05000336/LER-1980-030-03, /03L-0:on 800812,during Routine Operation, Containment Air Temp Exceeded 120 F.Caused by Svc Water Temp Control Valve to Reactor Bldg Closed Cooling Water Heat Exchangers Being Set Too High.Valve Readjusted

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/03L-0:on 800812,during Routine Operation, Containment Air Temp Exceeded 120 F.Caused by Svc Water Temp Control Valve to Reactor Bldg Closed Cooling Water Heat Exchangers Being Set Too High.Valve Readjusted
ML19343A226
Person / Time
Site: Millstone 
Issue date: 09/08/1980
From: Harris J
NORTHEAST NUCLEAR ENERGY CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19343A219 List:
References
LER-80-030-03L, LER-80-30-3L, NUDOCS 8009160469
Download: ML19343A226 (1)


LER-1980-030, /03L-0:on 800812,during Routine Operation, Containment Air Temp Exceeded 120 F.Caused by Svc Water Temp Control Valve to Reactor Bldg Closed Cooling Water Heat Exchangers Being Set Too High.Valve Readjusted
Event date:
Report date:
3361980030R03 - NRC Website

text

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l0lt1 7-8 60 61 DOCK ET NUM8 ER 68 69 EV ENT O ATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND pro 8ASLE CONSEQUENCES h Ioi2l l During routine power operation the containment air temperature was found to be in excess l -

i o l a 1 l of the limit of 120*F as specified by Tech. S'pec. 3.6.1.5.

The service water temper-

.l l o 14 l l ature control valve to Reactor Building Closed Cooling Water (RBCCW) heat exchangers wasl loIsl I found to be set too hich.

The temoerature control valve required adjustments to lower i lolsI! containment temoerature to less than 120*F within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. Maximum temoerature was I o l 7 I i 120.4 degrees.

Similar events

LER 80-03, 78-31.

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.7 li l o l l Plant conditions criar to refueling resulted in increased heat load on RBCCW with I

t i t i i i resultant decrease in coolino availability to containment.

The temoerature control I

li 121 I valve was readjusted and normal containment temoeratures restored.

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ISSUE CE CRIPTION

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