05000267/LER-1981-021-03, /03L-0:on 810302,liquid Nitrogen Storage Tank Level Lower than Tech Spec Requires.Caused by Sys Usage & Unavailable Recondensers.Level Restored W/Two Loads

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/03L-0:on 810302,liquid Nitrogen Storage Tank Level Lower than Tech Spec Requires.Caused by Sys Usage & Unavailable Recondensers.Level Restored W/Two Loads
ML20008F660
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 04/01/1981
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20008F657 List:
References
LER-81-021-03L, LER-81-21-3L, NUDOCS 8104210476
Download: ML20008F660 (3)


LER-1981-021, /03L-0:on 810302,liquid Nitrogen Storage Tank Level Lower than Tech Spec Requires.Caused by Sys Usage & Unavailable Recondensers.Level Restored W/Two Loads
Event date:
Report date:
2671981021R03 - NRC Website

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