LER-1981-007, Forwards LER 81-007/03T-0 |
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pubuc sendee company oe odende 16805 ROAD 19%
PLATTEVILLE, COLOR ADO 80651 February 3,1981 Fort St. Vrain Unit No. 1 P-81038 Mr. Karl V. Seyfrit, Director Nuclear Regulatory Comission Region IV Of fic.e of Inspection and Enforcement 611 Ryan Plaza Drive Suite 1000 Arlington, Texas 76012 Reference: FaciI tty Operating License No. DPR-34 Docket No. 50-267
Dear Mr. Seyfrit:
Enclosed please find a copy of Reportable Occurrence Report No. 50-267/
81-007, Final, submitted per the requirements of Technical Specification AC 7. 5. 2 (a)2.
Also, please find enclosed one copy of the Licensee Event Report for Reportable Occurrence Report No. 50-267/81-007.
Very truly yours,*
Don Warembourg Manager, Nuclear Production DW/cis Enclosure cc: Director, MIPC 0Mi g
snos1o,,3g9
REPORT DATE:
Februarv 3, 1981 REPORTABLE OCCURRENCE 81-007 Determined ISSUE O OCCURRENCE DATE:
Januarv 20, 1981 Page 1 of 5 FORT ST. VRAIN NUCLEAR CENERATING STATION PUBLIC SERVICE COMPANY OF COLORADO 16805 WELD C01.TIY ROAD 191/2 PLATTEVILLE, COLORADO 80651 REPORT No. 50-267/81-007/01-T-0 Final IDENTIFICATION OF OCCURRENCE:
On Tuesday, January 20, 1981, while evaluating PCRV cooling water system temperature data in preparation of a reportable occurrence for a degraded mode of LCO 4.2.15(e), it was determined that the minimum average of the inlet and outlet cooling water temperatures in Loop 2 were less than 100*F from approximately 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br /> on January 8, 1981, until approximately 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br /> on January 10, 1981.
This event is reportable per Fort St. Vrain Technical Specification AC 7.5.2(a)2.
CONDITIONS PRIOR TO OCCURRENCE:
Cold shutdotm.
THE MAJOR PLANT PARAMETERS AT THE TIME OF THE EVENT L' AS FOLLOWS:
Reactor Power 0.W"
.o%
Primary Coolant Pressure 300 7sIA 300 PSIA Temperature Circulator Inlet 85*F 4
Temperature Core Outler 120*F Total Flow 144,000 f/hout 4.1%
Secondary Coolant Pressure 232 PSIG Temperatura 111* F Flow 176,000 #/ hour, 7.7%
- - Electrical 0 MWe, 0.0%
REPORTABLE OCCURRENCE 81-007 ISSUE O Page 2 of 5 DESCRIPTION OF OCCURRENCE:
At 0430 hours0.00498 days <br />0.119 hours <br />7.109788e-4 weeks <br />1.63615e-4 months <br /> on January 8,1981, the average of the inlet and outlet water temperature of the PCRV liner cooling system Loop 2 decreased below 100*F.
At 2330 hours0.027 days <br />0.647 hours <br />0.00385 weeks <br />8.86565e-4 months <br /> on January 8, 1981, the Loop 1 average also dropped below 100*F.
Loop 1 increased to 100*F at 0415 hours0.0048 days <br />0.115 hours <br />6.861772e-4 weeks <br />1.579075e-4 months <br /> on January 9,1981.
Loop 2 increased to 100*F at 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br /> on January 10, 1981.
Fort St. Vrain Technical Specification LCO 4.2.15 states "The temperature of the PCRV cooling water system shall be maintained within the limits stated below, irrespective of whether the reactor is operating or shutdown:"
One of the limits states; "The minimum average of the inlet and outlet cooling water temperatures shall be greater than or equal to 100*F."
No time limit is specified in LCO 4.2.15; however, Section 4.0 of the Tech-nical Specifications allows a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period for correction of an LCO vio-lacion if no other tims limit is specified.
The Loop i event, corrected within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, constitutes operation in a de-1 graded mode allowed by an LCO and is reported as such in accordance with Section AC 7.5.2(b)2 of the Fort St. Vrain Technical Specifications.
The Loop 2 event extended for more than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and constitutes operation of a system with a parameter subject to a limiting condition less conserva-tive than the least conservative aspect of the limiting condition for oper-acion established in the Technical Specifications. This event is reported in accc rdance with AC 7.5.2(a)2 of the Fort St. Vrain Technical Specifi-cations.
APPARENT CAUSE OF OCCURRENCE:
Personnel error.
