LER-1980-105, /03L-0:on 801226,w/Unit 2 at 99.5% Power Turbine First Stage Pressure Channel Failed.Caused by Frozen Transmitter.Ventilation & Heating Problems Corrected & Channel Returned to Svc |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 3391980105R03 - NRC Website |
|
text
z U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT CONTROL BLOCK / / / / / / / (1)
(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
/0/1/
/V/A/N/A/S/2/ (2)
/0/0/-/0/0/0/0/0/-/0/0/ (3)
/4/1/1/1/1/ (4)
/ / / (5)
LICENSEE CODE LICENSE NUMBER LICENSE TYPE CAT
]
/0/1/
/L/ (6)
/0/5/0/0/0/3/3/9/
(7)
/1/2/2/6/8/0/
(8) / Of 1/ ?/1/ 8/1/ (9)
DOCKET NUMBER EVENT DATE REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES (10)
/0/2/
/
On December 26, 1980, with Unit 2 at 99.5 percent power, a turbine first stage /
/0/3/
/
pressure channel failed. This channel is used to generate a high steam line
/
/0/4/
/
flow protection setpoint for 1 of 2 high steam line flow protection channels. /
/0/5/
/
This event is reportable pursuant to T.S. 6.9.1.9.b.
One high st.eam line flow /
/0/6/
/
protection channel remained operable. The public health and safety were not
/
/0/7/
/
affected.
/
/0/8/
/
/
SYSTEM
CAUSE
CAUSE COMP.
VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE
/0/9/
/I/B/ 0 1) /C/ (12) /_Z/ (13) /I/N/S/T/R/U/ (14) /T/ (15)
/Z/ (16)
SEQUENTIAL OCCURRENCE REPORT REVISION LER/R0 EVENT YEAR REPORT NO.
CODE TYPE NO.
(17) REPORT NUMBER
/8/0/
[-/ /1/0/5/
[1/
/0/3/
/L/
/-/
/0/
ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRD-4 PRIME COMP. COMPONENT TAKEN ACTION ON PLANT METHOD MOURS StsMITTED F0P11 SUB. SUPPLIER MANUFACTURER g/ (18) /G/ (19) /Z/ (20) [Z/ (21) /0/0/0/0/ (22) /Y/ (23) /N/ (24) /N/ (25) /F/1/8/0/ (26)
CAUSE DESCRIPTION AND CORRECTIVE ACTIONS (27)
/1/0/
/
Due to failures in the turbine building ventilation and heating systems, a
/
/1/1/
/
turbine first stage transmitter froze. Due to inadequate procedures, channels /
/1/2/
/
required bv T.S. to be placed in trip within one hour were not placed in the
/
/1/3/
/
trip condition for 63 minutes.
Procedures will be revised. Ventilation
/
/1/4/
/
problems were corrected and the channel returned to service.
_/
FACILITY METHOD OF STATUS
- /. POWER OTHER STATUS DISCOVERY DESCRIPTION (32)
/ ( 0) DISCOVERY
/1/5/
g/ (28)
/1/0/0/ (29)
/
NA LA/ (31)
/ ODERATOR OBSERVATION /
ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY (35)
LOCATION OF RELEASE (36)
/1/6/
/Z/ (33)
/Z/ (34)
/
NA
/
/
NA
/
PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION (39)
/1/7/ /0/0/0/ (37) LZ/ (38)
/
NA
/
PERSONNEL INJURIES NUMBER DESCRIPTION (41)
/1/8/ /0/0/0/ (40) /
NA
/
LOSS OF OR DAMAGE TO FACILITY (43)
TYPE
DESCRIPTION
/1/9/
LZ[ (42)
/
NA
/
PUBLICITY ISSUED DESCRIPTION (45)
NRC USE ONLY
/_2/0/
/N/ (44) /
I!A
/////////////
8107200457 elo15s ~ ~ -"*RER
%. R. CARTWRIGHT PHONE (703) 894-5151 PDR ADOCK 05000339
~
S PDR
P e
Virginia Electric and Power Company North Anna Power Station, Unit #2
Attachment:
Page 1 of 2 Docket No. 50-339 Report No. LER 80-105/03L-0
Description of Event
On December 26, 1980, with Unit 2 at 99.5 percent power, the sensing line of a turbine first stage pressure transmitter (PT-2446) froze causing the transmitter to fail high. Turbine first stage pressure is used to generate a high steam line flow protcetion setpoint. Due to the failure or the transmitter, one of two high steam line flow protection channels became inoperable. This event is reportable pursuant to T.S.
6.9.1.9.b.
