ML20009F620

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LER 81-069/03L-0:on 810426,while in Mode 3 Initial Fuel Loading,Cold Leg Accumulator D Low Level Alarm Received in Control Room.Caused by Leaking Safety Injection Test Header. Level Restored.Leaking Valve Will Be Replaced & Tested
ML20009F620
Person / Time
Site: McGuire Duke Energy icon.png
Issue date: 05/26/1981
From: Ouellette R
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009F615 List:
References
LER-81-069-03L, LER-81-69-3L, NUDOCS 8107310359
Download: ML20009F620 (1)


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l o t 21 I While in Mode 3. initial fuel loadine. a cold leg accumulator D low level i 10 21 I alarm was received in the Control Room. The level was below the minimum j t o i.I I required by Technical Specification 3.5.1.1 and thus is reportable per ,

l o 6 51 1 Technical Specification 6.9.1.13(b). Since there is only new fuel in the i to al I core and the other three accumulators remained operable, the health and  ;

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tiio t 1 The safety injection test header was leaking which allowed the accumulator ,

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