ANALYSIS OF OCCURRENCE:
The reactor was shutdown on December 31, 1980, and cooled down to approxi-mately 115'F on January 1, 1981. Ths primary coolant temperature was re-duced further on January 6,1981, to about 100*F, and on January 7,1981,. co approximately 80*F.
REPORTABLE OCCURRENCE 81-007 ISSUE O Page 3 of 5 ANALYSIS OF OCCURRENCE: (Cont'd)
During shutdown conditions, the PCRV liner cooling system continues to remove heat from et.e PCRV, but the heat removal rate is reduced by warming the inlet water with steam coils in the surge tanks.
The cooling water side of the PCRV liner cooling heat system heat exchanger was isolated on January 2, 1981, to reduce system heat loss, and steam was placed on the surge tank January 3, 1981. Because of pri=ary coolant temp-eratures, there was little, if any, heat transfer to the PCRV cooling system from that sosrce, 4:4 after the reduction on January 7, 1981, there may have been some heat loss to the primary coolant.
The Technical Specificacicu LCO 4.2.15 places limits on the PCRV cooling water temperature in order to maintain the PCRV integrity. One of these limits requires that the average of the inlet and outlet cooling water temp-erature be greater than or equal to 100*F to ensure liner operation above the fracture transition elastic temperature.
The average of the PCRV liner cooling system Loop 2 inlet and outlet water temperature was 101.25'F at 0000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> on January 8,1981, but was decreasing and went below 100*F at approximately 0430 hours0.00498 days <br />0.119 hours <br />7.109788e-4 weeks <br />1.63615e-4 months <br />. Loop 1 average temperature was 100*F at 2200 hours0.0255 days <br />0.611 hours <br />0.00364 weeks <br />8.371e-4 months <br /> January 8,1981, but was below 100*F at about 2330 hours0.027 days <br />0.647 hours <br />0.00385 weeks <br />8.86565e-4 months <br />.
It is not possible to determine if the cooling water system temperature decrease was due to increased heat loss from the system or decreased heat input via the surge tanks. Probably, the decrease below 100*F resulted from a combination of these causes.
At 0130 hours0.0015 days <br />0.0361 hours <br />2.149471e-4 weeks <br />4.9465e-5 months <br />, January 9,1981, the out of limit condition was noticed by an operator, and the steam supply to the surge tank heating coils was in-crease d.
The increase in system heat input was sufficient to bring loop 1 inlet and outlet water temperature average back above 100*F by approximately 0415 hours0.0048 days <br />0.115 hours <br />6.861772e-4 weeks <br />1.579075e-4 months <br /> on January 9, 1981.
Loop 2, however, was colder (average = 96.25*F, the lowest temperature reached) and had been below 100*F for about 21 hours2.430556e-4 days <br />0.00583 hours <br />3.472222e-5 weeks <br />7.9905e-6 months <br /> by the time the heat input was increased. The increase in steam supply increased the average temperature, but not sufficiently to bring it back above 100*F within the 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> al-lotted by the LCO. Loop 2 continued to operate with an inlet water, outlet water temperature average below 100*F until 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br /> on January 10, 1981.
Loop 1 was below 100*F for about 4.75 hours8.680556e-4 days <br />0.0208 hours <br />1.240079e-4 weeks <br />2.85375e-5 months <br /> while Loop 2 was below 100*F for about 53.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.
I
REPORTABLE OCCL'RROiCE 81-007 I
ISSL'E O Page 4 of 5 CORRECTIVE ACTION:
The Loop 1 degraded condition was corrected by increasing the steam supply pressure to the system surge tanks.
The Loop 2 condition was corrected when the average water temperature in-creased abovs 100*F.
No specific cause for the correction can be. identified.
Correct cperation of the PCRV liner cooling system during all conditions will be reviewed with all Licensed Operators by the Training Department.
A request has been sent to the Nuclear Project Department to traluate the effects, if any, on the PCRV top head liner material as a result of the low cooling water temperature in Loop 2.
No further corrective action is anticipated or required.