Probable Consequences of Occurrence The redundancy for high steam line flow protection was reduced.
Since high steam line flow protection is designed to detect a steam line break accident and initiate appropriate corrective actions (SI, feeduster isolation, and trip of the main steam isolation valves), protection against a steam line break accident was reduced.
In addition to the operable high steam line flow channel the following signals were available for protection against a ; team line break accident.
1)
Pressurizer low pressure 2)
High differential pressure between steam lines 3)
Hi h containment pressure b
4)
Overpower reactor trips The refundancy provided by the P-7 interlock (blocks at power reactor trips during low power operation) was reduced. The redundancy of signals used for P-7 and the operability of all other signals used for P-7 except the one turbine impulse chamber pressure channel, made the effect of the failure on the P-7 signal negligible from a safety standpoint.
P-7 could have failed in the conservative direction only.
In addition to the protection functions described above the failed turbine first stage pressure transmitter provides control inputs for steam generator level, control rod, and condenser steam dump control.
Because the Unit was at 99.5% reactor power when the failure occurred and the transmitter failed high control functions were not affected.
Controls which could have been affected if power had been reduced were either placed under manual control or their first stage pressure input was switched to the operable turbine first stage pressure channel.
Coatrol functions were not affected.
The public health and safety were not sffected.
Cause of Event
The transmitter failed because its associated sensing line froze.
The t;ansmitter sensing line froze because a set of turbine building louvers were mechuaically bound in the open position allowing cold outside air emission to the lower level of the turbine building and two local area steam heaters were inoperable.
)
/'--
Attachment:
Page 2 of 2 Immediate Corrective Acti,on Automatic controls receiving input from the failed turbine first stage pressure transmitter were either placed under manual control or input was switched to the operable turbine first stage pressure transmitter.
Operations personnel immtdiately addressed a " Loss of Vital Instrumentation" procedure.
Unfertunately the procedure was inadequate and did not describe the actions to be taken when a turbine first stage pressure channel failed. Due to the inadequacy of the procedure, the high steam flow protection channel which receives an input frem the failed turbine first stage pressure channel was not tripped until 63 minutes after the event began. This is contrary to the action statement of the LCO (Actica Statement #14 T.S. 3.3.2.1) which requires trip of the inoperable channels within one hour.
The open turbine building louvers were covered, an asbestos blanket was wrapped around the instrument rack containing the failed transmitter and a heat lamp was placed in the instrument rack.
The transmitter sensing line was blown down and the turbine first stage pressure channel was declared operable after a channel functional test and channel check.
Scheduled Corrective Action The " Loss of Vital Instrumentation" procedure will be revised to include appropriate actions to be taken when a first stage pressure channel fails. This change should prevent recurrence of time delays in excess of those specified in the T.S. before appropriate actions are taken in response to a failed turbine first stage pressure channel.
Ares heaters in the turbine building will be repaired.
A formal winterization program will be developed to insure that freeze grotection equipment remains operable. The program will be implemented during the fall of 1981.
Actions Taken to Prevent Recurrence The initial actions and scheduled corrective action described above should prevent recurrence.
Generic Implications This event Lad no generic implications.
i 1
l
- - nn
