LER-1981-001, /01T-0:on 810107,during Performance of Quarterly Battery Check SP-511,determined That Battery Did Not Meet Tech Spec Requirements.Caused by Decrease in Specific Gravity of One Cell.Battery Placed on Equalize Charge |
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(o a :l lAt 1210 during performance of SP-511, Quarterly Battery Check (Units 1 & 2), it was,
(discovered that the Unit #2 battery did not meet the requirements of T. S. Surveil [o.2i Io s a i (lar,ee 4.8.1.1.1.c.2.b). This created an event contrary to T. S. 3.8.1.1. Redandancy l l o i s ! [wn e. nrnvided by Unit el batterv and by EDG-1A and IB.
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the public health or safety. This is the fifth occurrence for Unit 1& 2 batteries, i:.si(_the first occurrence for dav tank level and transfer numns, and the twenty-first i
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lii: lIThe cause of this event was that the soecific cravitv of one cell had decreased by I tiinI LO.013 More than 0.01 allowable) from the orevious readina.
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Nornbil ity was reetnred at 0925 of 1/8/81. The second I i. 3) [
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SUPPLEMENTARY INFORMATION 4
Report No.:
81-001/01T-0 Facility:
Crystal River Unit 83 Report Date:
February 6, 1981 Occurrence Date:
January 7, 1981 Identification of Occurrence:
Failure to meet Technical Specification Surveillance requirement 4.8.1.1.c.2.b) contrary to Technical Specification 3.8.1.1.
Conditions of Occurrence:
Mode 1 power operation (98%).
Description of Occurrence:
At 1210 during performance of SP-511, Quarterly Battery Check (Units 1 & 2), it was discovered that the Unit #3 battery did not meet the requirements of Technical Specification Surveillance 4.8.1.1.1.c.2.b).
The con-servative assumption was made that Action Statement 3.8.1.1.c was applicable. The Dmergency Diesels were fast-started to prove redundancy. The battery was put on equalize charge. At 1700, it was discovered that EDG-lA fuel oil storage tank had less than 400 gallons volume; the transfer pumps (DFP-1A and IC) had not auto started. The pumps would operate in manual control.
Maintenance was initiated and operability of the Emergency Diesels was restored at 1730 on January 7,1981, t.t 0925, on January 8, 1981, operability was restored to the Unit #3 battery.
Designation of Apparent Cause:
The cause of the.first occurrence was that the specific gravity of one cell deviated by more than 0.01 from the previous reading. The cause of the second event was a mal-adjustment of level switch DF-2-LS.
Analysis of Occurrence:
There was no effect upon the health ~or safety of the general public. The Unit #1 battery capacity was sufficient to ensure D. C. Control power to the 230 KV switchyard breakers to supply A. C. electrical power to the onsite class lE distribution system.
e SUPPLEMENTARY INFORMATION (CONTINUED)
Corrective Action
The equalizing charge restored the specific gravity of the cell to acceptable limits. A revision to Technical Soccifi-cations will be submitted to modify requirements to reflect plant design with regard to Units 1 & 2 batteries.
DP-2-Ls was adjusted and operability was restored.
Failure Data:
This is the fifth occurrence for Units 1 & 2 batteries, the first occurrence for day tank level and transfer pumps DFP-1A and 1C and this is the twenty-first event reported under this specification.