FAILURE DATA /SIMILAR REPORTED OCC'JRRE' ICES:
None PROGRAMMATIC IMPACT:
None CODE IMPACT:
None G
e REPORTABLE OCCtIRENCE 81-007 ISSLT 0 Page 5 of 5 Prepared By:
$ff{ k, M
Richard R. Fros:
Technical Services Technician Revie>ed By:
./
. f. Gahn Itchnical Services Supervisor Reviewed By:
4 Frank M. Mathie Operations Manager Approved By:
7[h Don Warembourg Manager, Nuclear Production 4
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| 05000267/LER-1981-001, Forwards LER 81-001/03L-0.Includes Narrative Description of Event Re High Outlet Temp in Pcrv Cooling Water Sys | Forwards LER 81-001/03L-0.Includes Narrative Description of Event Re High Outlet Temp in Pcrv Cooling Water Sys | | | 05000267/LER-1981-001-03, /03L-0:on 801230,outlet Temp of Loop 2 Pcrv Cooling Water Sys Exceeded Tech Spec Level.Caused by High Setpoint of Cooling Water Temp Controller Following Calibr. Controller Reset & Operators Will Be Reinstructed on Sys | /03L-0:on 801230,outlet Temp of Loop 2 Pcrv Cooling Water Sys Exceeded Tech Spec Level.Caused by High Setpoint of Cooling Water Temp Controller Following Calibr. Controller Reset & Operators Will Be Reinstructed on Sys | | | 05000267/LER-1981-002-03, /03L-0:on 810107,during Normal Operation,Sampling Requirements of SR NR1.1 Found Not Met for Day shift,801225. Caused by Personnel Error.Sampling Resumed on Next Shift & Personnel Reinstructed Re Importance of Requirements | /03L-0:on 810107,during Normal Operation,Sampling Requirements of SR NR1.1 Found Not Met for Day shift,801225. Caused by Personnel Error.Sampling Resumed on Next Shift & Personnel Reinstructed Re Importance of Requirements | | | 05000267/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000267/LER-1981-003-03, /03L-0:on 810106,during Test,One Channel of 1D Helium Circulator Drain Malfunction Found Inoperable.Caused by Blown Switch Module Fuse.Fuse Replaced & Switch Returned to Svc | /03L-0:on 810106,during Test,One Channel of 1D Helium Circulator Drain Malfunction Found Inoperable.Caused by Blown Switch Module Fuse.Fuse Replaced & Switch Returned to Svc | | | 05000267/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000267/LER-1981-004-03, /03L-0:on 810115,high Residual Chlorine Levels Found in Circulating Water Sys Liquid Effluent Sample.Cause Unknown.Subsequent Samples Normal | /03L-0:on 810115,high Residual Chlorine Levels Found in Circulating Water Sys Liquid Effluent Sample.Cause Unknown.Subsequent Samples Normal | | | 05000267/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000267/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000267/LER-1981-005-03, /03L-0:on 810107,during Surveillance Testing,Trip Setting on PDIS-21177 Bearing Water Differential Pressure Switch Found Below Tech Spec Limit.Caused by Instrument Drift.Switch Adjusted & Returned to Svc | /03L-0:on 810107,during Surveillance Testing,Trip Setting on PDIS-21177 Bearing Water Differential Pressure Switch Found Below Tech Spec Limit.Caused by Instrument Drift.Switch Adjusted & Returned to Svc | | | 05000267/LER-1981-006-03, During Annual Testing & Calibr,Six of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | During Annual Testing & Calibr,Six of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | | | 05000267/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000267/LER-1981-007, Forwards LER 81-007/03T-0 | Forwards LER 81-007/03T-0 | | | 05000267/LER-1981-007-03, /03T-0:on 810108,during Pcrv Cooling Water Sys Data Evaluation,Violation of Limiting Conditions of Operation Found Re Loop 2 Inlet & Outlet Average Temp Below Tech Spec Limit.Caused by Insufficient Heat Input | /03T-0:on 810108,during Pcrv Cooling Water Sys Data Evaluation,Violation of Limiting Conditions of Operation Found Re Loop 2 Inlet & Outlet Average Temp Below Tech Spec Limit.Caused by Insufficient Heat Input | | | 05000267/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000267/LER-1981-008-03, /03X-2:on 810120,during Primary Coolant Pressure Scram,Calibr Found Voltage Outputs of Three Pressure Transmitters High.Caused by Instrument Drift.Pressure Transmitters Calibr | /03X-2:on 810120,during Primary Coolant Pressure Scram,Calibr Found Voltage Outputs of Three Pressure Transmitters High.Caused by Instrument Drift.Pressure Transmitters Calibr | | | 05000267/LER-1981-009, Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | | | 05000267/LER-1981-009-03, /03L-0:on 810116-0131,plant Operated in