LER-1981-031, /01T-0:on 810624,notification Was Received That Containment Isolation Valves Were Operating Less Conservatively than Vendor re-evaluation for safety-related Application.Caused by Inadequacy of Valve Operators |
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| 3021981031R01 - NRC Website |
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f o i sj l condition contrary to T.S. 3.6.3.1 and T.S. 3.6.1.1 Engineering resolution was to es t [ initiated and coerability was restored at 1340 on 7/1/8'l.
Ther'e was no effect upon I: I7i i the health or safety of the ceneral public.
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t l i t o 1 [ The cause of this event was notification from the valve vendor, Henry Pratt Co.,.
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SUPPLEMENTARY INFORMATION e
j
. Report No.:
50-302/81-031/0lT-0 Facility: Crystal River Unit #3 j
4 Report Date: July 8,1981 l
1 Occurrence Date: June 24, 1981 i
Identification of Occurrence:
i' Containment Isolation Valves AHV-1A, 1B, 1C and ID were operating in a condition less conservative that the vendor's reevaluation for safety-related application. This condition was contrary to Technical Specifications
'3.6.1.1 and 3.6.3.1.
Conditions Prior to Occurrence:
Mode 1 power operation (100%).
Description c! Occurrence:
At 1245 during normal operation, notification was received that the Engineer-ing evaluation of the adequacy oe containment isolation valves AHV-1A,1B,1C and LD performed by Henry Pratt Company as a result of a 1979 commitment to 0
l the NRC, revealed the previously established operating limit of 60 was not adequate.for a LOCA condition. The Reactor B'tilding purge that was in progress was terminated at 1335, and the valves were deactivated pending implementation
' of an Engineering resolution.
l Designation of Apparent Cause:
i The cause'of the event was notification from the Pratt Company.
m
. Analysis of Occurrence:
The revised limit for Pratt Valves with Limitorque operators was determined to be 35 ; for Pratt Valves with the Bettis Actuator, the acceptable angle is 50. There was no effect upon the health or safety of the general public.
Corrective Action
MAR 81-6-37 modified the valves to comply with the recommended operating limits.
No further corrective action'is deemed necessary at this time. Operability was restored at 1340 on July 1, 1981.
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- - Failure Data:
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This was the first occurrence of this type, and this is the thirty-sixth l
event reported under Technical Specification 3.6.3'1 and the third under Technical Specification 3.6.1.1.
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