LER-1981-033, /03L-0:on 810616,lightning Struck Startup Transformer Causing Loss of Ac Power.Power Loss Tripped Air Handling Fans,Resulting in Temp Increase in Reactor Bldg. Cause Attributed to Failure of Lightning Arrestor Sys |
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The loss of power tripped AH fans I causing RB temperature to be > 130*F for 15 minutes, reaching a maximum temperature t=.4 of 135'F.
These events were contrary tp T.S. 3.8.1.1 & 3.6.1.5 respectively.
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These occurrences are the 24th (3.8.1.1) and the 6th events reported under these t: is.I Specifications.
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An engineering investiga-tion of the Lightning Arrestor System failure will be concluded by 1/31/82. High 7 RB temperature was reduced to <130*F when AHF-1A & 1C were restarted.
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SUPPLEMENTARY INFORMATION
+
e Report No.:
50-302/81-033/03L-0 Fecility:
Crystal River Unit 3 Report Date:
July 14,1981 Occurrence Date:
June 16, 1981 Identification of Occurrence:
Loss of all AC power contrary to Technical Specification 3.8.1.1; and Reactor Building temperature greater than 130*F, contrary to Technical Specification 3.6.1.5.
Conditons Prior to Occurrence:
Mode 1 power operation.
Description of Occurrence:
On June 16, 1981 at 2340 during Mode 1, lightning struck the 230 KV feeder line. The Lightning Arrestor System failed to prevent loss of the CR-3 startup transformer, resulting in loss of all AC power. Due to loss of AC power, air handling fans tripped causing Reactor Building temperature to be greater than 130*F for fifteen minutes on June 17, 1981.
Maximum Reactor Building temperature reached was 135'F.
Upon loss of AC power, Emergency Diesel Generator "A" was started to load "A" 4160 Volt Engineered Safeguards Bus; and "B" 4160 Volt engineered safeguards Bus was repowered by switching power to CR-3 4160 Volt engineered safeguards Bus "B" from the fossil plant startup transformer. Air handling fans 1B and 1C were restarted, and Reactor Building temperature was less than 130*1 by 0025 on June.17, 1981. Power was restored into the plan't through the CR-3 startup transformer on June 17, 1981 at 0436.
Designation of Apparent Cause:
The cause of these events is attributed to failure of the Lightning Arres-tor System to prevent loss of the CR-3 startup transformer, resulting in loss of all AC power. Loss of AC power caused the air handling fans to trip, resulting in high Reactor Building temperature.
Analysis of Occurrence:
Redundancy was provided by one Emergency Diesel Generator and one inde-pendent offsite power supply.
There was no effect upon the health or saf 'y of the general public.
Corrective Action
Corrective actions during the unit blackout were in accordance with Procedure EP-101, " Unit Blackout". An engineering investigation of the Lightning Arrestor System failure will be concluded by 31 January 1982.
Once high Reactor Building temperature was determined, the air handling fans were restarted and temperature returned to less than 130*F. No further corrective action is deemed necessary.
Failure Data:
These are: the twenty-fourth event to be reported under Technical Specification 3.8.1.1; and the sixth event reported under Technical Specification 3.6.1.5.
