ML19345B470

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LER 80-065/03L-0:on 801022,total Controlled Leakage During Reactor Coolant Pump Seal Controlled Leakage test,FNP-1-STP- 8.0,exceeded Tech Spec Limit.Caused by Failure to Verify Total Flow After Adjustment.Operating Procedure Changed
ML19345B470
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 11/24/1980
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19345B451 List:
References
LER-80-065-03L, LER-80-65-3L, NUDOCS 8012010367
Download: ML19345B470 (1)


Text

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I 5 60 twB 74 75 DATE NUMBER EVENT OESCRIPTION AND PROSASLE CONSEQUENCES h 10 I a I l At 1540 on 10-22-80, during the performance of FNP-1-STP-8.0 (RCP Seal Controlled I f o l3l l Leakage Test) it was determined that the total controlled leakage (36 com) exceeded j I o I 4 I l Tech. Spec. 3.4.6.2.e requirements (31 gpm maxi =um allowable) . The leakaee was I l o i 5 I l returned to Tech. Spec.1.imits at 1625 on 10-22-80. Health / Safety of the public l Iolel l were not affected by this occurrence. _

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