05000267/LER-1981-020-03, /03L-0:on 810226,primary Coolant Moisture & Oxidants Exceeded Limits.Caused by Circulator Buffer Sys Upset & Helium Circulator Trip Due to 810223 Reactor Scram. Reactor Power Reduced Until Moisture Level Decreased

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/03L-0:on 810226,primary Coolant Moisture & Oxidants Exceeded Limits.Caused by Circulator Buffer Sys Upset & Helium Circulator Trip Due to 810223 Reactor Scram. Reactor Power Reduced Until Moisture Level Decreased
ML20008F687
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 03/27/1981
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20008F680 List:
References
LER-81-020-03L, LER-81-20-3L, NUDOCS 8104210498
Download: ML20008F687 (1)


LER-1981-020, /03L-0:on 810226,primary Coolant Moisture & Oxidants Exceeded Limits.Caused by Circulator Buffer Sys Upset & Helium Circulator Trip Due to 810223 Reactor Scram. Reactor Power Reduced Until Moisture Level Decreased
Event date:
Report date:
2671981020R03 - NRC Website

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