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| 05000302/LER-1981-001-01, /01T-0:on 810107,during Performance of Quarterly Battery Check SP-511,determined That Battery Did Not Meet Tech Spec Requirements.Caused by Decrease in Specific Gravity of One Cell.Battery Placed on Equalize Charge | /01T-0:on 810107,during Performance of Quarterly Battery Check SP-511,determined That Battery Did Not Meet Tech Spec Requirements.Caused by Decrease in Specific Gravity of One Cell.Battery Placed on Equalize Charge | | | 05000302/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000302/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000302/LER-1981-002-03, /03L-0:on 810109,containment Isolation Valve CAV-1 Failed to Close After Sampling Pressurizer Steam Space. Caused by Failed Contacts in Torque Switch of Valve Operator.Switch Replaced & Operability Restored | /03L-0:on 810109,containment Isolation Valve CAV-1 Failed to Close After Sampling Pressurizer Steam Space. Caused by Failed Contacts in Torque Switch of Valve Operator.Switch Replaced & Operability Restored | | | 05000302/LER-1981-003, Forwards LER 81-003/01T-0 | Forwards LER 81-003/01T-0 | | | 05000302/LER-1981-003-01, /01T-0:on 810129,containment Isolation Valves AHV-1C & AHV-1D Found Inoperable Contrary to Tech Spec 3.6.3.1.Caused by Failure of Valve to Seal at Low Ambient Temp During Purge Conditions | /01T-0:on 810129,containment Isolation Valves AHV-1C & AHV-1D Found Inoperable Contrary to Tech Spec 3.6.3.1.Caused by Failure of Valve to Seal at Low Ambient Temp During Purge Conditions | | | 05000302/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000302/LER-1981-004-03, /03L-0:on 810119,position Indication for Containment Isolation Valves CAV-2 & CAV-126 Found Inoperable,In Violation of Tech Spec 3.6.3.1.Cause of CAV-2 Inoperability Unknown.Cause of CAV-126 Was Bad Breaker | /03L-0:on 810119,position Indication for Containment Isolation Valves CAV-2 & CAV-126 Found Inoperable,In Violation of Tech Spec 3.6.3.1.Cause of CAV-2 Inoperability Unknown.Cause of CAV-126 Was Bad Breaker | | | 05000302/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000302/LER-1981-005-03, /03L-0:on 801215,mechanical Seal for Bldg Spray Pump BSP-1A Found Leaking Greater than 6 Gallons/H,In Violation of Tech Spec 3.6.2.1.Caused by Defective Mechanical Seal.Review of Maint Procedure in Progress | /03L-0:on 801215,mechanical Seal for Bldg Spray Pump BSP-1A Found Leaking Greater than 6 Gallons/H,In Violation of Tech Spec 3.6.2.1.Caused by Defective Mechanical Seal.Review of Maint Procedure in Progress | | | 05000302/LER-1981-006-03, /03L-0:on 810123,breaker for Control Complex Emergency Ventilation Fan AHF-18A Found Open.Caused by Inadvertent Bumping of Breaker.Breaker Shut,Operability Checks Performed & Personnel Advised to Exercise Caution | /03L-0:on 810123,breaker for Control Complex Emergency Ventilation Fan AHF-18A Found Open.Caused by Inadvertent Bumping of Breaker.Breaker Shut,Operability Checks Performed & Personnel Advised to Exercise Caution | | | 05000302/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000302/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000302/LER-1981-007-03, /03L-0:on 810126,radiation Monitor RM-A5 Failed to Restart After Filter Change.Caused by Blown Fuse.Fuse Replaced | /03L-0:on 810126,radiation Monitor RM-A5 Failed to Restart After Filter Change.Caused by Blown Fuse.Fuse Replaced | | | 05000302/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000302/LER-1981-008-03, /03L-0:on 810204,during Charcoal Testing,Filter Sys AHFL-2D Methyl Iodide Removal Efficiency Was 92.14%. Caused by Atmospheric Pollutants & Normal Air Flow.Charcoal Cells Replaced W/New Impregnated Charcoal | /03L-0:on 810204,during Charcoal Testing,Filter Sys AHFL-2D Methyl Iodide Removal Efficiency Was 92.14%. Caused by Atmospheric Pollutants & Normal Air Flow.Charcoal Cells Replaced W/New Impregnated Charcoal | | | 05000302/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000302/LER-1981-009-03, /03L-0:on 810209,RCS Drain Tank Level Indication Was Erratic & Prevented Leak Rate Surveillance.Caused by Vapor Condensation in Instrument Sensing Lines.Lines Blown Down | /03L-0:on 810209,RCS Drain