ML19345B797

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LER 80-001/01T-0:on 801112,water for Lubrication & Cooling of a Train Svc Water Pumps Found to Be Provided by B Train Svc Water Header & Vice Versa.Caused by Design Error.Design Change to Provide Correct Separation Completed
ML19345B797
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 11/26/1980
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19345B792 List:
References
LER-80-001-01T, LER-80-1-1T, NUDOCS 8012020519
Download: ML19345B797 (1)


Text

U.S. NUCLEA ] RE;ULATL RY COMMISSION NRC FORM 366 (1 718 LICENSEE EVENT REPORT 80NTROL BLOCX:l l 1

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i 8 60 61 OCKET NUvega EVENT 0 ATE EVENT OESCRIPTION AND PRO 3 a ELE CONSEQUENCES h l o t a l l As a result of main:enance activities on the Service Water (SW) Lube and Cooling l t o l 3 I 1 System on 11/12/80, it was determined that the water for lubrication and cooling of I l o l .i l l A Train SW pu=ps was provided by the B Train SW header and the B Train SW pumps b, I l_o i s ] l the A Train SW header. This inadequate train seperation results in the potential forI lo is l l a failure in one train to adversely affect the second train during a Loss of Off-Site l Iol7ll Power with various accident conditions. This condition was reported on 11/13/80 in I l o l a l I accordance with Tech. Spec.6.9.1.12.1.~~ Initial fuel loading on Unit 2 has not co=menceti. 80 SYSTEM C USE CAUSE COMP. VALVE CODE 0;;E SUSCODE COMPONENT CODE SUSCCOE SUSCODR loisi IW I A l@ l 3l@ l C l@ l Z l 2 l 2 l Z l Z l Z l@ [Z_J@ 20[Zj @

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