LER-1981-004, /01T-0:on 810529,during Maint Shutdown,Msiv 2CV-2017 Failed to Shut.Caused by Two Vent Valves for Air Operator Failing to Open.Valves Replaced |
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NRC F ORJJ 366 '
U. S. NOC1.E AR RE!OL ATCGY COMMISSION (77/l LICENSEE EVENT REPORT CONTROL BLOCX: l l
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EVENT DATE 74
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REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10 l 2 l l At 0256 on May 29, 1981, during a routine shutdown for secondary plant l l maintenance, MSIV 2CV-2017 failed to shut as required.
Imme diate j
0 3 I investigation revealed the two vent valves for the air operator failed l O 4 l O l s i l to open, preventing the closure of 2CV-2017.
Vent valve 2SV-2017C was l
l manually tripped open and the MSIV shut irunediately.
This event is j
O s l reportable under Technical Specifi cation 15.6.9. 2. A.5.
This event is l
O 7 l 0 ;e j l similar to LER 77-02 Docket No. 50-301.
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CODE TYPE NO.
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40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h ITTo"l l Af ter the f ail ure of the vent valves. nnmorous a tte mo ts failed to 1
o i i i duplicate the failure mode.
Prior to returning to power, the MSIV I
l 2CV-2017 was again tested satisfactorily; howe ve r, due to the sluggish l
, 2 l operation of the vent valve, both vent valves were replaced on 6-1-81.
l i 3 l The testing frequenct has been incroased to detect future problems.
J i 4 8 9 80 ST S
% POWER OTHER ST ATUS 015 RY DISCOVERY DESCRIPTION [DJ@ l 0l 0l 0l@l N/A l
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Fay PHONE:
NAME OF PREPARER
1 ATTACHMENT TO LICENSEE EVENT REPORT NO. 81-004/0lT-0 Wisconsin Electric Power Conpany Point Beach Nuclear Plant Unit 2 Docket No. 50-301 At 0256 hours0.00296 days <br />0.0711 hours <br />4.232804e-4 weeks <br />9.7408e-5 months <br /> on May 29, 1981, with the unit in the off-line, zero power, critical condition in preparation for operator licensing startups and secondary plant maintenance,
the operator attempted to shut both main steam isolation valves with a remote manual signal in preparation to take steam out.
Main steam isolation valve 2CV-2018 shut as called for; main steam isolation valve 2CV-2017 failad to shut.
This is a reportable occurrence in accordance with Technical Specification 15.6.9.2. A.5 with 24-hour written notification provided to U. S.
NRC Region III on May 29, 1981.
An immediate investigation ensued and found the two air-operated vent solenoid-operated valves, 2SV-2017C&D, were shut preventing closure of 2CV-20l*/.
The two air-operator supply solenoid valves, 2SV-2017A&B, were shut as required.
Vent valve 2SV-2017C was locally manually tripped at the valve operator station and the main steam isolation valve, 2CV-2Ll7, shut immediatel".
The air operator of the main steam isolation valve has a two-train logic.
There are two in-series air supply solenoids.
The vent path has two parallel solenoid valves.
The supply line is orificed so that on failure of both supply solenoids to close, a ven' will still cause closure of the c
main steam isolation valve.
Two manual key-operated isolation valves are provided on the vent lines upstream of the air vent solenoid-operated valves to allow for testing.
Due to l
reliability problems experienced in the past with the original l
installed Lawrence Series 1200 internal pilot-operated sole-noid valve, they were replaced on one main steam isolation valve operator assembly with ASCO Bulletin 8015 internal pilot-cperated solenoid valves.
Prior to the initial installation of the new ASCO valves, a testing program was undertaken which included vibration, leakage, voltage and operational testing.
At the conclusion of these tests the ASCO valve was dis-assambled and inspected.
At the conclusion of this program the ASCO valves were approved for installation.
The new ASCO valves were installed during the recent refueling outage and were extensively tested in place l
prior to the successful completion on May 22, 19 81, o f the tined test required by Technical Specification 15.4.7.
After the failure of these valves to operate on 1:ay 29, 1981,
attempts were made to duplicate this failure mode but all the valves operated properly.
Upon the completion of the other secondary plant maintenance and training startupg the i
main stcam isolation valve 2CV-2017 was tested at 2000 hcurs on May 31, 1981.
Although 2CV-2017D
(" green" train vent valve) operated sluggishly, the main steam isolation valve cycled properly on each of six attempts.
Due to this sluggish operation, both vent valves, 2CV-2017C&D, were replaced on June 1,1981, and proper operation was again verified.
The removed valves are undergoing a testing and evaluation program to attempt to de termine the cause of their f ailure.
In addition, the testing frequency has been increased on the 2CV-2017 operator to foretell future problems.
