05000348/LER-1981-045-03, /03L-0:on 810613,train Svc Water Loop a Declared Inoperable.Caused by Inoperable Emergency Recirculation Valve Due to Blown Control Circuit Fuse.Fuse Replaced,Valve Tested & Loop Returned to Svc on 810613

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/03L-0:on 810613,train Svc Water Loop a Declared Inoperable.Caused by Inoperable Emergency Recirculation Valve Due to Blown Control Circuit Fuse.Fuse Replaced,Valve Tested & Loop Returned to Svc on 810613
ML20009F655
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 07/07/1981
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009F641 List:
References
LER-81-045-03L, LER-81-45-3L, NUDOCS 8107310384
Download: ML20009F655 (1)


LER-1981-045, /03L-0:on 810613,train Svc Water Loop a Declared Inoperable.Caused by Inoperable Emergency Recirculation Valve Due to Blown Control Circuit Fuse.Fuse Replaced,Valve Tested & Loop Returned to Svc on 810613
Event date:
Report date:
3481981045R03 - NRC Website

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40 di OCC.<ET NUMSER 68 63 5'v ENT OATE 74 75 4EPOF,7 QATE 50 EVENT CESCRIPTICN AND PRCSABLE CCNSECUENCES h oi2i i At 0730 on 6/13/81, the "A" train service water 1000 was declared inoperable when it was 3 62: I determined that the emergency recirculation valve (v539) would not operate. Tech. Spec.

l 3,4i j3.7.4 requires two independent service water loops to be operable. Tech. Spec. 3.7.4 l

3,3; ; action statement requirements were met.

Health / safety of the public was not affected.

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41 42 43 44 47 CAUSE CESCRIP*1CN AND CCRP=CT" ACitCNS 2 iaiiThe event was caused by a blowi, control circuit fuse. The fuse was replaced and the

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jservice at 1430 on 6/13/81. This !s considered to be an isolated occurrence.

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NAME OF PREPMtER H. G. Hairston, III PHONE: (205) 899-5156 ao j