05000267/LER-1981-011-03, /03L-0:on 810121,liquid Nitrogen Storage Tank Level Noted Below Min Required.Caused by Sys Usage & Late Delivery of Liquid Nitrogen.Delivery Restored Tank Levels to Acceptable Values.Second Load Delivered to Top Off Tank

From kanterella
(Redirected from ML20003B831)
Jump to navigation Jump to search
/03L-0:on 810121,liquid Nitrogen Storage Tank Level Noted Below Min Required.Caused by Sys Usage & Late Delivery of Liquid Nitrogen.Delivery Restored Tank Levels to Acceptable Values.Second Load Delivered to Top Off Tank
ML20003B831
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 02/19/1981
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20003B830 List:
References
LER-81-011-03L, LER-81-11-3L, NUDOCS 8102250647
Download: ML20003B831 (1)


LER-1981-011, /03L-0:on 810121,liquid Nitrogen Storage Tank Level Noted Below Min Required.Caused by Sys Usage & Late Delivery of Liquid Nitrogen.Delivery Restored Tank Levels to Acceptable Values.Second Load Delivered to Top Off Tank
Event date:
Report date:
2671981011R03 - NRC Website

text

. --

NRc FOIM 366 U. S. NUCLEAR RECULATORY COMMISSION

' (7 77)

LICENSEE EVENT REPORT CONTROL BLOCK: l l

l l

l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) i e

101i1 l c l o f y l s I v l 1.j@l o l o l-l o l o l o l o l o l-10 l o l@l 411111210 l@l l@

7 8 9 LICENSEE COCE 14 15 uCENSE NwM6ER 25 26 t.iCENSE TYPE JO

$7 CA T $8 CON'T I L @l 015101010 l 21617 @l 01112 ll ] 811 )@lo 12 li l o 19 li l@

10111 s cRcE 7

8 80 61 OOCKET NUV88R 6d 69 EVENT O ATE 14 75 REPORT OATE 80 EVENT DESCRIPTION AND PROBA8LE CONSEQUENCES h lo I:l lOn January 21, 1981, with the reactor operating at aporoximately 40': thermal power,

[ 5T3"I l the liquid nitrogen storage tank level was determined to be less than the minimum l

l o 141 1 650 gallons required by Technical Specifications. Degraded mode of LCO 4.2.12.

Re-l l o 1 s i i portable per Fort St. Vrain Technical Specification AC 7.5.2(b)2.

No accompanying

[

l o 16 l l occurrence or probable Consequence. No affect on public health or safety. Similar l

l 017 l l occurrence RO 80-39.

l 10181 l 80 7

8 9 0E Co E SUS O E COMPCNENT CODE SUSCCCE SW OCE 1o191 l Al Dlh [h Wh 12 12 IZ 12 lZ lZ Ih l Zlh l'Zlh 7

8 9

10 11 12 13 18 is 20 SEcutNTI A L OCOU R R ENCE R E' ORT REVISION LER EVENT YEAR REPORT NC.

CODE TYPE NO.

@ ygj/Ro 18 11 I l-l lo 1111 l I/I lo 13 l ltl 1-1 lo I g

a

_2t 22 23 24 26 27 28 29 30 31 32 CY MOURS S8 t 80R 8.

SUP Li MANUFAC RER TK N AC 0 0 P NT ME LT J@l v I@

LIJ@

12.J@

l o 1010101 IV l@

l Ni@

Iz l@

Iz 1919191@

33 34 35 36 34 40 el 42 43 44 47 CAUSE DESCRIPTION AND COARECTIVE ACTIONS h 1iloll System usage and late deliverv of a scheduled liquid nitrogen delivery resulted in I

w Iliquid nitrogen storage tank level being less than required by Technical Soecifi-

,,121Ications.

Receipt of the scheduled delivery restored storage tank levels to acceptablei i,, 3 g l values. A second load was ordered and delivered to top off the storage tank.

I 15 141 I l

80 7

8 9 1A inPOWER OTHER STATUS is O Y

DISCOVERY CESCRiPTtCN 11 151 l cl@ l o l 4 l 0 l@l N/A I

LLj@looerstorobservation l

7 8 3 1

12 13 44 45 46 80 AMOUNT OF ACTtVITY @ I LOCATICN CF RELEASE @

RELEASEO CF RELEASE I N/A l

liis1 W @ W @ l N/A

.ERse~~EiEx,c.3Es DEsCR,, Tic ~@

NUM.ER Tv,E li t 7 t l ol o f ol@lz l@l n/A I

a

.ER,oN~ENUL, DEsCR,TicN@

NUM8ER t i h i i ol ol 01@l s/A I

7 8 9 11 12 80 LOSS OF CR DAMAGE TQ FACILITY Q TYPE DESCRl* TION N./

1 F ITl L:J@l e

7 8 9 10 80 ISSU DE CRIPTION i 2 I o 1 LUE @lN/A 1

II'I'!I!'I, (303 785-2224 NAME OF PREPARER PHONE:

81022506@

/ /~