05000369/LER-1981-098-03, /03L-0:on 810521,routine Surveillance Revealed That Periodic Channel Check of Condenser Discharge Header Isolation Valve Low Flow Interlock Was Omitted from Preventive Maint Computer Data Base.Cause Unknown

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/03L-0:on 810521,routine Surveillance Revealed That Periodic Channel Check of Condenser Discharge Header Isolation Valve Low Flow Interlock Was Omitted from Preventive Maint Computer Data Base.Cause Unknown
ML20009C653
Person / Time
Site: McGuire Duke Energy icon.png
Issue date: 07/10/1981
From: Nardoci P
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009C651 List:
References
LER-81-098-03L, LER-81-98-3L, NUDOCS 8107210319
Download: ML20009C653 (1)


LER-1981-098, /03L-0:on 810521,routine Surveillance Revealed That Periodic Channel Check of Condenser Discharge Header Isolation Valve Low Flow Interlock Was Omitted from Preventive Maint Computer Data Base.Cause Unknown
Event date:
Report date:
3691981098R03 - NRC Website

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[TTT1lOn June 11, 1981 T3TTl I ceriodic check of the condenser discharce header isolation valve's low flow 1

io4.i l interlock was omitt I from the preventive maintenance (PM) computer data base.l Io!sii The valve was reouired to be retested on May 21, 1981, and by missing the re-1 i s.. i ! test the plant entered a degragd, mode of operation per Tech. Spec. 4.3.3.8 (4p)

I o,71 I which is reportable per Tech. Spec. 6.9.1.13B, since the interlock was actually operable the entire time it was declared inoperable, the health and satety ot F3TTlIcho nuh14e unre nne iffoccod.

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i,eiiiomitted from the PM computer data base, the reason for which is unk. town.

After gI discovery of the omission, the isolation valve's low flow interlock was (immediately tested and found operable.

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