Degraded Mode on Five Occasions.Caused by Moisture Outgassing from Core Graphite Due to Increased Power Level.Average Core Outlet Temp Reduced & Purification Sys Removed | /03L-0:on 810116-0131,plant Operated in Degraded Mode on Five Occasions.Caused by Moisture Outgassing from Core Graphite Due to Increased Power Level.Average Core Outlet Temp Reduced & Purification Sys Removed | | | 05000267/LER-1981-010-03, /03L-0:on 810120,five Sample Flow Circuits Found Out of Calibr.Caused by Change of Instrument Characteristics.Calibr Values Revised & Flow Transmitters Recalibr.Alarm Setpoint Functional Test Values Also Changed | /03L-0:on 810120,five Sample Flow Circuits Found Out of Calibr.Caused by Change of Instrument Characteristics.Calibr Values Revised & Flow Transmitters Recalibr.Alarm Setpoint Functional Test Values Also Changed | | | 05000267/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000267/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000267/LER-1981-011-03, /03L-0:on 810121,liquid Nitrogen Storage Tank Level Noted Below Min Required.Caused by Sys Usage & Late Delivery of Liquid Nitrogen.Delivery Restored Tank Levels to Acceptable Values.Second Load Delivered to Top Off Tank | /03L-0:on 810121,liquid Nitrogen Storage Tank Level Noted Below Min Required.Caused by Sys Usage & Late Delivery of Liquid Nitrogen.Delivery Restored Tank Levels to Acceptable Values.Second Load Delivered to Top Off Tank | | | 05000267/LER-1981-012-03, /03L-0:on 810127,six of Twelve Steam Pipe Rupture (Pipe Cavity)Ultrasonic Noise Channels Had Unacceptably Low Response to Known Noise Source During Test.Caused by Microphone &/Or Transmitter Gain Reduced to Stop Tripping | /03L-0:on 810127,six of Twelve Steam Pipe Rupture (Pipe Cavity)Ultrasonic Noise Channels Had Unacceptably Low Response to Known Noise Source During Test.Caused by Microphone &/Or Transmitter Gain Reduced to Stop Tripping | | | 05000267/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000267/LER-1981-013-01, /01T-0:on 810203,following Liquid Waste Release 429,tritium Concentration Exceeded Tech Spec.Caused by Sys Design Inadequacy W/Oil Separator on Liquid Waste Discharge Line.Bypass Installed Around Oil Separator | /01T-0:on 810203,following Liquid Waste Release 429,tritium Concentration Exceeded Tech Spec.Caused by Sys Design Inadequacy W/Oil Separator on Liquid Waste Discharge Line.Bypass Installed Around Oil Separator | | | 05000267/LER-1981-013, Forwards LER 81-013/01T-0.Detailed Event Analysis Submitted | Forwards LER 81-013/01T-0.Detailed Event Analysis Submitted | | | 05000267/LER-1981-014, Forwards LER 81-014/03L-0.Detailed Summary Also Encl | Forwards LER 81-014/03L-0.Detailed Summary Also Encl | | | 05000267/LER-1981-014-03, /03L-0:on 810104,instrument Air Compressors 1C & 1A Out of Svc,Leaving Only Compressor 1B in Svc.Caused by Compressor 1C Tripping on High Discharge Air Temp & Compressor 1A Being Cleared Out for Insp & Repairs | /03L-0:on 810104,instrument Air Compressors 1C & 1A Out of Svc,Leaving Only Compressor 1B in Svc.Caused by Compressor 1C Tripping on High Discharge Air Temp & Compressor 1A Being Cleared Out for Insp & Repairs | | | 05000267/LER-1981-015, Forwards LER 81-015/03L-0.Detailed Event Analysis Encl | Forwards LER 81-015/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-015-03, /03L-0:on 810204-0220,plant Operated in Degraded Mode on Nine Occasions.Causes Include Increased Oxidant Outgassing After Power Increase & Moisture Introduced Into Primary Coolant as Part of Approved Test | /03L-0:on 810204-0220,plant Operated in Degraded Mode on Nine Occasions.Causes Include Increased Oxidant Outgassing After Power Increase & Moisture Introduced Into Primary Coolant as Part of Approved Test | | | 05000267/LER-1981-016-03, During Testing,Three of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | During Testing,Three of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | | | 05000267/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000267/LER-1981-017-03, /03L-0:on 810217,standby Diesel Engine 1B Tripped on High Cooling Water Temp.Caused by Sticking Temp Control Valve.Valve Disassembled,Cleaned & Returned to Svc | /03L-0:on 810217,standby Diesel Engine 1B Tripped on High Cooling Water Temp.Caused by Sticking Temp Control Valve.Valve Disassembled,Cleaned & Returned to Svc | | | 05000267/LER-1981-017, Forwards LER 81-017/03L-0 | Forwards LER 81-017/03L-0 | | | 