LER-1981-019, /03L-0:on 810214,at 100% Power,Auxiliary Feedwater Overspeed Trip Valve Tripped Twice,Rendering Feedwater Pump Inoperable.Caused by Improper Alignment of Linkage Parts.Parts Machined & Pump Returned to Svc |
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O LICENSEE EVENT REPORT i
CONTROL BLOCK / / / / / / / (1)
(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
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LICENSEE CODE LICENSE NUMBER LICENSE TYPE CAT
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DOCKET NUMBER EVENT DATE REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES (10)
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On February 14, 1981, with Unit 2 at 100 percent power, the auxiliary feedwater/
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pump turbine overspeed trip valve tripped twice. Closure of the valve rendered /
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the turbine driven auxiliary feedwater pump inoperable. Both events are re-
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portable pursuant to T.S. 6.9.1.9.b.
Two redundant full size motor driven
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auxiliary feedwater pumps were operable. The action statement of the LCO was /
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met.
The public health and safety were not affected.
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SYSTEM
CAUSE
CAUSE COMP.
VALVE CODE CODE-SUBCODE COMPONENT CODE SUBCODE SUBCODE
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SEQUENTIAL OCCURRENCE REPORT REVISION LER/R0 EVENT YEAR REPORT NO.
CODE TYPE NO.
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ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRD-4 PRIME COMP. COMPONENT TAKEN ACTION ON PLANT METHOD HOURS SUBMITTED FORM SUB. SUPPLIER MANUFACTURER LB/ (18) LA/ (19) /_Z/ (20) LZ/ (21) /0/0/0/0/ (22) LY/ (23) LN/ (24) /A_/ (25) /T/1/4/7/ (26)
CAUSE DESCRIPTION AND CORRECTIVE ACTIONS (27)
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Improper alignment of the overspeed trip device linkage parts due to wear
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caused the unexpected trips. The parts were machined to obtain proper clear- /
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ances, the overspeed trip tested, and the pump returned to service after test- /
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ing.
New parts are on order and will be installed at a later date.
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FACILITY METHOD OF STATUS
% POWER OTHER STATUS
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/( ) DISCOVERY DISCOVERY DESCRIPTION (32)
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OPERATOR OBSERVATION
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ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY (35)
LOCATION OF RELEASE (36)
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PERSONNEL EXPOSURES NUMBER TYPE
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Z PERSONNEL INJURIES NUMBER DESCRIPTION (41)
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- - LOSS OF OR DAMAGE TO FACILITY
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TYPE
DESCRIPTION
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PUBLICITY ISSUED DESCRIPTION (45)
NRC USE ONLY
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NAME OF PREPARER-W. R. CARTWRIGHT PHONE (703) 894-5151 8103170437
Virginia Electric and Power Company North Anna Power Station, Unit #2 Attachment: Page 1 of 2 Docket No. 50-339 Report No. LER 80-019/03L-0
Description of Event
On February 14, 1981, with Unit 2 at 100 percent power, the auxiliary feedwater ptap turbine overspeed trip valve tripped twice. Closure of the valve rendered the turbine auxiliary feedwater pump inoperable.
This event is reportable pursuant to T.S. 6.9.1.9.b.
Probable Consequences of Occurrence Two redundant full size motor driven auxiliary feedwater pumps were operable. The turbine driven auxiliary feedwater pump was tested and returned to operable status 18 hours2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br /> after the first event (the second event occurred 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> after the firrt event). The action statement of the LCO was met.
The public health eafety were not affected.
Cause of Event
Improper alignment of turbine overspeed trip device to trip v21ve linkage (tappet nut to head lever alignment incorrect) caused the trips.
Imptcper alignment was caused by worn parts.
Immediate Corrective Action
The first time the valve closed the overspeed trip was reset, tripped to verify that it was functional, and reset. A security check verified that no one was in the turbine driven auxiliary feedwater pump house when the trip occurred. When the valve tripped again 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and 10 minutes after the first event, the turbine driven auxiliary feedwater pump was declared. inoperable. The existing parts were machined to obtain proper linkage clearances and reinstalled. The overspeed setpoint was checked after maintenance was complete and the pump was returned to operable status after being tested in accordance with T.S. and IWP requirements.
Scheduled Corrective Action i
New parts to replace the worn linkage parts are on order and will be installed at a later date. The linkage will be checked yearly as recommended by the manufacturer.
l Actions Taken to Prevent Recurrence Since August 1980, the Unit 1 turbine driven auxiliary feedwater pump has had three overspeed trips unexpectedly and the Unit 2 turbine driven auxiliary feedwater pump has had four unexpected trips. An on going investigation is being conducted to determine actions which should be taken to prevent recurrence, if any.