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| 05000302/LER-1981-001-01, /01T-0:on 810107,during Performance of Quarterly Battery Check SP-511,determined That Battery Did Not Meet Tech Spec Requirements.Caused by Decrease in Specific Gravity of One Cell.Battery Placed on Equalize Charge | /01T-0:on 810107,during Performance of Quarterly Battery Check SP-511,determined That Battery Did Not Meet Tech Spec Requirements.Caused by Decrease in Specific Gravity of One Cell.Battery Placed on Equalize Charge | | | 05000302/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000302/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000302/LER-1981-002-03, /03L-0:on 810109,containment Isolation Valve CAV-1 Failed to Close After Sampling Pressurizer Steam Space. Caused by Failed Contacts in Torque Switch of Valve Operator.Switch Replaced & Operability Restored | /03L-0:on 810109,containment Isolation Valve CAV-1 Failed to Close After Sampling Pressurizer Steam Space. Caused by Failed Contacts in Torque Switch of Valve Operator.Switch Replaced & Operability Restored | | | 05000302/LER-1981-003, Forwards LER 81-003/01T-0 | Forwards LER 81-003/01T-0 | | | 05000302/LER-1981-003-01, /01T-0:on 810129,containment Isolation Valves AHV-1C & AHV-1D Found Inoperable Contrary to Tech Spec 3.6.3.1.Caused by Failure of Valve to Seal at Low Ambient Temp During Purge Conditions | /01T-0:on 810129,containment Isolation Valves AHV-1C & AHV-1D Found Inoperable Contrary to Tech Spec 3.6.3.1.Caused by Failure of Valve to Seal at Low Ambient Temp During Purge Conditions | | | 05000302/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000302/LER-1981-004-03, /03L-0:on 810119,position Indication for Containment Isolation Valves CAV-2 & CAV-126 Found Inoperable,In Violation of Tech Spec 3.6.3.1.Cause of CAV-2 Inoperability Unknown.Cause of CAV-126 Was Bad Breaker | /03L-0:on 810119,position Indication for Containment Isolation Valves CAV-2 & CAV-126 Found Inoperable,In Violation of Tech Spec 3.6.3.1.Cause of CAV-2 Inoperability Unknown.Cause of CAV-126 Was Bad Breaker | | | 05000302/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000302/LER-1981-005-03, /03L-0:on 801215,mechanical Seal for Bldg Spray Pump BSP-1A Found Leaking Greater than 6 Gallons/H,In Violation of Tech Spec 3.6.2.1.Caused by Defective Mechanical Seal.Review of Maint Procedure in Progress | /03L-0:on 801215,mechanical Seal for Bldg Spray Pump BSP-1A Found Leaking Greater than 6 Gallons/H,In Violation of Tech Spec 3.6.2.1.Caused by Defective Mechanical Seal.Review of Maint Procedure in Progress | | | 05000302/LER-1981-006-03, /03L-0:on 810123,breaker for Control Complex Emergency Ventilation Fan AHF-18A Found Open.Caused by Inadvertent Bumping of Breaker.Breaker Shut,Operability Checks Performed & Personnel Advised to Exercise Caution | /03L-0:on 810123,breaker for Control Complex Emergency Ventilation Fan AHF-18A Found Open.Caused by Inadvertent Bumping of Breaker.Breaker Shut,Operability Checks Performed & Personnel Advised to Exercise Caution | | | 05000302/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000302/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000302/LER-1981-007-03, /03L-0:on 810126,radiation Monitor RM-A5 Failed to Restart After Filter Change.Caused by Blown Fuse.Fuse Replaced | /03L-0:on 810126,radiation Monitor RM-A5 Failed to Restart After Filter Change.Caused by Blown Fuse.Fuse Replaced | | | 05000302/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000302/LER-1981-008-03, /03L-0:on 810204,during Charcoal Testing,Filter Sys AHFL-2D Methyl Iodide Removal Efficiency Was 92.14%. Caused by Atmospheric Pollutants & Normal Air Flow.Charcoal Cells Replaced W/New Impregnated Charcoal | /03L-0:on 810204,during Charcoal Testing,Filter Sys AHFL-2D Methyl Iodide Removal Efficiency Was 92.14%. Caused by Atmospheric Pollutants & Normal Air Flow.Charcoal Cells Replaced W/New Impregnated Charcoal | | | 05000302/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000302/LER-1981-009-03, /03L-0:on 810209,RCS Drain Tank Level Indication Was Erratic & Prevented Leak Rate Surveillance.Caused by Vapor Condensation in Instrument Sensing Lines.Lines Blown Down | /03L-0:on 810209,RCS Drain