ML19340A603

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Insp Rept 50-010/73-02 & 50-249/73-03 on 730417,19,20,23-25. Noncompliance Noted:Failure to Comply W/Tech Specs Surveillance Testing,Reporting & Operating Requirements
ML19340A603
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 05/24/1973
From: Charles Brown, Dance H, Maura F
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML19340A601 List:
References
50-010-73-02, 50-10-73-2, 50-249-73-03, 50-249-73-3, NUDOCS 8008280655
Download: ML19340A603 (24)


See also: IR 05000010/1973002

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U. S. ATOMIC ENERGY COMMISSION

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DIRECTORATE OF REGULATORY OPERATIONS

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REGION III

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RO Inspection Report No. 050-010/73-02

RO Inspection Report No. 050-249/73-03

Licensee: Commonwealth Edison Company

P. O. Box 767

Chicago Illinois

60690

Dresden Nuclear Power Station

Licenses No. DPR-2

Units 1 and 3

and No. DPR-25

Morris, Illinois

Category: C

Type of Licensee:

GE, BWR 210 and 809 Mwe

Type of Inspection:

Routine, Unannounced

Dates of Inspection:

April 17, 19, 20, 23-25, 1973

Dates of Previous Inspection: Unit 1 - February 7, 8, 9, and 16, 1973

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Unit 3 - March 22, 1973

N C Lw/

F. A. Maura

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Principal Inspector:

'(Date)

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Accompanying Inspector:

C. Brown

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Other Accompanying Personnel: None

hC.k%w

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Reviewed By:

H. C. Dance, Senior Reactor Inspector

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BWR Operations Section

'(Date)

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SUMMARY OF FINDINGS

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Enforcement Action

A.

Deviations from Unit 1 Technical Specification surveillance testing

requirements were as follows:

1.

Contrary to paragraph B.16.f(1), the voltage of the pilot cell and

the temperature of the adjacent cells were not measured during the

weeks of January 1-7, 1973, and January 15-21, 1973.

(Paragraph 6.a)

2.

Contrary to paragraph B.16.f(l), the specific gravity and voltage

of the pilot cell, temperature of the adjacent cells and overall

battery voltage was not measured for the week of February 19-25,

1973.

(Paragraph 6.a)

3.

Contrary to paragraph B.16.e(l), the licensee did not have docu-

mentation to show that the Unit 1 diesel generator was started and

loaded to full load output and maintained in that condition until

the diesel engine and the generator reached equilibrium temperature

during the month of December 1972.

(Paragraph 9.a)

B.

Deviations from Unit 1 Technical Specifications reporting requirements

were as follows:

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1.

Contrary to paragraph J.3.a, the licensee failed to report the

bypassing of in-core monitoring string 113, an abnormal occurrence,

to its Production Department in a prompt manner.

(Paragraph 4.c)

2.

Contrary to paragraph J.3.a

the Station Review Board failed to

review the bypassing of in-core monitoring string 113 in a prompt

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manner.

(Paragraph 4.c)

3.

Ccatrary to paragraph J.5, the licensee failed to report to the

Cottission the fact that it operated with the emergency condenser

shell side water temperature greater than 100*F during the week

of March 5-11, 1973.

(Paragraph 3.f(l))

C.

Deviations from Unit 1 Technical Specifications operating requirements

were as follows:

Contrary to paragraph J.2.a(9), the licensee is operating without a

detailed written procedure, approved as specified in the Technical

Specifications, to assure the safe shutdown of the plant in the event

of a flood designated as a Probable Maximum Flood.

(Paragraph 2.a(16))

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Licensee Action on Previously Identified Enforcement items

A.

The corrective actions listed in the licensee's response to our letter

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of enforcement dated October 19,

972, concerning the installation of

the core spray system, were reviewed during this inspection. The items

are considered resolved.

(Paragraph 8.a)

B.

The corrective actions taken by the licensee concerning the items of

noncompliance identified in our letter of January 18, 1973, were reviewed.

The corrective action on the diesel generator breaker failure has been

completed satisfactorily.

It was noted that their commitment to report

events in accordance with Technical Specification requirements was not

carried out.

(Paragraphs 9.b and 3.f(l))

Unusual Occurrences

A.

Core spray valve CS-ll failed to open during surveillance testing.

(Paragraph 8.b)

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B.

Primary steam line isolation valve M0-169 failed to close during unit

shutdown.

(Paragraph 3.d)

C.

Emergency condenser shell side water temperature- exceeded 100*F with

reactor at pressure greater than 140 psig.

(Paragraph 3.f(l))

D.

Emergency condenser automatic initiating signals reduced during plant

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shutdown.

(Paragraph 3.f(2))

E.

In-core string 113 scram function bypassed during plant operation.

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(Paragraph 4.c)

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Otner Significant Findings

A.

Current Findings

1.

Organir cion

Effective April 2, 1973, W. Hildy replaced C. Weber, who has

terminated his employment with Commonwealth Edison Company, as

Instrument Engineer. Although Mr. Hildy will not meet all the

requirements of Section 6.1.D.5 of the Technical Specifications

until October 1973, the instrument group has two foremen who

meet all the requirements of Section 6.1.D.5 for the position

of Instrument Engineer.