On February 11, 1981, three days before the events, an investigation of the overspeed' trip device by the Safety Engineering Staff revealed the improper alignment problem. The Safety Engineering Staff documented
, their concern about - the problem and recommendations in a' memorandum to the Maintenance Department on February 11, 1981;: unfortunately, before L
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Attachment: Page 2 of 2 the Maintenance Department was able to take action the alignment problem caused the events described above.
Generic Implications An identical problem was found on the Unit 1 overspeed trip device.
' The probles is not considered generic because the manufacturer recommends checking overspeed trip device linkages and clearances once yearly for wear in their current maintenance manuals.
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| 05000339/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000339/LER-1981-001-03, /03L-0:on 810101,average RCS Temp Outside Tech Specs on Two Occasions.First Caused by Vol Control Tank Being Overborated;Second by Overcooling Primary.Steam Generator Blowdown Secured,Rods Withdrawn & RCS Diluted | /03L-0:on 810101,average RCS Temp Outside Tech Specs on Two Occasions.First Caused by Vol Control Tank Being Overborated;Second by Overcooling Primary.Steam Generator Blowdown Secured,Rods Withdrawn & RCS Diluted | | | 05000338/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000338/LER-1981-001-03, /03L:on 810318 & 19,nitrogen Supply Tank Pressure for Associated Pressure Operated Relief Valves Dropped Below Min Required to Operate Valves for Low Temp RCS Overpressurization Protection.Caused by Leaks in Tanks | /03L:on 810318 & 19,nitrogen Supply Tank Pressure for Associated Pressure Operated Relief Valves Dropped Below Min Required to Operate Valves for Low Temp RCS Overpressurization Protection.Caused by Leaks in Tanks | | | 05000338/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000338/LER-1981-002-03, /03L-0:on 801231,pressurizer Power Operated Relief Valve Declared Inoperable Because of Low Nitrogen Gas Supply Tank Pressure in 1-GN-TK-1A.Caused by Excessive Usage of Nitrogen to Cycle Relief Valves to Reduce RCS Pressure | /03L-0:on 801231,pressurizer Power Operated Relief Valve Declared Inoperable Because of Low Nitrogen Gas Supply Tank Pressure in 1-GN-TK-1A.Caused by Excessive Usage of Nitrogen to Cycle Relief Valves to Reduce RCS Pressure | | | 05000339/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000339/LER-1981-002-03, /03L-0:on 801230,w/unit in Mode 1,steam Flow Channel III Became Erratic W/O Any Annunciators or Computer Alarms.Cause Unknown.Channel Placed in Trip Condition, Calibr & Returned to Svc | /03L-0:on 801230,w/unit in Mode 1,steam Flow Channel III Became Erratic W/O Any Annunciators or Computer Alarms.Cause Unknown.Channel Placed in Trip Condition, Calibr & Returned to Svc | | | 05000338/LER-1981-003-03, /03L-0:on 810104,loop 3 Reactor Coolant Flow Protection Channel II,F-1435,found Out of Tolerance High. 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Probably Caused by Inleakage of Unknown Source.Boric Acid Transferred to Tank C.Investigation of Leak Underway | | | 05000338/LER-1981-007, Forwards Updated LER 81-007/99X-1 | Forwards Updated LER 81-007/99X-1 | | | 05000339/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000338/LER-1981-008-03, /03L-0:on 810117,steam Generator a Protection Channel 2 Narrow Range Level Transmitter LT-1475 Found Out of Calibr.Caused by Voltage Drift in Level Transmitter Serving Instrument Loop.Recalibr & Returned to Svc | /03L-0:on 810117,steam Generator a Protection Channel 2 Narrow Range Level Transmitter LT-1475 Found Out of Calibr.Caused by Voltage Drift in Level Transmitter Serving Instrument Loop.Recalibr & Returned to Svc | | | 05000338/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000339/LER-1981-008-03, /03L-0:on 810107,primary Coolant Iodine Isotopic Analysis Not Made within 2-6 Hour Per Tech Spec Re Power Changes Exceeding 15% Per Hour.Caused by Failure of Operations Personnel to Follow Procedures.Sample Analyzed | /03L-0:on 810107,primary Coolant Iodine Isotopic Analysis Not Made within 2-6 Hour Per Tech Spec Re Power Changes Exceeding 15% Per Hour.Caused by Failure of Operations Personnel to Follow Procedures.Sample Analyzed | | | 