05000267/LER-1981-015-03, /03L-0:on 810204-0220,plant Operated in Degraded Mode on Nine Occasions.Causes Include Increased Oxidant Outgassing After Power Increase & Moisture Introduced Into Primary Coolant as Part of Approved Test

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/03L-0:on 810204-0220,plant Operated in Degraded Mode on Nine Occasions.Causes Include Increased Oxidant Outgassing After Power Increase & Moisture Introduced Into Primary Coolant as Part of Approved Test
ML19347D237
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 03/06/1981
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19347D236 List:
References
LER-81-015-03L, LER-81-15-3L, NUDOCS 8103110527
Download: ML19347D237 (9)


LER-1981-015, /03L-0:on 810204-0220,plant Operated in Degraded Mode on Nine Occasions.Causes Include Increased Oxidant Outgassing After Power Increase & Moisture Introduced Into Primary Coolant as Part of Approved Test
Event date:
Report date:
2671981015R03 - NRC Website

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.2 EVENT DESCmPTION AND PRCB ASLE CONSECUENCES h l o ;;l l During the period from Februarv 4, 1981, to Februarv 20. 1981. the olant was coersted I ib5TT'l I in a degraded ciode of LCO 4.2.10 on nine occasions. These events are reportable per I s o ;4 l l Fo rt S t. Vrain Technical Specification AC 7. 5. 2(b)2. There are no prnbable cense-I jois;lquences. There is no effect on public health or safety. Related reports are 77-36, l

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