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Effective June 1, 1973, J. Diederich will report to N. Kershaw at

the corporate office as a member of the Nuclear and Fossil Systems

Group.

Mr. A. Roberts, presently Operating Engineer for Unit 1,

will replace Mr. Diederich as Supervisor, Technical Staff. He meets

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the requirements of Section 6.1.D.4 of the Technical Specifications.

Mr. T. Watts, presently Operating Engineer for Unit 3 and holder of

Senior Operator's License on all three units, will replace Mr.

Roberts as Operating Engineer, Unit 1.

Mr. D. Scott, presently a

Shift Foreman, will replace Mr. Watts as Operating Engineer, Unit 3.

Mr. Scott has a Senior Operators License for Units 2/3.

Mr. G.

Abrell remains as Operating Engineer, Unit 2.

All three Operating

Engineers meet the requirements of Section 6.1.D.3 of the Technical

Specifications.

2.

Unit 1 continues operating at approximately 115 mwe (approximately

58 percent power) with a chimney gaseous release rate of approxi-

mately 44,000 uci/sec.

3.

Unit 3 has complaced core reconstitution. Return to power operation

is planned by end of May.

B.

Status of Previously Reported Unresolved Items

On March 21, 1973, the licensee submitted the analysis of stresses on

Unit 1 safety valves. The results indicate no problem exists. This

item is considered resolved.

(Paragraph 3.e)

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Management Interview

The following subjects were discussed at the conclusion of the inspection on

April 25, 1973, with Messrs. W. Worden, Station Superintendent; F. Morris,

Assistant Station Superintendent; A. Roberts, Operating Engineer, Unit 1; and

C. Sargent, Engineer.

A.

The inspector stated that the licensee's actions to correct the nine items

of nonconformance, with regard to the installation of the core spray

system, were reviewed and that he had no further questions at this time.

However, it was noted that the station records do not include the latest

"as built" drawings of the system. Also, he stated that it is our

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understanding that the QC Engineer will review the QC welding record

requirements against what is maintained by some of the piping subcontractors

for applicability into the QC program.

The licensee indicated that the latest as built drawings would be obtained

and that a review of the QC welding record requirements will be performed.

(Paragraph 8.a)

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B.

The inspector stated that the licensee's actions concerning the noncom-

pliance items covered in our letter of January 18, 1973, were reviewed.

It was noted that although both items have been resolved, the licensee

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failed to report to the Commission in a timely manner several days during

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which the energency condenser temperature exceeded 100'F which was in

violation of the Technical Specificctions, and contrary to the comaitment

made in response to our enforcement letter.

(Paragraph 3.f(l))

C.

The inspector stated that we have received and reviewed their safety

valve etress analysis report for Unit 1, and that we have no further

questions at this time concerning the results of the stress calculations,

but that we question the use of Proposed Code Cases in their analysis.

The licensee indicated our comments would be passed on to their Engineering

Department.

(Paragraph 3.e)

D.

The inspector noted that a review of Unit 1 surveillance records showed

that problems similar to those found during the last Unit 2/3 inspection

continue to occur. For example, some of the data sheets have misaing

readings, lack date and signature of data taker and reviewer, etc. As

a result of the review, the following violations of Technical Specification

requirements were noted:

1.

The weekly checks for the 125V battery bank were not done during

the week of February 19-25, 1973.

2.

During the weekly check for the 125V battery bank, the voltage of

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the pilot cell and the temperatures of the adjacent cells were not

teken during the weeks of January 1-7, 1973, and January 15-21, 1973.

3.

The surveillance test records for the December 1972 monthly diesel

generator test could not be found.

(Paragraphs 6.a and 9.a)

E.

With regard to the bypassing of the scram function of in-core string 113

on April 8-9, 1973, the inspector stated that the review indicates

inadequate procedures appear to have contributed heavily as a cause of

the event, and that we note the procedure has been corrected, but that

we question how events such as this one are incorporated into the retraining

program in an effort to reduce or eliminate the number of human errors.

The inspector stated that he would look into this during a future inspec-

tion.

(Paragraph 4.c)

F.

The inspector noted that the bypassing of in-core string 113, an abnormal

occurrence, had not been reported to the Manager of Production or his

delegated alternate in a prompt manner. Assuming that the Superintendent

of Production, Division A, is the " delegated alternate," his notification

did not occur until approximately 63 hours7.291667e-4 days <br />0.0175 hours <br />1.041667e-4 weeks <br />2.39715e-5 months <br /> after the event took place.

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The licensee asked what the inspector considered " prompt not tr tent ton"

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and was informed that this inspector considered delays of up to eight

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to ten hours a2 satisfying the " prompt notificacion" requirement.

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(Paragraph 4.c)

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G.

The inspector noted that the Technical Specifications requirement for

an emergency procedure to cover the event designated as the " Probable

Maximum Flood" has not been complied with, 10 months since such

requirement has been in effect.

(Paragraph 2.a(16))

H.

With regard to procedures, the inspector stated that the abnormal pro-

cedures for the battery bank had not been reviewed in accordance with

our understanding of August 27,1971.1/ In addition, he stated that

the time to develop adequate procedures for conducting an orderly plant

shutdown, in case all de power was lost, was now and not during the event.

