05000296/LER-1980-058-03, /03L-0:on 801207,MSIV 1-14,1-15,1-26,1-27,1-37 & 1-38 & 1-51 Found Leaking.Caused by Seating Surface Deterioration Due to Normal Wear.Valves Repaired

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/03L-0:on 801207,MSIV 1-14,1-15,1-26,1-27,1-37 & 1-38 & 1-51 Found Leaking.Caused by Seating Surface Deterioration Due to Normal Wear.Valves Repaired
ML19351F563
Person / Time
Site: Browns Ferry 
Issue date: 01/06/1981
From:
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19351F548 List:
References
LER-80-058-03L-02, LER-80-58-3L-2, NUDOCS 8101130505
Download: ML19351F563 (2)


LER-1980-058, /03L-0:on 801207,MSIV 1-14,1-15,1-26,1-27,1-37 & 1-38 & 1-51 Found Leaking.Caused by Seating Surface Deterioration Due to Normal Wear.Valves Repaired
Event date:
Report date:
2961980058R03 - NRC Website

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42 43 44 es CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 27 ii t o ] l Valves exceedei leak rate due to seating surface deterioration caused by normal

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i BFRO 296 / 80058 Technical Specification involved 3.7.A Reported Under Technical Specification 6.7.2.a.3 Date of Occurrence 12/7/80 Time of Occurrence 0400 Unit 3

Identification and Description of Occurrence:

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Main steam isolation valves 1-14, 1-15, 1-26, 1-27, 1-37, 1-38 and 1-51 exceeded the allowable leak rate of 11.5 SCFH per valve.

gnditions ' Prior to Occurrence:

Unit 1 @ 97% NWe I

Unit 2 @ 78% NWe

" Unit 3 @ 0% refuel.ing outage 1

Action specified in the Technical Specification Surveillance Requirements met due to inoperable equipment. Describe.

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NA gparent Cause of Occurrence:

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Valve seat deterioration due to normal wear and steam erosion.

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Analpis of Occurrence:

Ih There was no damage to plant equipment. Here was no activity release, no personnel exposure or injury and pp danger to the health or safety of the public.

Corrective Action

MSIV's were repaired and then rosested in accordance with SI 4.7.A.2.g-3 until i,

satisfactory results were obtained. Iong-term recurrence control being studied 1

by IN DES.

i Failure Data:

l BFRO-50-259/77023, 259/78034, 260/79007, 296 /78025, 296/79014, 259/80003, 260/80042.

eriod - Lifetime; Responsibility - Administrative Supervisor

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