tightened & Locking Putty Applied
ML20009F891
Person / Time
Site: Sequoyah Tennessee Valley Authority icon.png
Issue date: 06/26/1981
From: Harding M
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009F889 List:
References
LER-81-062-03L, LER-81-62-3L, NUDOCS 8108030142
Download: ML20009F891 (1)


LER-1981-062, /03L-0:on 810531,following Reactor trip,turbine- Driven Auxiliary Feedwater Pump Failed to Deliver Full Flow. Caused by Speed Control Setpoint Drift.Trimpot Adjusted. Locking Nut Tightened & Locking Putty Applied
Event date:
Report date:
3271981062R03 - NRC Website

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