05000369/LER-1981-087-03, /03L-0:on 810518,during Initial Fuel Loading,Flow Indicator of Gross Radioactivity Monitor (EMF-31) on Waste Water Treatment Line Was Found Not Functioning.Caused by Clogged Flow Switch & Strainer.Monitor Cleaned

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/03L-0:on 810518,during Initial Fuel Loading,Flow Indicator of Gross Radioactivity Monitor (EMF-31) on Waste Water Treatment Line Was Found Not Functioning.Caused by Clogged Flow Switch & Strainer.Monitor Cleaned
ML20009C078
Person / Time
Site: McGuire Duke Energy icon.png
Issue date: 06/17/1981
From: Ouellette R
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009C075 List:
References
LER-81-087-03L, LER-81-87-3L, NUDOCS 8107200245
Download: ML20009C078 (1)


LER-1981-087, /03L-0:on 810518,during Initial Fuel Loading,Flow Indicator of Gross Radioactivity Monitor (EMF-31) on Waste Water Treatment Line Was Found Not Functioning.Caused by Clogged Flow Switch & Strainer.Monitor Cleaned
Event date:
Report date:
3691981087R03 - NRC Website

text

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73 agecnToArg so EVENT CESCAIPTICN AND PRC8 AOLE CONSECUENCES h tot 2lIWhile in Mode 5. initial fuel loadin-an encipeer noticed that the flow I

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