05000369/LER-1981-095-03, /03L-0:on 810606,flow Rate Measurement Instrumentation on Waste Monitor Tank a Declared Inoperable During Attempted Liquid Water Release.Caused by Supply Air Isolation Valve to Transmitter Left Closed Following Maint

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/03L-0:on 810606,flow Rate Measurement Instrumentation on Waste Monitor Tank a Declared Inoperable During Attempted Liquid Water Release.Caused by Supply Air Isolation Valve to Transmitter Left Closed Following Maint
ML20009F646
Person / Time
Site: McGuire Duke Energy icon.png
Issue date: 07/02/1981
From: Nardoci P
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009F636 List:
References
LER-81-095-03L, LER-81-95-3L, NUDOCS 8107310377
Download: ML20009F646 (1)


LER-1981-095, /03L-0:on 810606,flow Rate Measurement Instrumentation on Waste Monitor Tank a Declared Inoperable During Attempted Liquid Water Release.Caused by Supply Air Isolation Valve to Transmitter Left Closed Following Maint
Event date:
Report date:
3691981095R03 - NRC Website

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so y i On June 6, 1981, while in Mode 5. the flow rate measurement instrumentation on]

fcTT) I waste monitor tank (WMT) "A" was declared inoperable durine an attempted I

lat.1i liquid waste release (LWR). This was a violation of Technical Specification l

3.3.3.8 and reportable per Technical Specification 6.9.1.13B and is similar 1

I Io is j i I o t o 1 1 to previous RO #'s 81-66 and 81-94.

Because of the availability of other re-I lairJl lease measuring methods, this incident did no't adversely affect the health andt I

io!alI safety of the public'or the safe operation of the plant.

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31 of Technical Specification 3.3.3.8.

The I3 12#I released per action statement iiv.iI valve was opened and the instrument declared operational on Jun'a 8. 1981.

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