05000336/LER-1980-028-03, /03L-0:on 800811,at 100% Power,Control Element Assembly 41 Dropped from 180 to Zero Steps.Caused by Faulty Jumper Cable from Refuel Disconnect Panel to Reactor Head. Power Reduced & Assembly Realigned.Replacement Planned

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/03L-0:on 800811,at 100% Power,Control Element Assembly 41 Dropped from 180 to Zero Steps.Caused by Faulty Jumper Cable from Refuel Disconnect Panel to Reactor Head. Power Reduced & Assembly Realigned.Replacement Planned
ML19343A223
Person / Time
Site: Millstone 
Issue date: 09/08/1980
From: Harris J
NORTHEAST NUCLEAR ENERGY CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19343A219 List:
References
LER-80-028-03L, LER-80-28-3L, NUDOCS 8009160461
Download: ML19343A223 (1)


LER-1980-028, /03L-0:on 800811,at 100% Power,Control Element Assembly 41 Dropped from 180 to Zero Steps.Caused by Faulty Jumper Cable from Refuel Disconnect Panel to Reactor Head. Power Reduced & Assembly Realigned.Replacement Planned
Event date:
Report date:
3361980028R03 - NRC Website

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LICENSE 5 EVENT REPORT CONT 3ol stock: 1 I

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l l lh (PLEASE PRINT On TYPE ALL REQUIRED INFoRMATION) 1-6 foTi'l l CIT I M I N I s i 2 l@l 01 01-1 01010101 - l 01010 l@l 411 11 11 11 l@l l

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7 8 9 LICENSEE CODE le 15 LICENSE NUMBER 25 26 LICENSE TYPE JQ 57 CAT 58

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60 61 DOCKET NUMBER 68 69 EVENT 0 ATE 74 75 REPORT OATE 80 EVENT oESCRIPTioN AND PROB ABLE CONSEQUENCES h 21 I During steady-state 100% power operation, CEA No. 41 dropped to zero steps from 180 l

1o:

This resulted in operation in Action ' Statements 3.1.3.1.e (CEA misalignment)

I [Trr1 l steps.

l o 141 13.2.4 (Tilt-greater than.02).

Power was reduced and CEA No. ai realicned with Group 7 I t o lsl lwithin i hour.

Following recovery of CEA No. 41 and with power at 70%, CEA No. 65 1

lo is 1 I dropped and was realigned with Group 7 within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.

Tilt was within specification f

lo l7l l within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.

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10 11 12 13 18 19 20 SEQUENTIAL CCCURRENCE REPCRT REVis3ON gqfRo SVENT YEAR R EPORT NO.

CODE TYPE N O.

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J4 35 36 37 40 41 42 43 44 47 33 CAUSE CEsCRIPTION AND CORRECTIVE ACTIONS h li t o l l The accarent cause of the CEA's to droo was a faulty jumper cable from the refuel l

iili; l disconnect panel to the reactor head.

No parts were replaced. A new head cabling I

i system and checkout of all reed switches is planned for the 1980 refuel outaCe.

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