Tank Level Indication Was Erratic & Prevented Leak Rate Surveillance.Caused by Vapor Condensation in Instrument Sensing Lines.Lines Blown Down | | | 05000302/LER-1981-010-03, /03L-0:on 810217,after Routine Shutdown,Rcs Sampling Revealed That Dose Equivalent I-131 Exceeded Tech Specs.Caused by Leaking Fuel & Anticipated Dose Equivalent Iodine Transient.Purification Flow Increased | /03L-0:on 810217,after Routine Shutdown,Rcs Sampling Revealed That Dose Equivalent I-131 Exceeded Tech Specs.Caused by Leaking Fuel & Anticipated Dose Equivalent Iodine Transient.Purification Flow Increased | | | 05000302/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000302/LER-1981-011, Forwards LER 81-011/01T-1 | Forwards LER 81-011/01T-1 | | | 05000302/LER-1981-011-01, /01T-1:on 810306,containment Isolation Valves CAV-1,3,4,5 & 126 Found Incapable of Meeting Environ Qualification During Evaluation of IE Bulletin 79-01B.Caused by Potential Electrical Short Due to Flooding After LOCA | /01T-1:on 810306,containment Isolation Valves CAV-1,3,4,5 & 126 Found Incapable of Meeting Environ Qualification During Evaluation of IE Bulletin 79-01B.Caused by Potential Electrical Short Due to Flooding After LOCA | | | 05000302/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000302/LER-1981-012-03, /03L-0:on 810219,Limitorque-operated Containment Isolation Valves MUV-260 & 261 Failed to Close.Cause Unknown.Torque Switch MUV-261 Replaced & Operability Restored on 810224.Investigation Continuing | /03L-0:on 810219,Limitorque-operated Containment Isolation Valves MUV-260 & 261 Failed to Close.Cause Unknown.Torque Switch MUV-261 Replaced & Operability Restored on 810224.Investigation Continuing | | | 05000302/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000302/LER-1981-013-03, /03L-0:on 810302,during Routine Testing in Mode 5 Operation,Rcs Discovered W/Chloride Concentration of 0.18 Ppm.Caused by Release of Chlorides from Makeup. Procedures Will Be Revised by 810430 | /03L-0:on 810302,during Routine Testing in Mode 5 Operation,Rcs Discovered W/Chloride Concentration of 0.18 Ppm.Caused by Release of Chlorides from Makeup. Procedures Will Be Revised by 810430 | | | 05000302/LER-1981-014-03, /03L-0:on 810301,Clark Relay Model 5UK6-3 in Reactor Bldg Isolation Channel B,Group 2,failed to Actuate When Coil Was de-energized During SP-130.Caused by Burr on Relay Shaft.Relay Replaced | /03L-0:on 810301,Clark Relay Model 5UK6-3 in Reactor Bldg Isolation Channel B,Group 2,failed to Actuate When Coil Was de-energized During SP-130.Caused by Burr on Relay Shaft.Relay Replaced | | | 05000302/LER-1981-014, Forwards LER 81-014/03L-0 | Forwards LER 81-014/03L-0 | | | 05000302/LER-1981-015, Forwards LER 81-015/03L-0 | Forwards LER 81-015/03L-0 | | | 05000302/LER-1981-015-03, /03L-0:on 810301,Agastat Relay Model 3722B12C in Engineered Safeguards High Pressure Injection Actuation Channel B,Group 3 Block 4,failed to Change State After Receiving Signal During SP-130.Caused by Defective Relay | /03L-0:on 810301,Agastat Relay Model 3722B12C in Engineered Safeguards High Pressure Injection Actuation Channel B,Group 3 Block 4,failed to Change State After Receiving Signal During SP-130.Caused by Defective Relay | | | 05000302/LER-1981-016-03, /03L-0:on 810304,breaker for DHV-110,decay Heat Pump a Discharge Throttle Valve Tripped.Cause Unknown. DHV-110 Repetitively Cycled W/No Failures | /03L-0:on 810304,breaker for DHV-110,decay Heat Pump a Discharge Throttle Valve Tripped.Cause Unknown. DHV-110 Repetitively Cycled W/No Failures | | | 05000302/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000302/LER-1981-017, Forwards LER 81-017/03L-0.Detailed Event Analysis Encl | Forwards LER 81-017/03L-0.Detailed Event Analysis Encl | | | 05000302/LER-1981-017-03, /03L-0:on 810304,during Testing,Discovered That Containment Isolation Valve CFV-16 Would Not Move from mid-position.Caused by Valve Binding on Bushing Due to Insufficient Lubrication | /03L-0:on 810304,during Testing,Discovered That Containment Isolation Valve CFV-16 Would Not Move from mid-position.Caused by Valve Binding on Bushing Due to Insufficient Lubrication | | | 05000302/LER-1981-018, Forwards LER 81-018/03L-0 | Forwards LER 81-018/03L-0 | | | 05000302/LER-1981-018-03, /03L-0:on 810313,Gow Mac 20-250 Dihydrogen Analyzer Failed Calibr During Surveillance Program SP-708. Caused by Defective thermo-conductivity Cell.Cell Replaced & Instrument Calibr & Restored on 810316 | /03L-0:on 810313,Gow Mac 20-250 Dihydrogen Analyzer Failed Calibr During Surveillance Program SP-708. Caused by Defective thermo-conductivity Cell.Cell Replaced & Instrument Calibr & Restored on 810316 | | | 05000302/LER-1981-019-03, /03L-0:on 810313,during Normal operation,RC3,RC6 & RB3 Relays Tripped in Emergency Safeguards Actuation Channel B.Cause Attributed to Failed Hamlin Relay.Maint Revealed Addl Faulty Relays.Hamlin Replaced W/Cryden Relays | /03L-0:on 810313,during Normal operation,RC3,RC6 & RB3 Relays Tripped in Emergency Safeguards Actuation Channel B.Cause Attributed to Failed Hamlin Relay.Maint Revealed Addl Faulty Relays.Hamlin Replaced W/Cryden Relays | | | 05000302/LER-1981-019, Forwards LER 81-019/03L-0 | Forwards LER 81-019/03L-0 | | | 05000302/LER-1981-020-03, /03L-0:on 810405,during Performance of Engineered Safeguards Monthly Functional Tests,Discovered That Subsystem a Low Power Injection Channel RC-4 Would Not Reset W/Reset Permissive.Caused by Failed mercury-wetted Relay | /03L-0:on 810405,during Performance of Engineered Safeguards Monthly Functional Tests,Discovered That Subsystem a Low Power Injection Channel RC-4 Would Not Reset W/Reset Permissive.Caused by Failed mercury-wetted Relay | | | 05000302/LER-1981-020, Forwards LER 81-020/03L-0 | Forwards LER 81-020/03L-0 | | | 05000302/LER-1981-021, Forwards LER 81-021/03L-0 | Forwards LER 81-021/03L-0 | | | 05000302/LER-1981-021-03, /03L-0:on 810411,failure of Inverter D Resulted in Loss of Vital Bus VBDP-6.Caused by Shorted Diode & Blown Fuse Which May Have Resulted from Overheating in Inverter Cabinet.Diode & Fuse Replaced & Mod Procedure Revised | /03L-0:on 810411,failure of Inverter D Resulted in Loss of Vital Bus VBDP-6.Caused by Shorted Diode & Blown Fuse Which May Have Resulted from Overheating in Inverter Cabinet.Diode & Fuse Replaced & Mod Procedure Revised | | | 05000302/LER-1981-022-03, /03L-0:on 810412,following Reactor Trip,Main Steam Isolation Valve Msv Found Inoperable.Cause Undetermined.Mods Performed to Improve Valve Operation & Reliability. Functional Test Results Satisfactory.Operability Restored | /03L-0:on 810412,following Reactor Trip,Main Steam Isolation Valve Msv Found Inoperable.Cause Undetermined.Mods Performed to Improve Valve Operation & Reliability. Functional Test Results Satisfactory.Operability Restored | | | 05000302/LER-1981-022, Forwards LER 81-022/03L-0 | Forwards LER 81-022/03L-0 | | | 05000302/LER-1981-023, Forwards LER 81-023/03L-0 | Forwards LER 81-023/03L-0 | | | 05000302/LER-1981-023-03, /03L-0:on 810412,atmospheric Radiation Monitor RM-A5 Failed Due to Seized Sample Vacuum Pump.Caused by Worn Carbon Vanes.Pump Replaced.Engineering Evaluation in Progress.Supplementary Info Sheet Encl | /03L-0:on 810412,atmospheric Radiation Monitor RM-A5 Failed Due to Seized Sample Vacuum Pump.Caused by Worn Carbon Vanes.Pump Replaced.Engineering Evaluation in Progress.Supplementary Info Sheet Encl | | | 05000302/LER-1981-024-03, /03L-0:on 810414,emergency Diesel Generator 1A Found Inoperable During Monthly Test SP-354.Caused by Plugged Oil Separator in Air Ejector Train.Procedure Being Revised to Increase Cleaning & Insp Frequency | /03L-0:on 810414,emergency Diesel Generator 1A Found Inoperable During Monthly Test SP-354.Caused by Plugged Oil Separator in Air Ejector Train.Procedure Being Revised to Increase Cleaning & Insp Frequency | | | 05000302/LER-1981-024, Forwards LER 81-024/03L-0 | Forwards LER 81-024/03L-0 | | | 05000302/LER-1981-025-03, /03L-0:on 810417,EFP-2 Control Switch Discovered in Off Position.Caused by Procedural Deficiencies.Procedures Modified to Require Assurance That EFP-2 Is Selected to Auto | /03L-0:on 810417,EFP-2 Control Switch Discovered in Off Position.Caused by Procedural Deficiencies.Procedures Modified to Require Assurance That EFP-2 Is Selected to Auto | | | 05000302/LER-1981-025, Forwards LER 81-025/03L-0 | Forwards LER 81-025/03L-0 | |
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