05000364/LER-1981-019-03, /03L-0:on 810526,plant Vent Stack Effluent Monitor R-29B Was Declared Inoperable Due to Pump Trip. Caused by Dirty Filter.Filter Was Replaced.Frequency for Performing Preventative Maint on Filter Will Be Evaluated

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/03L-0:on 810526,plant Vent Stack Effluent Monitor R-29B Was Declared Inoperable Due to Pump Trip. Caused by Dirty Filter.Filter Was Replaced.Frequency for Performing Preventative Maint on Filter Will Be Evaluated
ML20005A423
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 06/25/1981
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20005A416 List:
References
LER-81-019-03L-01, LER-81-19-3L-1, NUDOCS 8106300309
Download: ML20005A423 (1)


LER-1981-019, /03L-0:on 810526,plant Vent Stack Effluent Monitor R-29B Was Declared Inoperable Due to Pump Trip. Caused by Dirty Filter.Filter Was Replaced.Frequency for Performing Preventative Maint on Filter Will Be Evaluated
Event date:
Report date:
3641981019R03 - NRC Website

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'I o 12 i l At 0500 on 5/26/81, R-29B (Plant Vent Stack Effluent Monitor) was declared inoperable l

.l0431 Iwhen the pump was found tripped. Tech. Spec. 3.3.3.1, in part, requires R-29B to be l

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