LER-1980-149, /03L-0:on 800807,during Preoperational Tests, Turbine Driven Feedwater Pump Failed to Maintain Rated Rpm. Caused by Overheated Automatic Governor.Ventilation Damper Linkage Repaired & Governor Controls Replaced |
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| 3271980149R03 - NRC Website |
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Tennessee Valley Authority Sequoyah Nuclear Plant 1.Elt SUFFLEMENTAL INFORMATION
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SQRO-50-327-/80149 Technical Specification Involved:
3.7.1.2 Reported Under Technical Specification: 6.9.1.&3.b Date of Occurrence: August 7, 1980 Time of Occurrence: 0905 EDT August 8, 1980 Time of Occurrence: 2130 EDT Identification and Description of Occurrence:
On August 7, 1980, at 0905 EDT, prior to performing the 48 hour5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> endurance run (preoperational test) a simulated safety injection signal to the auxil-iary feed water pumps was initiated. The turbine driven pump came up to rated rpm and pressure then in approximately 20 seconds fell to 2900 rpm at 850 psig discharge pressure. The pump was declared inoperable and action stater.ent 3.7.1.2 of the tech specs was entered.
The babsequent investigation could not duplicate the original problem but it was found that the auxiliary feedwater flow indicating controller, 1-FIC-46-57, was not operating correctly. This component was replaced realizing that it was not the cause of the problem. Since the problem could not be identified, the pump was returned to service and the preoperation-al test continued. Investigation of the problem continued.
On August 8, 1980, at 2130 EDT, during preoperational testing of the turbine driven auxiliary feedwater pump, the turbine reduced speed causing the pump output to fall below rated flow. The pump had been at rated flow for approximately 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br />. The pump was declared inoperable and action state-ment 3.7.1.2 of the tech specs was entered.
Investigation indicates that the turbine speed governor components are over heating. When the cover to the cabinet, which houses the electronic governor components, was opened and the components allowed to cool, for about 30 minutes, the speed increased and automatic control was reestablished. The pump then operated at full flow for the next 28 consecutive hours.
Conditions Prior to occurrence:
Mode 2, power at approximately 1.5%, RCS at 545 degrees F and 2235 psig Action specified in the Technical Specification Surveillance Requitecents met due to inoperable equipment.
3.7.1.2 states that the pump must be operable within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in Mode 3 within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. The automatic governor components were cooled and automatic speed control was maintained within 30 minutes.
Apparent Cause of Occurrence:
The turbine speed governor components were apparently overheating and as a result failed to maintain proper control of the turbine speed.
N
. Sequoyah Nuclear Plant i
LER Supplemental Information Analysis of Occurrence:
One ventilation damper to the auxiliary feedvater pump (turbine driven) room was found closed with broken linkage which caused deficient cooling. Also a length of insulation was found missing from the piping to the steam traps in this room. Governor electronic components were located in a non-ventilated panel adjacent to the turbine skid. During the 30 minuta loss of automatic control, manual control was available.
Corre tive Action:
The ventilation damper linkage was repaired and missing piping insulation was replaced. To provide additional assurance, the electronic governor controls were replaced and are now relocated in a cooler area with a vented panel to allow natural circulation of air.
Future retesting will be performed to evaluate operability of electronic components of the turbine speed governor in the new location.
The electronic components of the turbine speed governor will be returned to tie vendor for failure analysis. The resulta vill be evaluated to determine future reportability, and the need for any future modifications.
