LER-1981-066, /03L-0:on 811010,various Reactor Protection Instruments Found Out of Tolerance.Caused by Bellows Failure,Instrument Drift & Loose Test Point Output Terminal. Bellows Replaced,Terminal Tightened & Instruments Recalibr |
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,cSCRIPTION AND PROBABLE CONSEQUENCES h l o 121 l During performance of shutdown surveillance activities various reactor rirnrocrinn 1
instruments were found out-of-tolerance. These events were not attributed to a srecific I 3 g 10141 l shutdown activity,as required by Reg. Guide 1.16 and, therefore, are reportable as I
,being contrary to T.S. 3.3.1.1.
There was no effect upon the health or safety of the l
general public. Nine instruments (RC-14A-DPT4 on 10/10/81; RC-14A-DPTl on 10/11/81; I
y RC-14B-DPT4 and RC-14B-DPT1 on 10/13/81; RC-14B-DPT2 on 10/17/81; RC-14B-DPT3 on 10/20/81l RC-3B-PT1 and RC-3B-PT2 on 10/26/81 RC-3A-PTl on 10/27/81) were out-of-tolerance. This 10181 l s the ninth event reported under tfiis Specification.
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- - 14A-DPT4 had a bellows failure. The bellows was rep 1' aced.
RC-14A-DPT1, RC-14B-DPT4. I RC
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RC-14B-DPT1, and RC-14B-DPT2, RC-3B-PT1 and RC-3B-PT2, also RC-3A-PT1 failed due to l
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was tightened. All instruments were satisfactorily recalibrated. No further corrective l action is deemed necessary.
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SUPPLEMENTARY INFORMATION Report No.:
50-302/81-066/03L-0 Facility:
Crystal River Unit 3 Report Date:
November 6,1981 Occurrence Date:
October 10, 1981 Identification of Occurrence:
Various reactor protection instruments were found o it-of-toler-ance during shutdown surveillance activities. These events were not atttibuted to specific shutdown activities as required by Regulatory Guide 1.16, and, therefore, are being reported as contrary to Technical Specification 3.3.1.1.
Conditions Prior to Occurrence:
Mode 6 refueling (0%).
Description of Occurrence:
On October 10, 1981, during performance of SP-112, Calibration of the Reactor Protection System, RC-14A-DPT4 was found out-of-tolerance. On October 11, 1981, during performance of SP-112, RC-14A-DPT1 was found out-of-tolerance. On October 13, 1981, during performance of SP-112, RC-14B-DPT4 and RC-14B-DPTI were found out-of-tolerance. On October 17, 1981, during performance of SP-112, RC-14B-DPT2 was found out-of-tolerance. On October 20, 1981, during performance of SP-112, RC-14B-DPT3 was found out-of-tolerance. On October 26, 1981, during performance of SP-112, RC-3B-PTl and RC-3B-PT2 were found out-of-tolerance.
On October 27, 198], during performance of SP-ll2, RC-3A-PTl was found out-of-tolerance.
Designation of Apparent Cause:
RC-14A-DPT4 had a bellows failure. The bellows was replaced.
RC-14A-DPT1, RC-14B-DPT4, RC-14B-DPT1,and RC-14B-DPT2, RC-3B-PT1,and RC-3B-PT2,and RC-3A-PT1,all failed due to in-strument drift.
RC-14B-DPT3 had a loose test point output terminal. The terminal was tightened.
Aaalysis of Occurrence:
There was no effect upon the health or safety of the general public.
Corrective Action
All instruments were satisfactorily recalibrated. No further corrective action is deemed necessary.
Failure Data:
Nine instruments were found out-of-tolerance. This is the ninth event reported under this Spe,cification.