Tank Level Indication Was Erratic & Prevented Leak Rate Surveillance.Caused by Vapor Condensation in Instrument Sensing Lines.Lines Blown Down | | | 05000302/LER-1981-010-03, /03L-0:on 810217,after Routine Shutdown,Rcs Sampling Revealed That Dose Equivalent I-131 Exceeded Tech Specs.Caused by Leaking Fuel & Anticipated Dose Equivalent Iodine Transient.Purification Flow Increased | /03L-0:on 810217,after Routine Shutdown,Rcs Sampling Revealed That Dose Equivalent I-131 Exceeded Tech Specs.Caused by Leaking Fuel & Anticipated Dose Equivalent Iodine Transient.Purification Flow Increased | | | 05000302/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000302/LER-1981-011, Forwards LER 81-011/01T-1 | Forwards LER 81-011/01T-1 | | | 05000302/LER-1981-011-01, /01T-1:on 810306,containment Isolation Valves CAV-1,3,4,5 & 126 Found Incapable of Meeting Environ Qualification During Evaluation of IE Bulletin 79-01B.Caused by Potential Electrical Short Due to Flooding After LOCA | /01T-1:on 810306,containment Isolation Valves CAV-1,3,4,5 & 126 Found Incapable of Meeting Environ Qualification During Evaluation of IE Bulletin 79-01B.Caused by Potential Electrical Short Due to Flooding After LOCA | | | 05000302/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000302/LER-1981-012-03, /03L-0:on 810219,Limitorque-operated Containment Isolation Valves MUV-260 & 261 Failed to Close.Cause Unknown.Torque Switch MUV-261 Replaced & Operability Restored on 810224.Investigation Continuing | /03L-0:on 810219,Limitorque-operated Containment Isolation Valves MUV-260 & 261 Failed to Close.Cause Unknown.Torque Switch MUV-261 Replaced & Operability Restored on 810224.Investigation Continuing | | | 05000302/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000302/LER-1981-013-03, /03L-0:on 810302,during Routine Testing in Mode 5 Operation,Rcs Discovered W/Chloride Concentration of 0.18 Ppm.Caused by Release of Chlorides from Makeup. Procedures Will Be Revised by 810430 | /03L-0:on 810302,during Routine Testing in Mode 5 Operation,Rcs Discovered W/Chloride Concentration of 0.18 Ppm.Caused by Release of Chlorides from Makeup. Procedures Will Be Revised by 810430 | | | 05000302/LER-1981-014-03, /03L-0:on 810301,Clark Relay Model 5UK6-3 in Reactor Bldg Isolation Channel B,Group 2,failed to Actuate When Coil Was de-energized During SP-130.Caused by Burr on Relay Shaft.Relay Replaced | /03L-0:on 810301,Clark Relay Model 5UK6-3 in Reactor Bldg Isolation Channel B,Group 2,failed to Actuate When Coil Was de-energized During SP-130.Caused by Burr on Relay Shaft.Relay Replaced | | | 05000302/LER-1981-014, Forwards LER 81-014/03L-0 | Forwards LER 81-014/03L-0 | | | 05000302/LER-1981-015, Forwards LER 81-015/03L-0 | Forwards LER 81-015/03L-0 | | | 05000302/LER-1981-015-03, /03L-0:on 810301,Agastat Relay Model 3722B12C in Engineered Safeguards High Pressure Injection Actuation Channel B,Group 3 Block 4,failed to Change State After Receiving Signal During SP-130.Caused by Defective Relay | /03L-0:on 810301,Agastat Relay Model 3722B12C in Engineered Safeguards High Pressure Injection Actuation Channel B,Group 3 Block 4,failed to Change State After Receiving Signal During SP-130.Caused by Defective Relay | | | 05000302/LER-1981-016-03, /03L-0:on 810304,breaker for DHV-110,decay Heat Pump a Discharge Throttle Valve Tripped.Cause Unknown. DHV-110 Repetitively Cycled W/No Failures | /03L-0:on 810304,breaker for DHV-110,decay Heat Pump a Discharge Throttle Valve Tripped.Cause Unknown. DHV-110 Repetitively Cycled W/No Failures | | | 05000302/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000302/LER-1981-017, Forwards LER 81-017/03L-0.Detailed Event Analysis Encl | Forwards LER 81-017/03L-0.Detailed Event Analysis Encl | | | 05000302/LER-1981-017-03, /03L-0:on 810304,during Testing,Discovered That Containment Isolation Valve CFV-16 Would Not Move from mid-position.Caused by Valve Binding on Bushing Due to Insufficient Lubrication | /03L-0:on 810304,during Testing,Discovered That Containment Isolation Valve CFV-16 Would Not Move from mid-position.Caused by Valve Binding on Bushing Due to Insufficient Lubrication | | | 05000302/LER-1981-018, Forwards LER 81-018/03L-0 | Forwards LER 81-018/03L-0 | | | 05000302/LER-1981-018-03, /03L-0:on 810313,Gow Mac 20-250 Dihydrogen Analyzer Failed Calibr During Surveillance Program SP-708. Caused by Defective thermo-conductivity Cell.Cell Replaced & Instrument Calibr & Restored on 810316 | /03L-0:on 810313,Gow Mac 20-250 Dihydrogen Analyzer Failed Calibr During Surveillance Program SP-708. Caused by Defective thermo-conductivity Cell.Cell Replaced & Instrument Calibr & Restored on 810316 | | | 05000302/LER-1981-019-03, /03L-0:on 810313,during Normal operation,RC3,RC6 & RB3 Relays Tripped in Emergency Safeguards Actuation Channel B.Cause Attributed to Failed Hamlin Relay.Maint Revealed Addl Faulty Relays.Hamlin Replaced W/Cryden Relays | /03L-0:on 810313,during Normal operation,RC3,RC6 & RB3 Relays Tripped in Emergency Safeguards Actuation Channel B.Cause Attributed to Failed Hamlin Relay.Maint Revealed Addl Faulty Relays.Hamlin Replaced W/Cryden Relays | | | 05000302/LER-1981-019, Forwards LER 81-019/03L-0 | Forwards LER 81-019/03L-0 | | | 05000302/LER-1981-020-03, /03L-0:on 810405,during Performance of Engineered Safeguards Monthly Functional Tests,Discovered That Subsystem a Low Power Injection Channel RC-4 Would Not Reset W/Reset Permissive.Caused by Failed mercury-wetted Relay | /03L-0:on 810405,during Performance of Engineered Safeguards Monthly Functional Tests,Discovered That Subsystem a Low Power Injection Channel RC-4 Would Not Reset W/Reset Permissive.Caused by Failed mercury-wetted Relay | | | 05000302/LER-1981-020, Forwards LER 81-020/03L-0 | Forwards LER 81-020/03L-0 | | | 05000302/LER-1981-021, Forwards LER 81-021/03L-0 | Forwards LER 81-021/03L-0 | | | 05000302/LER-1981-021-03, /03L-0:on 810411,failure of Inverter D Resulted in Loss of Vital Bus VBDP-6.Caused by Shorted Diode & Blown Fuse Which May Have Resulted from Overheating in Inverter Cabinet.Diode & Fuse Replaced & Mod Procedure Revised | /03L-0:on 810411,failure of Inverter D Resulted in Loss of Vital Bus VBDP-6.Caused by Shorted Diode & Blown Fuse Which May Have Resulted from Overheating in Inverter Cabinet.Diode & Fuse Replaced & Mod Procedure Revised | | | 05000302/LER-1981-022-03, /03L-0:on 810412,following Reactor Trip,Main Steam Isolation Valve Msv Found Inoperable.Cause Undetermined.Mods Performed to Improve Valve Operation & Reliability. Functional Test Results Satisfactory.Operability Restored | /03L-0:on 810412,following Reactor Trip,Main Steam Isolation Valve Msv Found Inoperable.Cause Undetermined.Mods Performed to Improve Valve Operation & Reliability. Functional Test Results Satisfactory.Operability Restored | | | 05000302/LER-1981-022, Forwards LER 81-022/03L-0 | Forwards LER 81-022/03L-0 | | | 05000302/LER-1981-023, Forwards LER 81-023/03L-0 | Forwards LER 81-023/03L-0 | | | 05000302/LER-1981-023-03, /03L-0:on 810412,atmospheric Radiation Monitor RM-A5 Failed Due to Seized Sample Vacuum Pump.Caused by Worn Carbon Vanes.Pump Replaced.Engineering Evaluation in Progress.Supplementary Info Sheet Encl | /03L-0:on 810412,atmospheric Radiation Monitor RM-A5 Failed Due to Seized Sample Vacuum Pump.Caused by Worn Carbon Vanes.Pump Replaced.Engineering Evaluation in Progress.Supplementary Info Sheet Encl | | | 05000302/LER-1981-024-03, /03L-0:on 810414,emergency Diesel Generator 1A Found Inoperable During Monthly Test SP-354.Caused by Plugged Oil Separator in Air Ejector Train.Procedure Being Revised to Increase Cleaning & Insp Frequency | /03L-0:on 810414,emergency Diesel Generator 1A Found Inoperable During Monthly Test SP-354.Caused by Plugged Oil Separator in Air Ejector Train.Procedure Being Revised to Increase Cleaning & Insp Frequency | | | 05000302/LER-1981-024, Forwards LER 81-024/03L-0 | Forwards LER 81-024/03L-0 | | | 05000302/LER-1981-025-03, /03L-0:on 810417,EFP-2 Control Switch Discovered in Off Position.Caused by Procedural Deficiencies.Procedures Modified to Require Assurance That EFP-2 Is Selected to Auto | /03L-0:on 810417,EFP-2 Control Switch Discovered in Off Position.Caused by Procedural Deficiencies.Procedures Modified to Require Assurance That EFP-2 Is Selected to Auto | | | 05000302/LER-1981-025, Forwards LER 81-025/03L-0 | Forwards LER 81-025/03L-0 | |
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