The licensee could not recall any understanding regarding the battery

bank abnormal procedures.

(Paragraph 2.b)

I.

The inspector stated that an inspection of the records covering the

present refueling operations on Unit 3 indicated that the fuel and core

reconstitution was in accordance with the submittal to Licensing dated

March 5, 1973, except that the number of new elements placed in the core

periphery was increased from 28 to 52.

The licensee indicated a revised submittal to Licensing correcting the

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total number of new fuel assemblies placed in the core was recently

approved by the SRB and should be in the mail soon. The transient

analyses as described in the Safety Analysis Report remain unchanged

by the increase in new fuel acsemblies.

(Paragraph 5.a)

J.

The inspector stated that he had reviewed the repairs made to the Unit 3

torus painted surface and as far as he could tell they were similar to

the repairs performed on the Unit 2 torus in 1772; also that he under-

stands all the baffles in the Unit 3 torus have been removed and that

the Unit 2 torus baffles will be removed during its next refueling outage.

The licensee agreed.

(Paragraph 7.a)

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RO Inspection Report No. 050-010/71-07

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REPORT DETAILS

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Personnel Contacted

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W. Worden, Station Superintendent

F. Morris, Assistant Station Superintendent

J. Diederich, Supervising Engineer, Technical Staff

T. Watts, Operating Engineer, Unit 3

A. Roberts, Operating Engineer, Unit 1

G. Abrell, Operating Engineer, Unit 2

R. Bishop, Enginaer, Technical Staff

J. Bowers, Engineer, Technital Staff

T. Suchocki, Engineer, Technical Staff

W. Jack 1w, QC Engineer, Technical Staff

J. Groth, Engineer, Station Construction

S. Hlady, Engineer, Station Construction

R. Williams, Engineer, Technical Staff

R. Cozzi, Engineering Assistant, Surveillance

R. Dyer, Maintenance Foreman

C. Lawton, Office Supervisor

C. Sargent, Engineer

H. Habermeyer, Shift Engineer

D. Simpson, Refueling Foreman

J. Sullivan, Nuclear Station Operator

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2.

Procedures - Unit 1

a.

Resolution of Comments Given to Licensee During Previous Inspection

During the November 28 to December 1, 1972, inspection,2/ a number

of comments were given to the licensee for resolution. During this

inspection the items were reviewed with the licensee with the

following results:

(1) The control steps given in Technfcal Specifications section

G.2.d are being incorporated to the plant startup procedure

as indicated by Action Item 73-81.

This item is considered

resolved.

(2) All check lists will be included as part of the manual pro-

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cedures (Action item 73-72)." This~ item is co'hsidered resolved.

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RO Inspection Report No. 050-010/72-06

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(3) Administrative Procedure ADM-I will refer to present Technical

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Specifications (Action Item 73-81). This item is considered

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resolved.

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(4) ADM-II will be expanded to include specific assignments and

schedules.

(Action Item 73-81) This item is considered

resolved.

(5) ADM-VII will be rewritten to include more guidance of how log

books are to be maintained and what records are required. During

a previous inspection station management had indicated this is

one of their high priority goals for 1973. We plan to review

this during future inspections.

(6) ADM-II will refer to the specific QC procedure or method for

documenting temporary changes (Action Item 73-81). This item

is considered resolved.

(7) Table 30-C covering SRB responsibilities will be corrected so

that it will agree with Technical Specification requirements

(Action Item 73-71). This item is considered resolved.

(8) ADM-VIII is being deleted under Action Item 73-175. This item

is considered resolved.

(9) ADM-IX Appendix A is not missing. The licensee had erronecusly

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labeled it as Appendix B.

This is being corrected. This item

is considered resolved.

(10) The review of all outstanding operating orders has been

completed.

(11) Chapter 37 of the Operating Manual is being prepared under

Action Item 73-73 and will cover all our concerns about radiation

controls. This item is considered resolved. We vill review

Chapter 37 after its completion.

(12) The licensee stated their procedures will be changed to ensure

the unit is scrammed immediately whenever a ground level release

occurs. This is covered under Action Item AEC-45. This item

is considered resolved.

(13) The unloading heat exchanger system has been removed from direct

contact with the service water system. According to the licensee

the heat exchanger is now cooled by the closed cooling water

system. The system procedures must be revised to reflect this

change. We will inspect this at a future date.

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(14) The licensee is developing procedures for removal and replace-

ment of the reactor vessel head piping to rer' lect the addition

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of the core spray system. This is covered under Action Item

AEC-42 and is considered resolved.

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(15) The licensee plans to review Safety Guide No. 33 and ANS-3.2

to determine if the inservice inspection program ~ procedures

are required as part of the Station or Unit Procedures Manual.

The licensee agreed to conform to the recommendation of ANS-3.2

and Safety Guide No. 33.

It is the inspector's position that

such procedures are recommended by the above documents.

(16) The licensee has failed to provide an emergency procedure for

the event designated as the " Probable Maximum Flood" as required

by Technical Specifications paragraph J.2.a(9).

This require-

ment has been in effect for over 10 months. More recently, on

March 12, 1973, the Directorate of Licensing turned down a

request from the licensee for a Technical Specification change

to delete the requirement for such procedures.

b.