Failure Data:
None
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| 05000327/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000327/LER-1980-001-01, /01T-0:on 800301-03,during Initial Fuel Loading, Licensee Failed to Estimate Flowrate from Svc Bldg Exhaust at 4-h Intervals.Caused by Misunderstanding of Tech Spec Requirements.Plant Instructions Revised | /01T-0:on 800301-03,during Initial Fuel Loading, Licensee Failed to Estimate Flowrate from Svc Bldg Exhaust at 4-h Intervals.Caused by Misunderstanding of Tech Spec Requirements.Plant Instructions Revised | | | 05000327/LER-1980-002, Forwards LER 80-002/01T-0 | Forwards LER 80-002/01T-0 | | | 05000327/LER-1980-002-01, /01T-0:on 800306,contents of Task Decontamination Collector Tank Discharged Via Liquid Radwaste Effluent Line to Cooling Tower Blowdown W/O Flow Estimates Being Performed.Caused by Misunderstanding of Tech Specs | /01T-0:on 800306,contents of Task Decontamination Collector Tank Discharged Via Liquid Radwaste Effluent Line to Cooling Tower Blowdown W/O Flow Estimates Being Performed.Caused by Misunderstanding of Tech Specs | | | 05000327/LER-1980-003-01, /01T-0:on 800310,following Initial Fuel Loading, Flow Through Auxiliary Bldg Exhaust Sampler Not Maintained for 3.25-h.Caused by Misunderstanding of Tech Specs. Personnel Reinstructed in Applicable Requirements | /01T-0:on 800310,following Initial Fuel Loading, Flow Through Auxiliary Bldg Exhaust Sampler Not Maintained for 3.25-h.Caused by Misunderstanding of Tech Specs. Personnel Reinstructed in Applicable Requirements | | | 05000327/LER-1980-003, Forwards LER 80-003/01T-0 | Forwards LER 80-003/01T-0 | | | 05000327/LER-1980-004, Forwards LER 80-004/01T-0 | Forwards LER 80-004/01T-0 | | | 05000327/LER-1980-004-01, /01T-0:on 800311,following Initial Fuel Loading, Flow Estimates for Auxiliary Bldg Vent Monitor Not Performed for 10-h.Caused by Misunderstanding of Tech Specs.Personnel Reinstructed Re Applicable Requirements | /01T-0:on 800311,following Initial Fuel Loading, Flow Estimates for Auxiliary Bldg Vent Monitor Not Performed for 10-h.Caused by Misunderstanding of Tech Specs.Personnel Reinstructed Re Applicable Requirements | | | 05000327/LER-1980-005-03, /03L-0:on 800311,while Performing SI-247.605, Reactor Solid State Protection Sys Was Placed in Input Inhibit Mode,Removing High Voltage from Source Range Channel N31.Caused by Removal of Fuses from Voltage Cut Out Relay | /03L-0:on 800311,while Performing SI-247.605, Reactor Solid State Protection Sys Was Placed in Input Inhibit Mode,Removing High Voltage from Source Range Channel N31.Caused by Removal of Fuses from Voltage Cut Out Relay | | | 05000327/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000327/LER-1980-006-01, /01T-0:on 800314,w/essential Raw Cooling Water Radiation Monitors on Train a Inoperable,Personnel Determined That Limiting Condition of Operation Requires Sampling.Caused by Misinterpretation of Tech Specs | /01T-0:on 800314,w/essential Raw Cooling Water Radiation Monitors on Train a Inoperable,Personnel Determined That Limiting Condition of Operation Requires Sampling.Caused by Misinterpretation of Tech Specs | | | 05000327/LER-1980-006, Forwards LER 80-006/01T-0 | Forwards LER 80-006/01T-0 | | | 05000327/LER-1980-007-01, /01T-0:on 800315,following Initial Core Loading, Found Incorrect (Nonconservative) Valve Operator Weights Used in Seismic Analysis for Component Cooling Water Valves FCV-70-133,134 & 183.Caused by Incorrect Vendor Data | /01T-0:on 800315,following Initial Core Loading, Found Incorrect (Nonconservative) Valve Operator Weights Used in Seismic Analysis for Component Cooling Water Valves FCV-70-133,134 & 183.Caused by Incorrect Vendor Data | | | 05000327/LER-1980-007, Forwards LER 80-007/01T-0 | Forwards LER 80-007/01T-0 | | | 05000327/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000327/LER-1980-008-03, /03L-0:on 800303,cooling Tower Blowdown Effluent Line Flow Monitor O-FR-27-175 Was Declared Inoperable.Flow Monitor Consistently Indicated Higher Flowrate than Actually Existed.Cause Unknown.Different Instrument to Be Instal | /03L-0:on 800303,cooling Tower Blowdown Effluent Line Flow Monitor O-FR-27-175 Was Declared Inoperable.Flow Monitor Consistently Indicated Higher Flowrate than Actually Existed.Cause Unknown.Different