05000339/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000339/LER-1981-009-03, /03L-0:on 810107,during Leak Test Containment Personnel Hatch Outer Door Leaked Air Past Seals.Caused by Improper Fitup of Door Seals to Frame.Door Adjusted | /03L-0:on 810107,during Leak Test Containment Personnel Hatch Outer Door Leaked Air Past Seals.Caused by Improper Fitup of Door Seals to Frame.Door Adjusted | | | 05000338/LER-1981-009-03, Combined Leakage in Excess of Allowable Limits Noted from 14 Electrical Penetrations & 23 Valves.Valve Leakage Caused by Valve Seat Deterioration or Limit Switch Drift | Combined Leakage in Excess of Allowable Limits Noted from 14 Electrical Penetrations & 23 Valves.Valve Leakage Caused by Valve Seat Deterioration or Limit Switch Drift | | | 05000338/LER-1981-009, Forwards Updated LER 81-009/03X-1 | Forwards Updated LER 81-009/03X-1 | | | 05000338/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000338/LER-1981-010-03, /03L-0:on 810211,w/unit in Mode 6,containment Purge & Exhaust Isolation Sys Was Rendered Inoperable When Power to MOV-HV-100B,D Was Lost.Caused by Fault on High Resistance Connection.Defective Parts Replaced | /03L-0:on 810211,w/unit in Mode 6,containment Purge & Exhaust Isolation Sys Was Rendered Inoperable When Power to MOV-HV-100B,D Was Lost.Caused by Fault on High Resistance Connection.Defective Parts Replaced | | | 05000339/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000339/LER-1981-010-03, /03L-0:on 810113,w/unit at 100% Power,Overspeed Trip of Turbine Driven Auxiliary Feedwater Pump Occurred During Surveillance Testing.Caused by Failure of Turbine Governor to Control Speed.Governor Was Replaced | /03L-0:on 810113,w/unit at 100% Power,Overspeed Trip of Turbine Driven Auxiliary Feedwater Pump Occurred During Surveillance Testing.Caused by Failure of Turbine Governor to Control Speed.Governor Was Replaced | | | 05000338/LER-1981-011-03, /03L-0:on 810117,w/unit in Mode 6,loss of Power to Radiation Monitor Common Alarms Panel Was Experienced for Less than 5 Minutes.Caused by Failure of Electrician to Switch Power to Unit 2 During Unit 1 Trip | /03L-0:on 810117,w/unit in Mode 6,loss of Power to Radiation Monitor Common Alarms Panel Was Experienced for Less than 5 Minutes.Caused by Failure of Electrician to Switch Power to Unit 2 During Unit 1 Trip | | | 05000338/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000339/LER-1981-011-03, /03L-0:on 810114,w/unit at 100% Power,Breaker for 2-QS-P-1A Spray Pump Racked Out & Suction Valve MOV-QS-200A Closed & de-energized.Caused by Dirty Seat on Vent Valve. 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Valve Seat Cleaned & Disc Lapped | | | 05000339/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000338/LER-1981-012-03, /03L-0:on 810118,fuel Bldg Supply & Exhaust Fan Suction Dampers Switched to Failed Position,Bypassing Iodine Filter Bank When Control Bank Was Isolated.Caused by Low Outdoor Temp.Dampers Positioned to Exhaust Through Filter | /03L-0:on 810118,fuel Bldg Supply & Exhaust Fan Suction Dampers Switched to Failed Position,Bypassing Iodine Filter Bank When Control Bank Was Isolated.Caused by Low Outdoor Temp.Dampers Positioned to Exhaust Through Filter | | | 05000338/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000339/LER-1981-012-03, /03L-0:on 810121,containment Pressure Protection Channel 3 Failed Low.Caused by Blown Transistor on Loop Power Supply Card,Resulting in Power Loss to Each Comparator in Loop.Failed Card Replaced W/Calibr Card | /03L-0:on 810121,containment Pressure Protection Channel 3 Failed Low.Caused by Blown Transistor on Loop Power Supply Card,Resulting in Power Loss to Each Comparator in Loop.Failed Card Replaced W/Calibr Card | | | 05000339/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000339/LER-1981-013-03, /03L-0:on 810126,containment Hi & hi-hi Pressure Channel III Annunciator Energized.Caused by Instrument Drift in Nonisolated Power Supply Card S/N 5088,increasing Output Voltage.Card Replaced & Channel Calibr | /03L-0:on 810126,containment Hi & hi-hi Pressure Channel III Annunciator Energized.Caused by Instrument Drift in Nonisolated Power Supply Card S/N 5088,increasing Output Voltage.Card Replaced & Channel Calibr | | | 05000338/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000339/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | |
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