Abnormal Procedures - 125V Batterv Bank

During an August 25-27, 1971, inspection,3/ the licensee agreed to

review the battery bank procedures for what steps should be taken,

such as plant shutdown, in the event the battery chargers are lost.

The inspector had stated that the procedures should include the

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point in time, af ter the loss of the chargers, when a controlled .

plant shutdown would be initiated.

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A review of procedures 9800 AN I, II and III showed that the licensee

had not performed the intended ?- iew.

In addition, it was noted

that 9800 AN III called for an orderly plant shutdown if all de power

was lost (chargers and batteries). When questioned, the licensee

stated that an orderly shutdown for such an event was preferable to

a scram because without de power many of the required breaker actions

have to be performed manually and time was needed to ensure the proper

actions were taken. The inspector determined that, although the

licensee considers such an event unlikely to happen and one which if

it happens requires manual actuation of much equipment, the licensee

had not considered developing a procedure which would outline what

equipment had to be operated, in which sequence, and from where in

order to conduct an orderly. plant shutdown. The licensee's plans

were to get out the drawings and start searching after the event had

taken place. The licensee has been requested to develop such an

emergency procedure now.

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RO Inspection Report No. 050-010/71-07

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3.

Reactor Coolant System - Unit 1

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a.

Leak Monitoring

The records on airborne activity in the containment sphere and its

seven compartments were reviewed for the period from January 1, 1973,

to April 20, 1973. The frequency of sampling and response to obtained

results was in accordance with previous commitments and the proposed

addition to the Technical Specifications.

b.

Reactor Coolant

A review of the reactor coolant chemistry records for the period of

January 1, 1973, to March 31, 1973, was performed. Typical range

of values was: pH - 8.7 to 6.4

Conductivity - 0.46 to 0.26 umhos

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.07 to .01 ppm

The values are within the Itaits proposed by the licensee to be

included in their Technical Specifications.

c.

Steam Generator Tuba Leak Repair - Unit 1

A review was made of the leak history and repairs associated with

the four secondary steam generators. The units are vertical U-tube

generators and have 1801 tubes each. The tubes are made of 304L

stainless steel and are supported by baffles of carbon steel (SA-7).

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Since initial startup, the following number of steam generator tube

leaks have occurred and have been plugged.

Tubes Plugged Since Startup

Latest Plugging Number /Date

S/G A - 6 tubes

5 Tubes - 2/4/73

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S/G B - 32 tubee

12 Tubes - 10/17/73

S/G C - 1 tube

1 Tube - 1/21/69

S/G D - None

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Leaks were detected by mismatch in steam flow / feed flow, activity

increase in the secondary water of the affected steam generator and

by increase in the chimney release rate of I-131.

The particular

leaking tube is located by flooding the secondary side of the

generator and observing which tube water issues from. The tube is

then plugged and a primary side hydro is conducted at 1000 psig.

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An audit of the secondary water chemistry values for January and

March indicate the following range of values:

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pH - 6.4 - 8.3

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Cl - 0.2 ppm max

Conductivity - 0.5 umho/cm max

There is no chemistry limit imposed by the facility Technical

Specifications.

According to the licensee, steam generator tube leaks have not

been a major problem and there are no plans for an engineering

study of tube failure.

d.

Failure to Close of Primary Steam Line Isolation Valve

on February 4, 1973, during a normal shutdown of Unit 1, a signal

was given to the primary steam line isolation valves to shut. The

valves, MO-169 and MD-170, isolate the primary steam lines just

upstream of the containment penetration. Valve MO-170 shut, but

MO-169 failed to close. The investigation revealed that foreign

material had prevented the opening interlock from clearing in the

valve's motor operated breaker. Simultaneous operation of motor

operator in open and close direction is prevented both electrically

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and mechanically. Following repairs MO-169 operated satisfactorily.

M0-170 operator breaker cubicle was inspected for foreign material

and appeared in satisfactory condition.

The licensee plans to inspect and clean all similar breaker cubicles

and review overhaul procedures for breakers throughout the Dresden

Station. At the time of the inspection, neither of the above items

was complete. Both items are covered by Action Items No. 73-52 and

53.

The event was reviewed by the SRB during its 433d meeting and

reported to the Directorate of Licensing on February 14, 1973.

e.

Unit 1 Safety Valves Stress Analysis

The report on Unit 1 safety valves stress analysis indicates that

while the allowable stress limit is 17,220 psi, the highest calculated

stress level is 13,750 psi. A review of the analysis showed that

the licensee utilized Proposed Code Cases to ASME,Section III,

ND-7221, to calculate the valve reaction force, account for dynamic

impact, and for uncertainties in the maximum mass flow rate. While

the analysis appears to be satisfactory and we do not question the

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results, the licensee was reminded that Proposed Code Cases should

not be used until approved by the ASME Code Committee. This item

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is considered resolved.

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f.

Emergency Condenser

(1) Operation with Shell-Side Temperatures in Excess of 100*F

The corrective measures described in the licensee's letter

(Lee to Grier) dated February 7, 1973, were not satisfactorily

carried out. A record review indicated that from March 5, 1973,

through March 11, 1973, the licensee operated with a shell side

temperature greater than 100*F, but failed to report it in

accordance with paragraph J.5 of the Technical Specifications.