Instrument to Be Installed | | | 05000327/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000327/LER-1980-009-03, /03L-0:on 800303,liquid Radwaste Effluent Line Flow Monitor 0-FT-77-42 Consistently Indicated Higher Discharge Flow Rate than Actually Observed.Cause Not Stated.Flow Monitor Modified & Returned to Svc | /03L-0:on 800303,liquid Radwaste Effluent Line Flow Monitor 0-FT-77-42 Consistently Indicated Higher Discharge Flow Rate than Actually Observed.Cause Not Stated.Flow Monitor Modified & Returned to Svc | | | 05000327/LER-1980-010-03, /03L-0:on 800304,gaseous Vent Flow Rate Monitors for Units 1 & 2 Shield Bldgs & Auxiliary Bldg Were Declared Inoperable.Cause Not Stated.Gaseous Flow Rate Monitors to Be Redesigned | /03L-0:on 800304,gaseous Vent Flow Rate Monitors for Units 1 & 2 Shield Bldgs & Auxiliary Bldg Were Declared Inoperable.Cause Not Stated.Gaseous Flow Rate Monitors to Be Redesigned | | | 05000327/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000327/LER-1980-011, Forwards LER 80-011/01T-0 | Forwards LER 80-011/01T-0 | | | 05000327/LER-1980-011-01, /01T-0:on 800314,support Pin Insp at Foreign Plant Revealed Stress Corrosion Cracking in Westinghouse Supplied Pins.Insp Supported Westinghouse Ltr Informing Utils of Potential Hazard.Pins Will Be Replaced | /01T-0:on 800314,support Pin Insp at Foreign Plant Revealed Stress Corrosion Cracking in Westinghouse Supplied Pins.Insp Supported Westinghouse Ltr Informing Utils of Potential Hazard.Pins Will Be Replaced | | | 05000327/LER-1980-012-03, /03L-0:on 800301,during Initial Core Loading,Rhr Flow Secured or Throttled Above Tech Specs.Caused by Intentional Increase to Allow Placement of Fuel Assemblies Near Loop 4 Hot Leg | /03L-0:on 800301,during Initial Core Loading,Rhr Flow Secured or Throttled Above Tech Specs.Caused by Intentional Increase to Allow Placement of Fuel Assemblies Near Loop 4 Hot Leg | | | 05000327/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000327/LER-1980-013-03, /03L-0:on 800302,failed to Analyze Samples from Unit 2 Shield Bldg Exhaust.Caused by Misunderstanding of Surveillance Requirements.Lab Personnel Instructed on Sampling & Analysis Requirements | /03L-0:on 800302,failed to Analyze Samples from Unit 2 Shield Bldg Exhaust.Caused by Misunderstanding of Surveillance Requirements.Lab Personnel Instructed on Sampling & Analysis Requirements | | | 05000327/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000327/LER-1980-014, Forwards LER 80-014/03L-0 | Forwards LER 80-014/03L-0 | | | 05000327/LER-1980-014-03, /03L-0:on 800328,while Performing Check Source Test,Auxiliary Bldg Vent Noble Gas Monitor Had Module Power Problem & Failed in Svc.Caused by Zener Diode IN4740 & Transistor Fmps A13 Shorting Out | /03L-0:on 800328,while Performing Check Source Test,Auxiliary Bldg Vent Noble Gas Monitor Had Module Power Problem & Failed in Svc.Caused by Zener Diode IN4740 & Transistor Fmps A13 Shorting Out | | | 05000327/LER-1980-015-03, /03L-0:on 800305,while in Mode 6 W/Fuel Loading Complete,Pressure Was Only Being Monitored in One Steam Generator & Reactor Pressure Vessel.Caused by Misunderstanding of Surveillance Instruction | /03L-0:on 800305,while in Mode 6 W/Fuel Loading Complete,Pressure Was Only Being Monitored in One Steam Generator & Reactor Pressure Vessel.Caused by Misunderstanding of Surveillance Instruction | | | 05000327/LER-1980-015, Forwards LER 80-015/03L-0 | Forwards LER 80-015/03L-0 | | | 05000327/LER-1980-016, Forwards LER 80-016/03L-0 | Forwards LER 80-016/03L-0 | | | 05000327/LER-1980-016-03, /03L-0:on 800307,at Completion of Fuel Loading & W/Core Alterations Still underway,SI-65 Was Not Performed. Caused by Misinterpretation of Tech Specs by Personnel.No Corrective Actions Necessary | /03L-0:on 800307,at Completion of Fuel Loading & W/Core Alterations Still underway,SI-65 Was Not Performed. Caused by Misinterpretation of Tech Specs by Personnel.No Corrective Actions Necessary | | | 05000327/LER-1980-017-03, /03L-0:on 800310,while in Mode 6,turbine Bldg Sump Monitor O-RM-90-212 Alarm Kept Coming In.Monitor Was Declared Inoperable.Caused by Malfunctioning Flow Switch Not Allowing Sufficient Flow Through Monitor | /03L-0:on 800310,while in Mode 6,turbine Bldg Sump Monitor O-RM-90-212 Alarm Kept Coming In.Monitor Was Declared