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000338/LER-1980-001-01, /01T-0:on 800118,during Review for IE Bulletin 79-14,letdown Lines 3/4-CH-275-1502Q1 & 3/4-CH-123-1502-Q2 Reported Overstressed.Caused by Incorrect Valve Weights Used in Pipe Stress Calculations | /01T-0:on 800118,during Review for IE Bulletin 79-14,letdown Lines 3/4-CH-275-1502Q1 & 3/4-CH-123-1502-Q2 Reported Overstressed.Caused by Incorrect Valve Weights Used in Pipe Stress Calculations | | | 05000338/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000339/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000339/LER-1980-001-03, /03L-0:on 800423,w/unit in Mode 6 Following Fuel Loading,Rhr Sys Inlet Valve MOV-2700 Ran Closed,Causing Loss of Operable RHR Loop.Caused by Blown Signal Comparator Card Power Supply Fuse in Process Control Sys.Card Replaced | /03L-0:on 800423,w/unit in Mode 6 Following Fuel Loading,Rhr Sys Inlet Valve MOV-2700 Ran Closed,Causing Loss of Operable RHR Loop.Caused by Blown Signal Comparator Card Power Supply Fuse in Process Control Sys.Card Replaced | | | 05000338/LER-1980-002, Forwards LER 80-002/01T-0 | Forwards LER 80-002/01T-0 | | | 05000338/LER-1980-002-01, /01T-0:on 800107,S&W Informed Util That Stress on Vertical Supports RH-R-19 & WS-R-316 & Snubbers SI-HSS-101B,101C & 107A Exceeded Allowable Design Values. Caused by Wrong Valve Weights Used in Design Calculations | /01T-0:on 800107,S&W Informed Util That Stress on Vertical Supports RH-R-19 & WS-R-316 & Snubbers SI-HSS-101B,101C & 107A Exceeded Allowable Design Values. Caused by Wrong Valve Weights Used in Design Calculations | | | 05000339/LER-1980-002-01, /01T-0:on 800429,during Structural Review for IE Bulletin 79-14,S&W Discovered Overstressed Pipe Hangers in Svc Bldg.Caused by Error in Stress Analysis Used to Design Pipe Hanger Supports.Mods Will Be Implemented | /01T-0:on 800429,during Structural Review for IE Bulletin 79-14,S&W Discovered Overstressed Pipe Hangers in Svc Bldg.Caused by Error in Stress Analysis Used to Design Pipe Hanger Supports.Mods Will Be Implemented | | | 05000339/LER-1980-002, Forwards LER 80-002/01T-0 | Forwards LER 80-002/01T-0 | | | 05000339/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000339/LER-1980-003-03, /03L-0:on 800528,2H Diesel Generator Frequency & Voltage Response Was Not Verified Every 8-h,contrary to Tech Spec.Caused by Faulty Lead on Monitoring Instrumentation. Offsite Power Sources Verified & Found Acceptable | /03L-0:on 800528,2H Diesel Generator Frequency & Voltage Response Was Not Verified Every 8-h,contrary to Tech Spec.Caused by Faulty Lead on Monitoring Instrumentation. Offsite Power Sources Verified & Found Acceptable | | | 05000338/LER-1980-003-03, /03L-0:on 800121,nuclear Instrumentation Sys Power Range Channel 4 Declared Inoperable Due to Erratic Power Bistable Operation.Caused by Failed Ion Chamber Detector.Ion Chamber Detector Replaced | /03L-0:on 800121,nuclear Instrumentation Sys Power Range Channel 4 Declared Inoperable Due to Erratic Power Bistable Operation.Caused by Failed Ion Chamber Detector.Ion Chamber Detector Replaced | | | 05000338/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000339/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000339/LER-1980-004-03, /03L-0:on 800519,during Mode 3 Operation,Steam Generator Level Channel LT-2475 Indicated Level 9% Lower than Two Redundant Channels.Caused by Voltage Drift.Channel Was Placed in Trip Mode | /03L-0:on 800519,during Mode 3 Operation,Steam Generator Level Channel LT-2475 Indicated Level 9% Lower than Two Redundant Channels.Caused by Voltage Drift.Channel Was Placed in Trip Mode | | | 05000338/LER-1980-004-03, /03L-0:on 800109,during Test of Equipment Hatch Emergency Escape Lock,Inner Door Seal Found Leaking When Door Opened & Lock Found to Be Under Slight Vacuum.Caused by Frequent Door Operation.Seals Replaced | /03L-0:on 800109,during Test of Equipment Hatch Emergency Escape Lock,Inner Door Seal Found Leaking When Door Opened & Lock Found to Be Under Slight Vacuum.Caused by Frequent Door Operation.Seals Replaced | | | 05000338/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000338/LER-1980-005-03, /03L-0:on 800110,w/unit in Mode 4,main Steam Isolation Trip Valve TV-MS101C Would Not Close Using Train a Push Button.Caused by Open Auxiliary Relay in Circuit. Relay Replaced from Stock & Tested Satisfactorily | /03L-0:on 800110,w/unit in Mode 4,main Steam Isolation Trip Valve TV-MS101C Would Not Close Using Train a Push Button.Caused by Open Auxiliary Relay in Circuit. Relay Replaced from Stock & Tested Satisfactorily | | | 05000338/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000339/LER-1980-005-03, /03L-0:on 800517,2J Emergency Diesel Generator Tripped After Starting & Operability of 2H Diesel Generator Was Not Verified