ML19343A224

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LER 80-029/03L-0:on 800812,during Surveillance Test on 12 U diesel,125 Vdc Ground Alarm Received.Caused by Frayed Insulation on Wire in Bendix Connector Allowing Contact Between Bare Wire & Connector Shell.Wire Recovered
ML19343A224
Person / Time
Site: Millstone Dominion icon.png
Issue date: 09/08/1980
From: Harris J
NORTHEAST NUCLEAR ENERGY CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19343A219 List:
References
LER-80-029-03L, LER-80-29-3L, NUDOCS 8009160464
Download: ML19343A224 (1)


Text

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7 8 60 61 CCCKET NUMB ER EVENT DESCRIPTION AND PROB AB'.E CONSEQUENCES h 1o 121 lWhile the 120 diesel was being run for surveillance testing, a 125 VDC (Bus 201A) ground]

I o ! a l l alarm was received. The 13U diesel was verified operable and the plant was operated in l 1 o 141 Laccordance with the Action Statement 3.8.1.1.a of Technical Soecifications. The ground I i o i s i lwas corrected and the 12U diesel returned to operable status within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. l l

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4A l of 1101@47 CAUSE CESCRIPTION AND CCRRECTIVE ACTICNS l i l o l l The cause of the ground was frayed insulation on one wire in the Bendix connector wnichi It li j l connects the sceed sensor to the governor allowing a bare wire to contact the connectori li#2l l shell causing a short circuit. The connector leads were removed, cut back,stricoed, 1 IiI3l l reconnected and covered with heat shrink tubino. I t i la t I l 7 8 9 80 ST *.PCwER CTHER STATUS blS C RY DISCCVERY DESCAIPTION Ii 15 I l E l@ l 1 l 0 l 0 l@l NA l [.Bj@l Surveillance Test l ACTIVITY CCNTENT RELEASE CF mELE ASE A ' CUNT CF ACTIVITY LCCATICN OF RELEASE It lsl[y @D l zl@l NA l l NA [

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BOSTON EDISON COMPANY PILGRIM NUCLEAR POWER STATION DOCKET No. 50-293 Attachment to LER 80-049/03L-0 Description On August 10 and 11, 1980 SSW P208B tripped. On August 11 and 17, 1980 SSW P208E tripped. On each occasion the trips resulted from thermal overload of their respective breaker's B1533 and B1444. I= mediate investigation revealed no cause for these trips. A detailed analysis was initiated to ascertain the cause of the trips and recommend corrective action.

Cause & Corrective Action The analysis indicates that the major conditions contributing to these trips are:

1. An improvement in the SSW inlet water flow due to maintenance performed during the refuel IV outage.
2. A reduction in heat transfer capability of the THCCW system in non essential loops.
3. The number of SSW pumps in operation.
4. The inlet water level to the SSW pumps.
5. The inlet water temperature to the SSW pumps.

It is believed at this time that simultaneous operation of four SSW pumps with specific inlet water levels shifted the dynamic operating characteristic of B & E SSW pumps and resulted in protective trips of their respective breaker.

Permanent corrective action is being contemplated ; meanwhile , inlet water temperature decrease has alleviated the problem.

Emergency mode of operation requires two pump operation and therefore the safety margin, in this mode has not been reduced.

Following the completion of the analysis and implementation of permanent corrective measures an update report will be issued.

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