Inoperable.Caused by Malfunctioning Flow Switch Not Allowing Sufficient Flow Through Monitor | | | 05000327/LER-1980-017, Forwards LER 80-017/03L-0 | Forwards LER 80-017/03L-0 | | | 05000327/LER-1980-018-01, /01T-0:on 800326,while in Mode 6 W/All Fuel Loaded,Exposed Cables Inside Containment Between Conduit & Penetrations Not Qualified to re-evaluated post-LOCA Max Dose Levels.Cables Shielded from Exposure to New Dose Level | /01T-0:on 800326,while in Mode 6 W/All Fuel Loaded,Exposed Cables Inside Containment Between Conduit & Penetrations Not Qualified to re-evaluated post-LOCA Max Dose Levels.Cables Shielded from Exposure to New Dose Level | | | 05000327/LER-1980-018, Forwards LER 80-018/01T-0 | Forwards LER 80-018/01T-0 | | | 05000327/LER-1980-019, Forwards LER 80-019/01T-0 | Forwards LER 80-019/01T-0 | | | 05000327/LER-1980-019-01, /01T-0:on 800326,found Possibility of Not Maintaining Control Room Habitability Due to Leakage of Unfiltered Air.Possibly Caused by Isolation Dampers. Corrective Mods Planned | /01T-0:on 800326,found Possibility of Not Maintaining Control Room Habitability Due to Leakage of Unfiltered Air.Possibly Caused by Isolation Dampers. Corrective Mods Planned | | | 05000327/LER-1980-020, Forwards LER 80-020/01T-0 | Forwards LER 80-020/01T-0 | | | 05000327/LER-1980-020-01, /01T-0:on 800404,investigation Revealed That Several vendor-designed Pipe Supports Were Designed Utilizing Manufacturer Std 0.25-inch U-bolt Which Overstressed During Seismic Event.Caused by Design Error | /01T-0:on 800404,investigation Revealed That Several vendor-designed Pipe Supports Were Designed Utilizing Manufacturer Std 0.25-inch U-bolt Which Overstressed During Seismic Event.Caused by Design Error | | | 05000327/LER-1980-021-03, /03L-0:on 800308,while in Mode 6,flow Rates from Auxiliary Bldg Ventilation Sys Flow Rate Monitor Were Not Recorded for Three Shifts.Caused by Misreading of Notation Used in Surveillance Instruction.Temporary Change Issued | /03L-0:on 800308,while in Mode 6,flow Rates from Auxiliary Bldg Ventilation Sys Flow Rate Monitor Were Not Recorded for Three Shifts.Caused by Misreading of Notation Used in Surveillance Instruction.Temporary Change Issued | | | 05000327/LER-1980-021, Forwards LER 80-021/03L-0 | Forwards LER 80-021/03L-0 | | | 05000327/LER-1980-022-03, /03X-2:on 800318,sample Isolation Valves 1-FCV-90-108,109,110,114,115 & 116 Closed,Isolating Radiation Monitors.Caused by Isolation of Nonessential Control Air to Sample Valves.Valves Reopened | /03X-2:on 800318,sample Isolation Valves 1-FCV-90-108,109,110,114,115 & 116 Closed,Isolating Radiation Monitors.Caused by Isolation of Nonessential Control Air to Sample Valves.Valves Reopened | | | 05000327/LER-1980-022, Forwards LER 80-022/03L-0 | Forwards LER 80-022/03L-0 | | | 05000327/LER-1980-023, Forwards LER 80-023/03L-0 | Forwards LER 80-023/03L-0 | | | 05000327/LER-1980-023-03, /03L-0:on 800402,during Surveillance Testing, Diesel Generator 2A-A Feedbreaker Failed to Close.Caused by Power Contacts Being Dirty.Power Contacts Cleaned | /03L-0:on 800402,during Surveillance Testing, Diesel Generator 2A-A Feedbreaker Failed to Close.Caused by Power Contacts Being Dirty.Power Contacts Cleaned | | | 05000327/LER-1980-024, Forwards LER 80-024/03L-0 | Forwards LER 80-024/03L-0 | | | 05000327/LER-1980-024-03, /03L-0:on 800331,flow Switches on Radiation Monitors ORM-90-212 & 122 Found Inoperable.Caused by Small Particulate Matter in Monitored Liquid.Design Change Request Initiated.Weekly Preventive Maint Program Established | /03L-0:on 800331,flow Switches on Radiation Monitors ORM-90-212 & 122 Found Inoperable.Caused by Small Particulate Matter in Monitored Liquid.Design Change Request Initiated.Weekly Preventive Maint Program Established | | | 05000327/LER-1980-025, Forwards LER 80-025/03L-0 | Forwards LER 80-025/03L-0 | | | 05000327/LER-1980-025-03, /03L-0:on 800313 W/Unit 1 in Mode 6,O-RM-90-225 Condensate Demineralizer Effluent Line Was Taken Out of Svc for Maint.Caused by Weak Transistor.Transistor Replaced & Monitor Returned to Svc | /03L-0:on 800313 W/Unit 1 in Mode 6,O-RM-90-225 Condensate Demineralizer Effluent Line Was Taken Out of Svc for Maint.Caused by Weak Transistor.Transistor Replaced & Monitor Returned to Svc | |
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