within 1-h.Caused by Existing Procedures Not Specifying Test Connections Required to Test Diesel | /03L-0:on 800517,2J Emergency Diesel Generator Tripped After Starting & Operability of 2H Diesel Generator Was Not Verified within 1-h.Caused by Existing Procedures Not Specifying Test Connections Required to Test Diesel | | | 05000339/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000339/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000339/LER-1980-006-03, /03L-0:on 800520,during Startup Testing in Mode 3, B Steam Generator Narrow Range Level Channel III Was Observed Reading Below Redundant Level Channels & Drifting Low.Caused by Air Pocket in Steam Generator Sensing Line | /03L-0:on 800520,during Startup Testing in Mode 3, B Steam Generator Narrow Range Level Channel III Was Observed Reading Below Redundant Level Channels & Drifting Low.Caused by Air Pocket in Steam Generator Sensing Line | | | 05000338/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000338/LER-1980-006-03, /03L-01:on 800111,w/unit in Mode 3,casing Coolant Pump Discharge Valve MOV-RS-100A Was Discovered to Be Inoperable.Caused by Removal of Casing Cooling Tank Level Transmitter LT-RS103A During Execution of Design Change | /03L-01:on 800111,w/unit in Mode 3,casing Coolant Pump Discharge Valve MOV-RS-100A Was Discovered to Be Inoperable.Caused by Removal of Casing Cooling Tank Level Transmitter LT-RS103A During Execution of Design Change | | | 05000338/LER-1980-007-03, /03L-0:on 800111,during Mode 3 Reactor Heating Containment Average Temp Decreased to 85 F,Less than Tech Specs.Caused by Insufficient Procedural Precautions. Removed Chiller from Svc.Monitored Temp | /03L-0:on 800111,during Mode 3 Reactor Heating Containment Average Temp Decreased to 85 F,Less than Tech Specs.Caused by Insufficient Procedural Precautions. Removed Chiller from Svc.Monitored Temp | | | 05000339/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000339/LER-1980-007-03, /03L-0:on 800521,during Mode 3 Operation,Channel in Tave Protection Loop 2 Failed in High Direction.Cause Is Unknown.Failed Channel Was Removed from Svc & Replaced by Spare | /03L-0:on 800521,during Mode 3 Operation,Channel in Tave Protection Loop 2 Failed in High Direction.Cause Is Unknown.Failed Channel Was Removed from Svc & Replaced by Spare | | | 05000339/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000338/LER-1980-008-01, /01T-0:on 800111,during Review for IE Circular 78-08,S&W Found Control Room Air Conditioning Chiller Units Control Panel Not Qualified to Seismic Category I Requirements.Cause Unknown.Vendor Reviewing Components | /01T-0:on 800111,during Review for IE Circular 78-08,S&W Found Control Room Air Conditioning Chiller Units Control Panel Not Qualified to Seismic Category I Requirements.Cause Unknown.Vendor Reviewing Components | | | 05000339/LER-1980-008-03, /03L-0:on 800521,during Mode 3 Operation,Redundant Channel Protection Was Lost.Caused by Personnel Not Placing Tave Protection Loop Failed Channel in Trip Mode within Required Time.Failed Channel Placed in Trip Mode | /03L-0:on 800521,during Mode 3 Operation,Redundant Channel Protection Was Lost.Caused by Personnel Not Placing Tave Protection Loop Failed Channel in Trip Mode within Required Time.Failed Channel Placed in Trip Mode | | | 05000338/LER-1980-009-03, /03L-0:on 800111,while Performing Periodic Test on Main Steam Safety Valves,Found Valves SV-MS-101-A & C, SV-MS-102-A & B & SV-MS-105-A & C Did Not Lift at Pressure Setpoints Per Tech Specs.Caused by Setpoint Drift | /03L-0:on 800111,while Performing Periodic Test on Main Steam Safety Valves,Found Valves SV-MS-101-A & C, SV-MS-102-A & B & SV-MS-105-A & C Did Not Lift at Pressure Setpoints Per Tech Specs.Caused by Setpoint Drift | | | 05000339/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000339/LER-1980-009-03, /03L-0:on 800522,power Supply for Main Steam Pressure Protection Channel III Failed High,Causing Steam Line Pressure Mismatch.Caused by Failed Card in Power Supply.Card Was Replaced & Calibr | /03L-0:on 800522,power Supply for Main Steam Pressure Protection Channel III Failed High,Causing Steam Line Pressure Mismatch.Caused by Failed Card in Power Supply.Card Was Replaced & Calibr | | | 05000338/LER-1980-010-01, /01T-0:on 800111,during Review for IE Bulletin 79-14,S&W Found Stress on Vertical Rod Hangers SW-H-162A & SW-H-160A to Be Over Design Allowable.Caused by Incorrect