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| 05000302/LER-1981-001-01, /01T-0:on 810107,during Performance of Quarterly Battery Check SP-511,determined That Battery Did Not Meet Tech Spec Requirements.Caused by Decrease in Specific Gravity of One Cell.Battery Placed on Equalize Charge | /01T-0:on 810107,during Performance of Quarterly Battery Check SP-511,determined That Battery Did Not Meet Tech Spec Requirements.Caused by Decrease in Specific Gravity of One Cell.Battery Placed on Equalize Charge | | | 05000302/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000302/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000302/LER-1981-002-03, /03L-0:on 810109,containment Isolation Valve CAV-1 Failed to Close After Sampling Pressurizer Steam Space. Caused by Failed Contacts in Torque Switch of Valve Operator.Switch Replaced & Operability Restored | /03L-0:on 810109,containment Isolation Valve CAV-1 Failed to Close After Sampling Pressurizer Steam Space. Caused by Failed Contacts in Torque Switch of Valve Operator.Switch Replaced & Operability Restored | | | 05000302/LER-1981-003, Forwards LER 81-003/01T-0 | Forwards LER 81-003/01T-0 | | | 05000302/LER-1981-003-01, /01T-0:on 810129,containment Isolation Valves AHV-1C & AHV-1D Found Inoperable Contrary to Tech Spec 3.6.3.1.Caused by Failure of Valve to Seal at Low Ambient Temp During Purge Conditions | /01T-0:on 810129,containment Isolation Valves AHV-1C & AHV-1D Found Inoperable Contrary to Tech Spec 3.6.3.1.Caused by Failure of Valve to Seal at Low Ambient Temp During Purge Conditions | | | 05000302/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000302/LER-1981-004-03, /03L-0:on 810119,position Indication for Containment Isolation Valves CAV-2 & CAV-126 Found Inoperable,In Violation of Tech Spec 3.6.3.1.Cause of CAV-2 Inoperability Unknown.Cause of CAV-126 Was Bad Breaker | /03L-0:on 810119,position Indication for Containment Isolation Valves CAV-2 & CAV-126 Found Inoperable,In Violation of Tech Spec 3.6.3.1.Cause of CAV-2 Inoperability Unknown.Cause of CAV-126 Was Bad Breaker | | | 05000302/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000302/LER-1981-005-03, /03L-0:on 801215,mechanical Seal for Bldg Spray Pump BSP-1A Found Leaking Greater than 6 Gallons/H,In Violation of Tech Spec 3.6.2.1.Caused by Defective Mechanical Seal.Review of Maint Procedure in Progress | /03L-0:on 801215,mechanical Seal for Bldg Spray Pump BSP-1A Found Leaking Greater than 6 Gallons/H,In Violation of Tech Spec 3.6.2.1.Caused by Defective Mechanical Seal.Review of Maint Procedure in Progress | | | 05000302/LER-1981-006-03, /03L-0:on 810123,breaker for Control Complex Emergency Ventilation Fan AHF-18A Found Open.Caused by Inadvertent Bumping of Breaker.Breaker Shut,Operability Checks Performed & Personnel Advised to Exercise Caution | /03L-0:on 810123,breaker for Control Complex Emergency Ventilation Fan AHF-18A Found Open.Caused by Inadvertent Bumping of Breaker.Breaker Shut,Operability Checks Performed & Personnel Advised to Exercise Caution | | | 05000302/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000302/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000302/LER-1981-007-03, /03L-0:on 810126,radiation Monitor RM-A5 Failed to Restart After Filter Change.Caused by Blown Fuse.Fuse Replaced | /03L-0:on 810126,radiation Monitor RM-A5 Failed to Restart After Filter Change.Caused by Blown Fuse.Fuse Replaced | | | 05000302/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000302/LER-1981-008-03, /03L-0:on 810204,during Charcoal Testing,Filter Sys AHFL-2D Methyl Iodide Removal Efficiency Was 92.14%. Caused by Atmospheric Pollutants & Normal Air Flow.Charcoal Cells Replaced W/New Impregnated Charcoal | /03L-0:on 810204,during Charcoal Testing,Filter Sys AHFL-2D Methyl Iodide Removal Efficiency Was 92.14%. Caused by Atmospheric Pollutants & Normal Air Flow.Charcoal Cells Replaced W/New Impregnated Charcoal | | | 05000302/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000302/LER-1981-009-03, /03L-0:on 810209,RCS Drain Tank Level Indication Was Erratic & Prevented Leak Rate Surveillance.Caused by Vapor Condensation in Instrument Sensing Lines.Lines Blown Down | /03L-0:on 810209,RCS Drain