05000336/LER-1981-019-03, /03L-0:on 810527,steam-driven Auxiliary Feedwater Pump Was Removed from Svc for Planned Maint to Replace Bearings.Bearing Failure Caused by Inadequate Lubrication. Sightglass Marks Changed to Acceptable Level

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/03L-0:on 810527,steam-driven Auxiliary Feedwater Pump Was Removed from Svc for Planned Maint to Replace Bearings.Bearing Failure Caused by Inadequate Lubrication. Sightglass Marks Changed to Acceptable Level
ML20004E917
Person / Time
Site: Millstone Dominion icon.png
Issue date: 06/15/1981
From:
NORTHEAST NUCLEAR ENERGY CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20004E915 List:
References
LER-81-019-03L, LER-81-19-3L, NUDOCS 8106160145
Download: ML20004E917 (1)


LER-1981-019, /03L-0:on 810527,steam-driven Auxiliary Feedwater Pump Was Removed from Svc for Planned Maint to Replace Bearings.Bearing Failure Caused by Inadequate Lubrication. Sightglass Marks Changed to Acceptable Level
Event date:
Report date:
3361981019R03 - NRC Website

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CON'T 60 68 DOCK ET NUVBER 68 69 EVENT DATE 74 75 REPORT DATE 80 F

S EVENT DESCRIPiloN AND PROB ABLE CONSEQUENCES h lo Til I During routine power operation, the steam driven Auxiliary Feedwater pump was removed I

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g i rom service for planned maintenance to replace bearings.

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