Valve Weights Used in Pipe Support Design Calculations | /01T-0:on 800111,during Review for IE Bulletin 79-14,S&W Found Stress on Vertical Rod Hangers SW-H-162A & SW-H-160A to Be Over Design Allowable.Caused by Incorrect Valve Weights Used in Pipe Support Design Calculations | | | 05000339/LER-1980-010, Forwards LER 80-010/01T-0 | Forwards LER 80-010/01T-0 | | | 05000339/LER-1980-010-01, /01T-0:on 800523,during Review of ECCS Piping for Fluid Temp Below 70 F,Determined That Loadings on Both Low Head Safety Injection Pump Nozzles Exceeded Design Stress Allowables.Caused by Deficiency in Sys Stress Analysis | /01T-0:on 800523,during Review of ECCS Piping for Fluid Temp Below 70 F,Determined That Loadings on Both Low Head Safety Injection Pump Nozzles Exceeded Design Stress Allowables.Caused by Deficiency in Sys Stress Analysis | | | 05000339/LER-1980-011-03, /03L-0:on 800520,personnel Air Lock Doors Would Not Seal Completely,Causing Air Leakage While Performing Surveillance Test 2-PT-62.4.Caused by Leakage Past Seals on Inner & Outer Doors.New Seals Were Installed | /03L-0:on 800520,personnel Air Lock Doors Would Not Seal Completely,Causing Air Leakage While Performing Surveillance Test 2-PT-62.4.Caused by Leakage Past Seals on Inner & Outer Doors.New Seals Were Installed | | | 05000339/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000338/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000338/LER-1980-011-03, /03L-0:on 800115,when Sys Sample Monitoring Pumps Were Removed from Svc,Ventilation Vent Stack B Particulate & Gas Radiation Monitors RM-VG112 & 113 Were Rendered Inoperable.Design Changes Will Add High Range Monitor | /03L-0:on 800115,when Sys Sample Monitoring Pumps Were Removed from Svc,Ventilation Vent Stack B Particulate & Gas Radiation Monitors RM-VG112 & 113 Were Rendered Inoperable.Design Changes Will Add High Range Monitor | | | 05000339/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000339/LER-1980-012-03, /03L-0:on 800618 While in Mode 2,control Rod Demand Position Indication Noted 19 Steps Higher than Associated Rod Position Indication.Caused by Drift of Rod Position Indicator Channel.Channel Recalibr | /03L-0:on 800618 While in Mode 2,control Rod Demand Position Indication Noted 19 Steps Higher than Associated Rod Position Indication.Caused by Drift of Rod Position Indicator Channel.Channel Recalibr | | | 05000338/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000338/LER-1980-012-03, /03L-0:on 800111,during Testing in Mode 3 to Verify Main Steam Trip Valve Closure Time,Trip Valve Failed to Close Fully within Required Five Seconds.Cause Unknown. Valve Was Retested.Closure Time within Acceptable Limits | /03L-0:on 800111,during Testing in Mode 3 to Verify Main Steam Trip Valve Closure Time,Trip Valve Failed to Close Fully within Required Five Seconds.Cause Unknown. Valve Was Retested.Closure Time within Acceptable Limits | | | 05000338/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000338/LER-1980-013-03, /03L-0:on 800114,while Using Steam Driven Feedwater Pump 1-FW-P-2 to Add Feedwater to Steam Generator A,Water Leaked from Pump Oil Cooler Gasket.Caused by Blown Gasket.Gasket Replaced | /03L-0:on 800114,while Using Steam Driven Feedwater Pump 1-FW-P-2 to Add Feedwater to Steam Generator A,Water Leaked from Pump Oil Cooler Gasket.Caused by Blown Gasket.Gasket Replaced | | | 05000339/LER-1980-013-03, /03L-0:on 800520 & 27,w/unit in Hot Standby, Samples of Boron Injection Tank & C Boric Acid Storage Found to Contain Less than 20,000 Ppm Boron.Caused by Leaks Past Inlet Valves MOV-2867 a & B.Switch Settings Increased | /03L-0:on 800520 & 27,w/unit in Hot Standby, Samples of Boron Injection Tank & C Boric Acid Storage Found to Contain Less than 20,000 Ppm Boron.Caused by Leaks Past Inlet Valves MOV-2867 a & B.Switch Settings Increased | | | 05000339/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000338/LER-1980-014, Forwards LER 80-014/03L-0 | Forwards LER 80-014/03L-0 | | | 05000338/LER-1980-014-03, /03L-0:on 800113,during Insp of Auxiliary Feedwater Pump 1-FW-P-2 Outboard Bearing,Discovered Inboard Side of Thrust Bearing Had Been Wiped.Caused by Lack of Oil. Bearing Replaced & Pump Returned to Svc | /03L-0:on 800113,during Insp of Auxiliary Feedwater Pump 1-FW-P-2 Outboard Bearing,Discovered Inboard Side of Thrust Bearing Had Been Wiped.Caused by Lack of Oil. Bearing Replaced & Pump Returned to Svc | |
|