05000278/LER-1981-003-01, /01T-0:on 810113,during Surveillance Test W/Unit at Full Power,Oil Leak of Approx 3-5 Gallons Per Minute Discovered on Oil Supply Line to HPCI Turbine Manual/ Overspeed Trip Mechanism.Caused by Ruptured Diaphragm

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/01T-0:on 810113,during Surveillance Test W/Unit at Full Power,Oil Leak of Approx 3-5 Gallons Per Minute Discovered on Oil Supply Line to HPCI Turbine Manual/ Overspeed Trip Mechanism.Caused by Ruptured Diaphragm
ML20003B104
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 01/27/1981
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20003B097 List:
References
LER-81-003-01T, LER-81-3-1T, NUDOCS 8102100355
Download: ML20003B104 (1)


LER-1981-003, /01T-0:on 810113,during Surveillance Test W/Unit at Full Power,Oil Leak of Approx 3-5 Gallons Per Minute Discovered on Oil Supply Line to HPCI Turbine Manual/ Overspeed Trip Mechanism.Caused by Ruptured Diaphragm
Event date:
Report date:
2781981003R01 - NRC Website

text

NRC pORM X,6 U. 4. *SUCLsAd dLGulal uit Y C041.%IlaS40fd (7 771 ' "Un,tc 3 LICENSEE EVENT REPORT Report No.

3-81-03/1T

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CONTROL BLOCK: l l

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(PLEASE PRINT OR TYPE ALL REQUIREO INFORMATION) i e

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7 8 3 LICENSEE CCOE 14 IS LICENSE NUMSER 25 26 LICENSE TYPE 40 67 GAT $8 C090'T l0IiI 5o R$ l L l@lO l 5 l 0l -l Ol2 l7 18 @l _0 l 1 l 1 l 3 l 8 l 1 l@l 0 l 1 l 2 l 7 l 8 l1 l@

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60 68 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPQRT DATE 80 EVENT DESCRIPTION AND PRO 8ABLE CONSEQUENCES h Io !aI l During a Surveillance Test with the unit at full power, an oil leak of I

f o lai I about 3 to 5 GPM was discovered on the oil supply line to the HPCI l

l o 14 I I turbine manual /overspeed trip mechanism.

If HPCI turbine had started l

og5l l with oil leaking from the line, oil would still have been supplied to l

l 016 l l the bearings for about 30 minutes at reduced pressure. At that coint a l

jol7ll turbine bearing low pressure alarm would have been received. Remaining l

t o is i i ECCS systems were immediately verified to be operable.

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9 10 11 12 13 1d 19 20 SEQUENTIAL CCCURRENCE REPORT REVISsCN L

EVENT YEAR REPORT No.

CODE TYPE NG.

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9 00 31 32 KN AC C oP NT ME HOURS 22 38 i FCR 8.

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37 40 el 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h gg oj l The cause was determined to be a ruptured diaphragm on the Robertshaw l

i ii l l oil pressure control valve Model VC-210. A new diaphracm was installed I

,,,, j in the valve and the system satisfactorily tested and returned to l

,,3l l service on January 13, 1981 I

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8 9 to 11 44 46 80 ptRSONNEL EXPOSURES NUM6ER TYPE

DESCRIPTION

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2 PERSc~NEl'i,uu' RIES oESCRiPTioNh NuvsER i la l l 0l 0l 0l@l N/A l

8 9 11 12 80 LOSS CP CR DAMAGE To FAC3LITV TVPE

DESCRIPTION

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'4 to 30 PUBLICITY a 101 l N l@DEScalPTICN NRC USE ONLY ISSU E D thSL(_-,

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