On March 12, 1973, a change in the Technical Specifications

allowing shell-water temperatures as high as 212*F was approved

by the Directorate of Licensing. The present limit cannot be

exceeded since the system is open to the atmosphere. The

highest recorded temperature so far has been 210*F on March 18,

1973.

(2) Reduction of Emergency Condenser Effectiveness in Terminating

A Transient

The licensee reported that on March 17, 1973, during a controlled

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shutdown of Unit 1, the emergency condenser key switch was placed

in bypass position with 47 control rods withdrawn and pressure at

650 psig. With the switch in bypass, high reactor pressure and

closure of primary steam isolation valves do not initiate

emergency condenser operation; however, the bypass did not affect

the auto oparation of the emergency condenser if needed for

emergency core cooling which is initiated by signals from high

sphere pressure and low primary drum level. The normal shutdown

procedure, which does not cover shutdown to hot standby, was

used, as modified by instructions from the Operating Engineer.

The licensee stated that procedure inadequacies were the major

cause of this incident. As corrective action, the licensee is

in the process of generating additional, more detailed procedures

to cover shutdown to hot standby and cooldown from hot standby.

This is covered under Action Item 73-105. The SRB reviewed the

event during its 452d meeting and it was reported to the

Directorate of Licensing by letter dated March 27, 1973.

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4.

Reactivity and Power Control

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a.

Control Rod Drives - Unit 1

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CRD F-1 remains out of service in the fully inserted position. No

further attempts to wichdraw it have been made and the plans are to

investigate and correct the problem during the refueling outage

scheduled for next fall. All other rods continue to operate satis-

factorily.

The performance of surveillance tests as required by the Technical

Specifications was reviewed as noted below:

Item

T/S Requirement

Results

Time required

At intervals dC

Performed 4/11-14/73. Min,

to fully

six months

withdraw time was 15.5 sec.

withdraw and

between refueling

After adjustment min. time

insert each CRD

outages Due 5/1/73

to withdraw was 17.0 sec.

Exercise up

Same as above

Performed 4/11/73. No

and down.

Stop

abnormalities recorded.

at each latch

po sition. Check

for proper

latching,

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unlatching,

position switch

and indicator

operation.

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Friction test

Same as above

Performed 4/10-11/73. Ten

CRD's recorded A P in excess

of 100 psi required to move

drive. Max was 174 psi

(E-5).

Lowest recorded was

49.5 psi (C-7 and B-6).

Scram times

Same as above.

Performed 4/11/73. Longest

Max. time

scram time recorded 1.68 see

allowable 2.5

(H-2).

Shortest 1.08 sec

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sec.

(F-8).

Time in buffer ranged

from 0.63 to 0.15 sec.

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b.

Scram Accumulators - Units 1, 2, and 3

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A review was made of the maintenance history of the accumulators for

Units 1, 2 and 3.

There is no regularly scheduled inspection of the

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accumulators.

'te accumulators are replaced with a spare if a

problem occuta with the installed unit. The replaced accumulator is

then inspected, repaired (if the problem was in the seals) and then

placed in stores as a spare. Unit 1 has 53 accumulators, 26 pairs

operating three control rods and a single accumulator operating two

control rods, and 73 change outs have occurred since the unit was

started up in 1960. Of these 73 accumulators, 25 of the cylinders

have been junked. According to the licensee, the major cause for

rejection was minute pitting of the chromium plating on the inside

of the cylinder. A few had the chromium plating pealing off wherc

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the piston had sat for long periods of time.

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Units 2 and 3 each have 177 accumulators and the records show that

Unit 2 has had 16 accumulator change outs and Unit 3 has had 12

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change outs. A total of 14 cylinders have been scrapped from the

two units because the chromium plating had become pitted. No peeling

of the ' plating has been observed.

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Units 2-3 also experienced another problem whereby "0" rings made

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of Buna-N appeared to be dissolving and " smearing" on the cylinder

surface when the piston moved. The cylinder had to be cleaned

with CCl . The licensee representative stated all the Buna-N

"0"

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rings were replaced with new "0" rings made of Viton. The Buna-N

"0" rings appeared to have been mistakenly installed on a few

accumulators by the manufacturer.

c.

Bypassing of In-Core String 113 - Unit 1

On April 8, 1973, the scram function of in-core string 113 was

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bypassed, in violation of Section B.9.a of the Technical Specifications,

following an upscale failure of all four chamber amplifiers. This

action left a four foot diameter, vertical cylindrical core volume

without scram protection for approximately 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />. The event was

reviewed by the SRB during its 468th reeting on April 17, 1973,

approximately nine days after its occurrence, and the details were

reported to the Directorate of Licensing on April 17, 1973. The

SRB review approximately nine days after the event cannot be con-

sidered to have been conducted in a prompt manner as required by

the Technical Specifications.

.

The inspector verified that the procedures in effect at the time

of the event were utilized by the shift personnel, but that the

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procedures did not identify the strings which constituted " critical

('

pairs" and therefore were a contributing factor in the erroneous

.

decision to bypass the scram function of all four chambers. The

,

procedure has been revised and should no longer be a cause of con-

fusion to the operating personnel.

