05000348/LER-1980-079-03, /03L-0:on 801108,main Steam Safety Valve 01N11V010B Failed to Meet Tech Spec Lift Setting Requirements.Caused by Setpoint Drift.Valve Adjusted

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/03L-0:on 801108,main Steam Safety Valve 01N11V010B Failed to Meet Tech Spec Lift Setting Requirements.Caused by Setpoint Drift.Valve Adjusted
ML19341A829
Person / Time
Site: Farley 
Issue date: 01/23/1981
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19341A827 List:
References
LER-80-079-03L, LER-80-79-3L, NUDOCS 8101280295
Download: ML19341A829 (1)


LER-1980-079, /03L-0:on 801108,main Steam Safety Valve 01N11V010B Failed to Meet Tech Spec Lift Setting Requirements.Caused by Setpoint Drift.Valve Adjusted
Event date:
Report date:
3481980079R03 - NRC Website

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LICENSEE EVENT REPORT wNTaot stoCx:

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60 61 00Cx ET NVMa E R 68 63 EVENT D ATE 74 79 REPGRT3 ATE 50 EVENT DESCRIPTION AND PROBABLE CCNSECUENCES h Io l2I I On 11/08/80 durine the eerformnee of FNP-1-STP-608.0 (Main Sem I.ine *lrferv Valve l

l ITTil l Test) main steam safetv valve 01N11v010B failed to meet the Tech. Soee.17.1.1 life I

h I setting requirements (1101 PSIG actual vs 1088 PSIG + 1% required). Uom discovery of I l o ! s 1 I the out of soec. condition the valve was immediate1v adinsted and retur:ad to service. I i

foTal l Health / safety of the public were not af fected.

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CO I SL C E COMPONENT CODE SLBCCDE 5

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10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE R EPCRT REV154CN L

EVENT YEAR REPORT NO.

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- s 33 34 25 34 37 40 41 42 43 as 4y CAUSE DESCRIPTION AND CCARECTIVE ACTICNS M y i This incident is attributable to setooint drift. The late submittal of this LER is duel m I to a procedural inadequacy which failed to adequately specify ic=ediate wification of t
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This lack of notif5sation was l

I 13l l discovered by a OA audit on 12/30/80. A revision will be made to the strueillance l

g 1 procedure to clearly identify notification requirements.

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NAME OP PREPARER W.

G. Hairston, III PHONE:(2053899-II%

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