05000267/LER-1981-018-03, /03L-0:on 810214,sample Flow Alarm Setpoints of Three Dewpoint Moisture Monitors Found Outside Tech Spec. Probably Caused by Previous Misadjustment.Trip Points Readjusted | /03L-0:on 810214,sample Flow Alarm Setpoints of Three Dewpoint Moisture Monitors Found Outside Tech Spec. Probably Caused by Previous Misadjustment.Trip Points Readjusted | | | 05000267/LER-1981-018, Forwards LER 81-018/03L-0.Detailed Event Analysis Encl | Forwards LER 81-018/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-019, Forwards LER 81-019/03L-0.Detailed Event Analysis Encl | Forwards LER 81-019/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-019-03, /03L-0:on 810220,plant Operated in Degraded Mode to Repair Pressure Control Valve PV-21243-1.Caused by Excessive Leakage Through 1/2-inch Masoneilan Pressure Control Valve.Valve Stroke Lengthened.Seat & Stem Replaced | /03L-0:on 810220,plant Operated in Degraded Mode to Repair Pressure Control Valve PV-21243-1.Caused by Excessive Leakage Through 1/2-inch Masoneilan Pressure Control Valve.Valve Stroke Lengthened.Seat & Stem Replaced | | | 05000267/LER-1981-020, Forwards LER 81-020/03L-0.Detailed Event Analysis Encl | Forwards LER 81-020/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-020-03, /03L-0:on 810226,primary Coolant Moisture & Oxidants Exceeded Limits.Caused by Circulator Buffer Sys Upset & Helium Circulator Trip Due to 810223 Reactor Scram. Reactor Power Reduced Until Moisture Level Decreased | /03L-0:on 810226,primary Coolant Moisture & Oxidants Exceeded Limits.Caused by Circulator Buffer Sys Upset & Helium Circulator Trip Due to 810223 Reactor Scram. Reactor Power Reduced Until Moisture Level Decreased | | | 05000267/LER-1981-021, Forwards LER 81-021/03L-0.Detailed Event Analysis Encl | Forwards LER 81-021/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-021-03, /03L-0:on 810302,liquid Nitrogen Storage Tank Level Lower than Tech Spec Requires.Caused by Sys Usage & Unavailable Recondensers.Level Restored W/Two Loads | /03L-0:on 810302,liquid Nitrogen Storage Tank Level Lower than Tech Spec Requires.Caused by Sys Usage & Unavailable Recondensers.Level Restored W/Two Loads | | | 05000267/LER-1981-022, Forwards LER 81-022/03L-0.Detailed Event Analysis Encl | Forwards LER 81-022/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-022-03, /03L-0:on 810310,found That Total Dissolved Solids in Plant Nonradioactive Liquid Waste Effluent Exceeded Tech Specs on 810224.Caused by Restoration of Water Sys Blowdown at High Rate.Blowdown Reduced | /03L-0:on 810310,found That Total Dissolved Solids in Plant Nonradioactive Liquid Waste Effluent Exceeded Tech Specs on 810224.Caused by Restoration of Water Sys Blowdown at High Rate.Blowdown Reduced | | | 05000267/LER-1981-023, Forwards LER 81-023/03L-0.Detailed Event Analysis Encl | Forwards LER 81-023/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-023-03, /03L-0:on 810310,during Release of Reactor Bldg Sump,Sump Pump Effluent Discharge Proportional Sampler Found Inoperable.Caused by Error in Instructions.New Instructions Issued to Assure Sampler Operability | /03L-0:on 810310,during Release of Reactor Bldg Sump,Sump Pump Effluent Discharge Proportional Sampler Found Inoperable.Caused by Error in Instructions.New Instructions Issued to Assure Sampler Operability | | | 05000267/LER-1981-024-03, During Testing,Five of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Accumulation of Dirt on Switches.Switches Replaced | During Testing,Five of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Accumulation of Dirt on Switches.Switches Replaced | | | 05000267/LER-1981-024, Forwards LER 81-024/03L-0.Detailed Event Analysis Encl | Forwards LER 81-024/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-025, Forwards LER 81-025/03L-0.Detailed Event Analysis Encl | Forwards LER 81-025/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-025-03, /03X-1:on 810317,liquid Nitrogen Storage Tank Level Decreased to Below 650 Gallons.Caused by Loss of Power to Fill Line Isolation Valve.Circuit Breaker Reclosed.Level Reestablished.Bypass Valve Installed Around Converter | /03X-1:on 810317,liquid Nitrogen Storage Tank Level Decreased to Below 650 Gallons.Caused by Loss of Power to Fill Line Isolation Valve.Circuit Breaker Reclosed.Level Reestablished.Bypass Valve Installed Around Converter | |
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