Tank Level Indication Was Erratic & Prevented Leak Rate Surveillance.Caused by Vapor Condensation in Instrument Sensing Lines.Lines Blown Down | | | 05000302/LER-1981-010-03, /03L-0:on 810217,after Routine Shutdown,Rcs Sampling Revealed That Dose Equivalent I-131 Exceeded Tech Specs.Caused by Leaking Fuel & Anticipated Dose Equivalent Iodine Transient.Purification Flow Increased | /03L-0:on 810217,after Routine Shutdown,Rcs Sampling Revealed That Dose Equivalent I-131 Exceeded Tech Specs.Caused by Leaking Fuel & Anticipated Dose Equivalent Iodine Transient.Purification Flow Increased | | | 05000302/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000302/LER-1981-011, Forwards LER 81-011/01T-1 | Forwards LER 81-011/01T-1 | | | 05000302/LER-1981-011-01, /01T-1:on 810306,containment Isolation Valves CAV-1,3,4,5 & 126 Found Incapable of Meeting Environ Qualification During Evaluation of IE Bulletin 79-01B.Caused by Potential Electrical Short Due to Flooding After LOCA | /01T-1:on 810306,containment Isolation Valves CAV-1,3,4,5 & 126 Found Incapable of Meeting Environ Qualification During Evaluation of IE Bulletin 79-01B.Caused by Potential Electrical Short Due to Flooding After LOCA | | | 05000302/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000302/LER-1981-012-03, /03L-0:on 810219,Limitorque-operated Containment Isolation Valves MUV-260 & 261 Failed to Close.Cause Unknown.Torque Switch MUV-261 Replaced & Operability Restored on 810224.Investigation Continuing | /03L-0:on 810219,Limitorque-operated Containment Isolation Valves MUV-260 & 261 Failed to Close.Cause Unknown.Torque Switch MUV-261 Replaced & Operability Restored on 810224.Investigation Continuing | | | 05000302/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000302/LER-1981-013-03, /03L-0:on 810302,during Routine Testing in Mode 5 Operation,Rcs Discovered W/Chloride Concentration of 0.18 Ppm.Caused by Release of Chlorides from Makeup. Procedures Will Be Revised by 810430 | /03L-0:on 810302,during Routine Testing in Mode 5 Operation,Rcs Discovered W/Chloride Concentration of 0.18 Ppm.Caused by Release of Chlorides from Makeup. Procedures Will Be Revised by 810430 | | | 05000302/LER-1981-014-03, /03L-0:on 810301,Clark Relay Model 5UK6-3 in Reactor Bldg Isolation Channel B,Group 2,failed to Actuate When Coil Was de-energized During SP-130.Caused by Burr on Relay Shaft.Relay Replaced | /03L-0:on 810301,Clark Relay Model 5UK6-3 in Reactor Bldg Isolation Channel B,Group 2,failed to Actuate When Coil Was de-energized During SP-130.Caused by Burr on Relay Shaft.Relay Replaced | | | 05000302/LER-1981-014, Forwards LER 81-014/03L-0 | Forwards LER 81-014/03L-0 | | | 05000302/LER-1981-015, Forwards LER 81-015/03L-0 | Forwards LER 81-015/03L-0 | | | 05000302/LER-1981-015-03, /03L-0:on 810301,Agastat Relay Model 3722B12C in Engineered Safeguards High Pressure Injection Actuation Channel B,Group 3 Block 4,failed to Change State After Receiving Signal During SP-130.Caused by Defective Relay | /03L-0:on 810301,Agastat Relay Model 3722B12C in Engineered Safeguards High Pressure Injection Actuation Channel B,Group 3 Block 4,failed to Change State After Receiving Signal During SP-130.Caused by Defective Relay | | | 05000302/LER-1981-016-03, /03L-0:on 810304,breaker for DHV-110,decay Heat Pump a Discharge Throttle Valve Tripped.Cause Unknown. DHV-110 Repetitively Cycled W/No Failures | /03L-0:on 810304,breaker for DHV-110,decay Heat Pump a Discharge Throttle Valve Tripped.Cause Unknown. DHV-110 Repetitively Cycled W/No Failures | | | 05000302/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000302/LER-1981-017, Forwards LER 81-017/03L-0.Detailed Event Analysis Encl | Forwards LER 81-017/03L-0.Detailed Event Analysis Encl | | | 05000302/LER-1981-017-03, /03L-0:on 810304,during Testing,Discovered That Containment Isolation Valve CFV-16 Would Not Move from mid-position.Caused by Valve Binding on Bushing Due to Insufficient Lubrication | /03L-0:on 810304,during Testing,Discovered That Containment Isolation Valve CFV-16 Would Not Move from mid-position.Caused by Valve Binding on Bushing Due to Insufficient Lubrication | | | 05000302/LER-1981-018, Forwards LER 81-018/03L-0 | Forwards LER 81-018/03L-0 | | | 05000302/LER-1981-018-03, /03L-0:on 810313,Gow Mac 20-250 Dihydrogen Analyzer Failed Calibr During Surveillance Program SP-708. Caused by Defective thermo-conductivity Cell.Cell Replaced & Instrument Calibr & Restored on 810316 | /03L-0:on 810313,Gow Mac 20-250 Dihydrogen Analyzer Failed Calibr During Surveillance Program SP-708. Caused by Defective thermo-conductivity Cell.Cell Replaced & Instrument Calibr & Restored on 810316 | | | 05000302/LER-1981-019-03, /03L-0:on 810313,during Normal operation,RC3,RC6 & RB3 Relays Tripped in Emergency Safeguards Actuation Channel B.Cause Attributed to Failed Hamlin Relay.Maint Revealed Addl Faulty Relays.Hamlin Replaced W/Cryden Relays | /03L-0:on 810313,during Normal operation,RC3,RC6 & RB3 Relays Tripped in Emergency Safeguards Actuation Channel B.Cause Attributed to Failed Hamlin Relay.Maint Revealed Addl Faulty Relays.Hamlin Replaced W/Cryden Relays | | | 05000302/LER-1981-019, Forwards LER 81-019/03L-0 | Forwards LER 81-019/03L-0 | | | 05000302/LER-1981-020-03, /03L-0:on 810405,during Performance of Engineered Safeguards Monthly Functional Tests,Discovered That Subsystem a Low Power Injection Channel RC-4 Would Not Reset W/Reset Permissive.Caused by Failed mercury-wetted Relay | /03L-0:on 810405,during Performance of Engineered Safeguards Monthly Functional Tests,Discovered That Subsystem a Low Power Injection Channel RC-4 Would Not Reset W/Reset Permissive.Caused by Failed mercury-wetted Relay | | | 05000302/LER-1981-020, Forwards LER 81-020/03L-0 | Forwards LER 81-020/03L-0 | | | 05000302/LER-1981-021, Forwards LER 81-021/03L-0 | Forwards LER 81-021/03L-0 | | | 05000302/LER-1981-021-03, /03L-0:on 810411,failure of Inverter D Resulted in Loss of Vital Bus VBDP-6.Caused by Shorted Diode & Blown Fuse Which May Have Resulted from Overheating in Inverter Cabinet.Diode & Fuse Replaced & Mod Procedure Revised | /03L-0:on 810411,failure of Inverter D Resulted in Loss of Vital Bus VBDP-6.Caused by Shorted Diode & Blown Fuse Which May Have Resulted from Overheating in Inverter Cabinet.Diode & Fuse Replaced & Mod Procedure Revised | | | 05000302/LER-1981-022-03, /03L-0:on 810412,following Reactor Trip,Main Steam Isolation Valve Msv Found Inoperable.Cause Undetermined.Mods Performed to Improve Valve Operation & Reliability. Functional Test Results Satisfactory.Operability Restored | /03L-0:on 810412,following Reactor Trip,Main Steam Isolation Valve Msv Found Inoperable.Cause Undetermined.Mods Performed to Improve Valve Operation & Reliability. Functional Test Results Satisfactory.Operability Restored | | | 05000302/LER-1981-022, Forwards LER 81-022/03L-0 | Forwards LER 81-022/03L-0 | | | 05000302/LER-1981-023, Forwards LER 81-023/03L-0 | Forwards LER 81-023/03L-0 | | | 05000302/LER-1981-023-03, /03L-0:on 810412,atmospheric Radiation Monitor RM-A5 Failed Due to Seized Sample Vacuum Pump.Caused by Worn Carbon Vanes.Pump Replaced.Engineering Evaluation in Progress.Supplementary Info Sheet Encl | /03L-0:on 810412,atmospheric Radiation Monitor RM-A5 Failed Due to Seized Sample Vacuum Pump.Caused by Worn Carbon Vanes.Pump Replaced.Engineering Evaluation in Progress.Supplementary Info Sheet Encl | | | 05000302/LER-1981-024-03, /03L-0:on 810414,emergency Diesel Generator 1A Found Inoperable During Monthly Test SP-354.Caused by Plugged Oil Separator in Air Ejector Train.Procedure Being Revised to Increase Cleaning & Insp Frequency | /03L-0:on 810414,emergency Diesel Generator 1A Found Inoperable During Monthly Test SP-354.Caused by Plugged Oil Separator in Air Ejector Train.Procedure Being Revised to Increase Cleaning & Insp Frequency | | | 05000302/LER-1981-024, Forwards LER 81-024/03L-0 | Forwards LER 81-024/03L-0 | | | 05000302/LER-1981-025-03, /03L-0:on 810417,EFP-2 Control Switch Discovered in Off Position.Caused by Procedural Deficiencies.Procedures Modified to Require Assurance That EFP-2 Is Selected to Auto | /03L-0:on 810417,EFP-2 Control Switch Discovered in Off Position.Caused by Procedural Deficiencies.Procedures Modified to Require Assurance That EFP-2 Is Selected to Auto | | | 05000302/LER-1981-025, Forwards LER 81-025/03L-0 | Forwards LER 81-025/03L-0 | |
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