All corrective actions listed in the licensee's report' have been

completed. The inspector questioned how the licensee's retraining

program incorporated hunan error in order to reduce the number of

such errors. The licensee was not able to answer this question,

and the inspector stated that he would follow the matter at a

future inspection with the Training Supervisor.

While reviewing the event, the inspector noted that the licensee

did not report the event to the Superintendent of Production,

Division A, until 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> on April 11, 1973, or approximately

63 hours7.291667e-4 days <br />0.0175 hours <br />1.041667e-4 weeks <br />2.39715e-5 months <br /> after the event had taken place. This is an extremely

loose interpretation of the requirements of paragraph J.3.a of

the Technical Specifications, which requires prompt notification

of the event to the Manager of Production or his delegated alternate.

5.

Core and Internals - Unit 3

a.

Refueling Operations

The inspectors observed Unit 3 refueling operations on April 17,

-

1973. The observation, which included refueling procedure steps

253 through 270, covered:

(1) Transfer of fuel from the storage well to the reactor core

(2) Transfer of fuel from one core position to another

(3) Testing of the fuel grapple interlocks (at the request of the

inspector)

,

(4) Control room operation, including rod withdrawal following the

loading of each fuel cell

(5) Fuel element reconstitution, including the handling of fuel

rods, and eddy current and ultrasonic testing of fuel rods

The inspectors verified that the refueling operations were being

conducted in accordance with the requirement established by

Operating Orders 17-73 and 21-73, the unit Technical Specification

requirements, and the liceneee's Proposed Modification 73-2, entitled

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"Dresden Unit 3 First Reload Fuel," dated March 5,1973; the only

('

devistion being that 52 new fuel elements were loaded in the core

-

1

internals of 28 elements as stated in Proposed Modification 73-2.

.

!

The licensee stated the change does not affect the safety analysis

prea'. ted in the document and that a supplementary .1.etter informing

of the change would be submitted to Licensing before Unit 3 restart.

Communications between the refueling area and the control room were

satisfactory. The inspector noted that during the rod withdrawal

following the loading of each fuel cell the operator verified

coupling integrity by attempting to withdraw the rod past position

48.

The operator stated this is normal practice following withdrawal

of any control rod.

1

b.

Fuel Inspection Results

4

A review of the results of fuel sipping and reconstitution showed

that 103 fuel assemblies contained failed fuel rods. Of these,

seven were discovered during partial in-core sipping, and 90 during

100 percent out-of-core sipping. Six additional assemblies were

rescheduled for sipping due to suspected initial results. Of these,

five were rejected as a result of ultrasonic (UT) and eddy current

(EC) tests and were not resipped. The sixth was resipped with satis-

factory results, but UT and EC testing gave positive indication on

two of its fuel rods. Of the 103 rejected assemblies, 52 were replaced

with new fuel assemblies and the remaining were replaced with recon-

!

stituted assemblies in which failed fuel rods were replaced with sound

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rods scavenged from within the 103 fuel assemblies. In addition to

passing a satisfactory UT and eddy current test, a fuel rod could

only replace a failed rod if the criteria outlined by a document

titled " Bundle Repair Rules," dated February 16, 1973, and its

addendum dated Feburary 28, 1973, were met.

The Station Review

Board approved the criteria at its 440th meeting on March 7,1973.

In addition, all reconstituted fuel assemblies were resipped with

satisfactory results prior to being returned to the reactor. The

inspectors randomly selected fuel assemblies 84, 134 and 440 and

determined that all the criteria for bundle repair had been complied

with.

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All fuel rods, except for the spacer capture rods and 18 stuck rods

which were rejected, comprising the 103 failed fuel assemblies were

ultrasonically (UT) and eddy current (EC) tested. The criteria for

rod rejection consisted of a positive UT and/or greater than 35

percent EC indication. Of the 5,047 rods, 603 were rejected, an

average of approximately 5.9 rods per assembly. A summary of the

rejected rods follows:

1

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(1) By Enrichment

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Enrichment _

Failure

-

,

1.2%

80

1.69%

168

1.69% (Tie Rods)

90

2.44%

226

2.44% (Tie Rods)

39

603

(2) By Testing Criteria

EC

UT

Failure

35%

Positive

187

'

35%

Positive

86

35%

Negative

269

35%

Negative

61

at spacer

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603

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The locations of the 197 fuel roda with greater than 35 percent

EC and positive UT withir. the fud assembly is shown below.