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| 05000301/LER-1981-001-03, /03L-0:on 810324,steam Generator Loop a Pressure Safeguards Actuation Setpoint Found Below Tech Spec.Caused by Setpoint Drift in Foxboro Model 63U-BC-OHCA-F Bistable. Bistable Replaced | /03L-0:on 810324,steam Generator Loop a Pressure Safeguards Actuation Setpoint Found Below Tech Spec.Caused by Setpoint Drift in Foxboro Model 63U-BC-OHCA-F Bistable. 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2CV-2017 Failed to Shut.Caused by Two Vent Valves for Air Operator Failing to Open.Valves Replaced | | | 05000266/LER-1981-005-03, /03L-0:on 810515,control Room Emergency Filtration Sys Fans,Common to Both Units,Found Operating Outside Design Flow Rates Per Tech Specs.Caused by Improperly Balanced Backdraft Damper at Fan Discharge.Dampers Readjusted | /03L-0:on 810515,control Room Emergency Filtration Sys Fans,Common to Both Units,Found Operating Outside Design Flow Rates Per Tech Specs.Caused by Improperly Balanced Backdraft Damper at Fan Discharge.Dampers Readjusted | | | 05000266/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000301/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000301/LER-1981-005-03, /03L-0:on 810625,during Normal Operation, Contractor Accidently Tripped Turbine Overspeed Trip Valve on Auxiliary Feedwater Pump.Valve Reset.Contractors Removed from Area & Reminded to Use Caution | /03L-0:on 810625,during 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Probably Caused by Dirty Contacts.New Rees Contact Block Installed | | | 05000266/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000266/LER-1981-012, Forwards LER 81-012/01T-0 | Forwards LER 81-012/01T-0 | | | 05000266/LER-1981-012-01, /01T-0:on 810828,control Room Critical Control Power Failure Alarm Annunciated.Caused by Breakers Accidentally Opened by Contractor Personnel Installing Fire Barriers in Control Room.Breakers Closed & Alarm Cleared | /01T-0:on 810828,control Room Critical Control Power Failure Alarm Annunciated.Caused by Breakers Accidentally Opened by Contractor Personnel Installing Fire Barriers in Control Room.Breakers Closed & Alarm Cleared | | | 05000266/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000266/LER-1981-013-03, /03L-0:on 810921,records Revealed That Safeguards Bus Undervoltage Relays Were Not Tested within Required Time Frame.Caused by Earlier than Normal Testing During Annual Diesel Overhaul.Surveillance Callup Modified | /03L-0:on 810921,records Revealed That Safeguards Bus Undervoltage Relays Were Not Tested within Required Time Frame.Caused by Earlier than Normal Testing During Annual Diesel Overhaul.Surveillance Callup Modified | | | 05000266/LER-1981-014, Forwards LER 81-014/01T-1 | Forwards LER 81-014/01T-1 | | | 05000266/LER-1981-014-01, /01T-1:on 811010,while Performing Refueling Leakage Tests of Containment Isolation valves,4-inch Check Valve in Svc Air Supply Found to Have Leakage Exceeding Tech Specs.Caused by Foreign Matl in Internals | /01T-1:on 811010,while Performing Refueling Leakage Tests of Containment Isolation valves,4-inch Check Valve in Svc Air Supply Found to Have Leakage Exceeding Tech Specs.Caused by Foreign Matl in Internals | | | 05000266/LER-1981-015-01, /01T-0:on 811010,during Refueling Outage,High & Low Head Safety Injection Check Valve Leakage Test Indicated Excessive Leakage.Cause Not Stated.Affected Line Flushed & Passed Retest | /01T-0:on 811010,during Refueling Outage,High & Low Head Safety Injection Check Valve Leakage Test Indicated Excessive Leakage.Cause Not Stated.Affected Line Flushed & Passed Retest | | | 05000266/LER-1981-015, Updated LER 81-015/01T-1:on 811010,high & Low Head Safety Injection Check Valve Leakage Test Indicated Leakage in Excess of Acceptable Criteria for 1-853C.Cause Not Stated. 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Affected Line Flushed & 1-853C Retested | | | 05000266/LER-1981-016, Forwards LER 81-016/01T-0 | Forwards LER 81-016/01T-0 | | | 05000266/LER-1981-016-01, /01T-0:on 811016,vendor Notified of Unusually High Failure Rate of Westinghouse Nbfd Relays Upon de-energization.Caused by Voltage Spike.Gradual Replacement of Designed Relays or Coils Planned | /01T-0:on 811016,vendor Notified of Unusually High Failure Rate of Westinghouse Nbfd Relays Upon de-energization.Caused by Voltage Spike.Gradual Replacement of Designed Relays or Coils Planned | | | 05000266/LER-1981-017, Forwards LER 81-017/01T-0 | Forwards LER 81-017/01T-0 | | | 05000266/LER-1981-017-01, /01T-0:on 811030,during refueling,10 Tubes in a Steam Generator & 7 Tubes in B Steam Generator Found to Exceed Tech Specs.Caused by Caustic.Crevice Flush Planned Before Startup & Defective Tubes Sleeved | /01T-0:on 811030,during refueling,10 Tubes in a Steam Generator & 7 Tubes in B Steam Generator Found to Exceed Tech Specs.Caused by Caustic.Crevice Flush Planned Before Startup & Defective Tubes Sleeved | |
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