LER-1981-011, /01T-1:on 810306,containment Isolation Valves CAV-1,3,4,5 & 126 Found Incapable of Meeting Environ Qualification During Evaluation of IE Bulletin 79-01B.Caused by Potential Electrical Short Due to Flooding After LOCA |
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SUPPLEMENTARY INFORMATION
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Report No.:
50-302/81-Oll/0lT-1 Facility:
Crystal River Unit 3 Report Date:
11 arch 20,1981 Occurrence Date:
March 6, 1981 Identification of Occurrence:
Containment isolation valves CAV-1, 3, 4, 5, and 126 are not capable of meeting the environmental qualifications of I. E.
Bulletin 79-01B due to submergence following a Loss of Coolant Accident (LOCA).
Conditions Prior to Occurrence:
Mode 1 power operations (46%).
Description of Occurrence:
At 1630 during evaluation of I. E. Bulletin 79-01B, it was discovered through conversations with the vendor and through engineering analysis, that ' containment isolation valves CAV-1, 3, 4, 5, and 126 would not meet the environmental qualification requirements due to submergence following a LOCA.
Designation of Apparent Cause:
The cause is attributed to potential electrical short due to flooding in the Reactor Containment following a LOCA.
Analysis of Occurrence:
There was no effect upon the health or safety of the general public. Containment isolation valves CAV-2, 6, and 7 provide redundant isolation capability.
Corrective Action
Emergency Procedure EP-106 is being revised to instruct an operator to close and de-energize the subject valves in event of a LOCA.
In the interim, a Short Term Instruction has been issued which maintains these valves closed and de-energized ex-cept when needed for sampling. An engineering evaluation is in progress to resolve this potential problem.
Failure Data:
This is the first occurrence or event of this type and the first event reported under I. E. Bulletin 79-01B.
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