2

1

5

1

5

0

6

'

2

2

1

1

0

5

1

1

1

0

1

0

1

4

1

0

1

2

1 10

2

1

1

0

3

2

24

1

1

1

5

1

3

2

control Rod Blade

O

3

2

9

19

7 45

  • Not tested

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The locations of the 603 rejected fuel rods within the fuel

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assembly are as shown below.

s

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9

7

12

8

10

9

11

11

8

7

10

6

11

17

7

9

9

8

5

8

9

10

4

9

12

9

22

13

9

8

8

15

13

37

8

7

7

19

9

18

7

Control Rod Blade

13

12

11

26

33

17

56

  • Not tested

During the EC and UT scanning of the fuel rods, defect signals may -

have been observed in more than one axial location. The licensee

recorded the area where the highest signal was observed for each

rejected rod. The axial distribution of these " worst" areas is

given below:

-

Axial Location

Above Lower End

Rods With 35% EC

Plug (inches)

and Positive UT

All Rejected Rods

0-10

36

255

11-20

12

58

21-30

4

8

31-40

11

22

41-50

5

10

51-60

5

10

,

61-70

6

8

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Axial Location

Above Lower End

Rods With 35% EC

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Plus (inches)

and Positive UT

All Rejected Rods

,

,

71-80

3

8

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81-90

14

23

91-100

20

34

101-110

19

30

111-120

15

22

121-130

8

13

131-140

11

25

Location not identified

18

77

187

603

The licensee's records indicated that at least 1.0 fuel rods separated

circumferentially as follows:

(1) Six fuel rods separated at lower end plug.

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(2) One fuel rod separated at approximately one-third from lower

end plug.

(3) One fuel rod separated approximately eight to 12 inches from

lower and plug.

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(4) Two fuel rods separated approximately 12 inches from upper

and plug.

6.

Electrical Systems - Unit 1

a.

Unit 1, 125V Battery

The licensee's performance of surveillance tests required by the

Technical Specifications was reviewed as noted below:

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T.S.

Period

Itam

Requirement

Inspected

Results

(

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Cell voltage to

Every three

1/73-3/73

Satisfactorily

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nearest .01 volt,

months

performed

specific gravity

1/12/73

of each cell cnd

temperature of

every fifth cell.

Specific gravity

We' ekly

1/73-3/73

Voltage of pilot

and voltage of

cell and tempera-

pilot cell.

ture of adjacent

Temperature of

cells not taken

adjacent cells

during the week

and overall

of 1/1-1/7/73 and

battery voltage.

1/15-1/21/73.

,

Entire record

missing for week

of 2/19 to 2/25

.

The above violations are probably the result of the lack of adequate

data sheets as previously noted in RO Inspection Report No.

050-237/73-01. During this inspection it was noted that the licensee

has prr. pared new data sheets which provide space for all the required

_

readings and is in the process of inn.orporating them in the Unit 1

Operating Manu21. The new data sheets were approved by the SRB

during its 461st meeting.

b.

Essential Service Power Supply

The inspector reviewed the normal and emergency supplies of power

to the essential service buses 15 and 16.

Bus 16 is supplied through

its transformers from bus 11, and bus 15 from bus 12 via its trans-

former. Bus 11 is supplied through transformer 11 from the main

generator, or section 1 of the 138 KV bus. Bus 12 is supplied

through transformer 12 from section 2 of the 138 KV bus. As an

alternate supply, transformers 11 and 12 can supply either bus 11

'

or 12 through an automatic throwever. Bus 11 can also be supplied

from transformer 13 which is supplied from the 34.5 KV bus. The

low voltage signal on buses 11 and 12 that closes the breaker from

transformer 13 also starts the diesel-generator.

If the buses 15

and 16 are not energized by the time the diesel-generator is up to

normal speed and voltage, buses 15 and 16 are electrically isolated

from the rest of the system and the diesel-generator is automatically

closed into the buses.

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Control of the diesel-generator and the above breakers can also be

accomplished manually from the control room.

(w

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7.

Containment

.

Unit 3 Torus

The licensee stated that the following work was completed in the Unit 3

torus during the present outage.

a.

All baffles were removed and disposed of.

4

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b.

An inspection of the surface below the water line indicated a large

i

amount of small blisters (1/4 to 1/2" in diameter) covering

approximately 25 percent of the surface area. A few large blisters

were also noted.

c.

The surface below normal water level and a band up to one foot above

the water level were sandblasted to bare metal. This area was then

painted with Carbozine-11. A bellyband of Carboline's Phenoline 368

winter grade primer was applied approximately four inches above and

below the transition line to overlap the existing paint and the new

Carbozine-ll. This repair procedure is similar to that used on

Unit 2 during 1972.

d.

An inspection of the above water line surface indicated a few areas

of pin-hole rust. No flaking or blisters were noted. As before,

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the repair procedure consisted of touch-up.

1

Improved bracing of the relief valve lines similar to that performed

e.

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on Unit 2 in 1972 was completed.

f.

Paint test coupons were installed.

These repairs, with the exception of the baffle removal, update Unit 3

torus to the condition of the Unit 2 torus. Unit 2 baffles will be

removed during its next refueling outage scheduled for 1974

8.

ECCS - Unit 1

a.

Response to Items of Noncompliance

The corrective measures, to items of nonconformance, cutlined in the

licensee's (Lee to Grier) letter of November 21, 1972, were inspected

as noted.

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(1) The cable installation for spare core spray pump 1C was enclosed

in conduit prior to initial operation of the core spray system,

and now satisfies IEEE-279 criteria. This item is considered

(

resolved.

.

(2) As-built drawings for pipe hangers and seismic restraints were

reviewed with Construction personnel.

The new drawings are

dated April 19, 1972, and November 21, 1972. As.a result of

the problems identified during the February 1972 inspection,

a review of the installation, by the Architect-Engineer,

determined that the piping routing was not identical to what

was originally analyzed. A new analysis was performed and a

copy of the results transmitted to CE Company on April 19, 1972.

As a result of the analysis four additional seismic restraints,

CSR 15A, 17, 12 and 13, the latter two being located in the

reactor cavity, were installed. This item is considered resolved,

however, it was noted that the licensee's technical staff and

QA records do not include copies of the latest drawings.

Station

management was informed and an Action Item has been generated to

ensure the copies are obtained.

(3) The inspector verified that the licensee has documentation from

Atwned and Morrill Company, manufacturers of the two cast check

valves in the system, which gives the dimensional measurements

of the valve body castings made by C. A. Wills on October 28, 1971.

The dimensions meet the minimum wall thickness specified in the

drawings.

In addition, the licensee has documentation from

Sargent and Lundy. Engineers concerning a trip to Velan Engineering

~

for the purpose of auditing Velan's records for the four high

pressure forged valves. The licensee is satisfied that the

forged valves meet the engineering specifications. This item

is considered resolved.

(4) The liquid penetrant inspection procedure was approved by the

Architect-Engineer firm by letter dated February 29, 1972. In

addition, the qualifications of the two Level II inspectors

involved were reviewed and approved by the Architect-Engineer.

'

The documentation is now in the site files. This item is

considered resolved.

(5) Three welders were requalified to F. Conry's procedure WSSTM-3,

Revision 4.

They were reviewed with no comments by Sargent and

Lundy on August 17, 1972. They had also been approved by

Pittsburgh Testing Laboratory. This item is considered resolved.

(6) The licensee's QC Procedure 9-51.1 provides a Quality Control

Weld Check Sheet in which a visual inspection of joint fit-up

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is documented. The check sheet does not list all the specific

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fit-up elements that were checked. The licensee plans to

.

compara his check sheets against the check sheets used by

'

other piping contractors, and will modify his to include at

least as much information as is being documented by the piping

contractors' check sheets. This items is considered resolved.

(7) The licensee's QCP 9-51.1 check sheet documents prehcat and

interpass temperature. The above comment on a check sheet

comparison study also applies to chia item. This item is

considered resolved.

(8) A procedure was developed for welding electrode control and,

according to the licensee, used in the completion of the job.

l

The licensee's QCP 9-51.1 controls the issuance and handling

of welding rod and wire during future safety related jobs.

!

This item is considered resolved.

(9) A weld repair procedure was developed. The licensee stated

that all future safety related jobs, and whenever the ASME

Code requires it, will be supplied with a weld repair proce-

dure. This item is considered resolved.

b.

Core Spray Valve CS-ll Failure to Open

During surveillance testing on December 29, 1972, and January 12,

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1973, core cpray valve CS-11 experienced temporary failures to open.

Given a closed signal followed by a second signal to open, the

valve would operate satisfactorily.

Satisfactory operation of the

two valves on the redundant injection line assured the operability

of the system. After consulting with the valve manufacturer, the

licensee has reset the open torque switch on all four valves from

a setting of "1" to "2.5" and the closing torque switch on all four

7

valves-to "2.0".

This was completed on February 26, 1973, at which

time the valves were cycled satisfactorily,

the event was reviewed

by the SRB on its 425th meeting and reported to the Directorate of

Licensing on January 25, 1973.

I

c.

Barton Differential Pressure Transmitters

The inspector questioned the licensee regarding the use of Barton

Model 368, 384 and 386 for which a manufacturing deficiency had

been identified. The licensee identified the use of Barton Model

386 for the transmittal of sphere level information (readout plus

,

alarm in control room) in connection with the core spray system.

The licensee indicated no other Barton d P equipment is in use for

Unit 1, and that the mcnufacturer would be contacted for instructions

on the required corrective action for Model 386.

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9.

Emergency Power - Unit 1

a.

Diesel Generator

,

The licensee's performance of surveillance tests required by the

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Technical Specifications was reviewed as noted below:

Item

T/S Requirement

Period Inspected

Results

2100 gal of

Record Monthly

1/73-4/73

Performed.

fuel for diesel

Quantity

generator

> 3500 gal

Quality of

Check Monthly

1/73-3/73

Water con-

diesel

tent and

generator

microorganism

fuel

growth

c

results

negative

Manual start

Monthly

11/72-4/73

12/72

and load of

Records

diesel

missing

generators

,

Operability

Monthly

11/72-4/73

12/72

2

of diesel

Records

_

fuel oil

missing

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transfer pump

b.

Diesel Generator to Bus 15 Breaker Failure

The corrective measures described in the licensee's letter (Lee to

<

Grier) dated February 7, 1973, have been completed. The breaker was

replaced with an identical unit on April 13, 1973. The replacement

was satisfactorily tested. The breaker to bus 16 was not replaced.

The licensee stated that in the past failures have been experienced

with the breaker to bus 15 while no failures have ever been experienced

with the breaker feeding bus 16. The item was reported in the semi-

'

annual report as indicated in the letter. This item is considered

resolved.

10.

Radioactive Waste Systems - Units 2 and 3

Reactor Building CAM Alarms

The inspector verified that the reactor building continuous air monitor

alarm has been wired to the annunciators of Units 2 and 3 in the control

room. This item is considered resolved.

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