ML19338F470
| ML19338F470 | |
| Person / Time | |
|---|---|
| Site: | Fort Calhoun |
| Issue date: | 10/10/1980 |
| From: | Tira Patterson OMAHA PUBLIC POWER DISTRICT |
| To: | |
| Shared Package | |
| ML19338F468 | List: |
| References | |
| NUDOCS 8010200402 | |
| Download: ML19338F470 (9) | |
Text
'
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..AVERAGt. DAILY UNIT POWER LEVEL
' DOCKET NO. 50-285 UNIT Fort Calhoun No. 1 DATE Octobe.- 10, 1980 COMPLETED BY T. L.~Patterson TELEPHONE (402)536-4413 MONTH-September, 1980 DAY
' AVERAGE DAILY POWER LEVEL DAY
~ AVERAGE DAILY POWER LEVEL (MWe-Net) -
(MWe-Net)
- I 436.4' 462.6 37 2
442.4-464.4 18 3-458.2 ~
295.4 39 457.2 373.8 20 457.9 375.3 5
2, l
6
.457.1-22 371.6 7 s-456.l'~
23 302.2 8-455.1 24 301.3 9
455.6 25 302.2 l
30 458.6'-
26 302.6 l
-1I 460.2' 27 301.6 12 459.7 300.9
-28 i
'13 459.4 300.5 l
29 l
14 460.1 299.2 39 15'.
461.7 3,
.16 463'5-
~ INSTRUCTIONS.
-t:, *his format. list the average daily ~ unit power levelin MWe-Net for each day in the reporting month. Compute to
- the nearest whole megawatt.
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~
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e OPERATING DATA REPORT' u
n
, 7
- DOCKET NO. 50-285-a
~
DATE 1 October-10, 1980?
+5 COMPLETED BY Tc L. Patterson :
^
su TELEPHONE: (402)536-4413
' IOPERATING STATUS I
- O Unit Name:
Fort Calhoun No.11 Not*5 d/ Reporting Periodi 'SeDtember,i1980
,3.: Licensed Thermal Powei(MWt):-
1500-
[
T. Naineplate. Rating (Gross MWe){.
502-4 bl:x
! 5.i Design Electrical Rating (Net MWe):. 4574
- 26. Maximum De'pendable Capacity (Gross MWe):l 401 L
- 17. Maximum Dependable Capacity (Net MWe)i 457
. 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
NRC"acoroved st' retch poweri o -1500:MWt effective Auoust 15. 1980 t
L-
- 19. Power Level To Which Restricted,If Any(net MWe)i N/A
- 10. Reasons For Restrictions,1f'Any:
N/A-M, j-
~
This Month ;
Yr.-to.Date Cumulative,.
y i1. Hours In Reporting Period :-
i20.0
- 6,575.0~
61,512.0 l:
- 12c' Number'Of flouriReaktor Was Critical.
718.6 3,167.7--
47.569.3-
!4
/13[ Reactor Reserve Shutdown Hours 3
-0.0
- 0.0 -
'1,309.51
[>
il4.l Hours Generator On.Line' -
716.4*
3,103.7--
46,554'.8
-w 715; Unit Reserve Shutdown Hours 0.0
'0.0 0.0~
~
ll6.1 Gross ThermSI Energy Generated (MWii) --
935.546.7
- 4.102.293.0-57.337.322.3'
- 17.- Cross Electrical Energy Generated (MWH)1 3051248.D_ _.
l'.333'.180.0
- 18.993.409.6_,
- e
- is.. Net Ele'etrichl Energy Genera'ted (MWH) 289.263.3-1.263.462;3 17.950.982.1 19.
- Unit Service' Factor:
'99.5^
47.2 75.7-
, gf S20J Unit'Avsilability Factor r 99.5-
-47.2 7 S. 7--
21 p. Unit Capacity Facht (Using MDC Net)j 87.9
- 42.0 '
- 64.3 7.
87.9 42.0-63.9-3 22.(Unit Capacity Factor;(Using DER Net) -
7 1
[f l23. Unit Forced Outage Ratet 0.5-0.4 4 ~. 2 -
c24[ SSundiiwin SchEdukd Over Nex't 6 Months (Type, Date,and Duration of Each):
5:
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N/A 4
- 25. If Shut Down At End Of Report Period. Estimated Date of Startupi Jp-12QUnits in tnt'Sthius (Prior to Commercial Op' eiation)
- (
Forecast' -
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INITIAlhlECTRICITY?.
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Y DOCKET NO., 50-285 UNITSIIUTDOWNS AND POWER REDUCTIONS UNITNAME Fort Calhoun Nc.il'
'DATE October 10. 1980.
u-
.. COMPLETED By lT.
L'. Patterson REPORTMONTil September.1980 TELEPilONE - (402)S36-4413 t:
3E-3.
.Y ~
Licensee
-,E t, Cause & Corrective.
No.
,Date g-q g;
,g g 5 Event -
3,3 g3 Action to
$5
~gg
. Report a m O_
U
~ Prevent Recurrence '
o e
u
- o 80-03
-800919 F
3.6 A
3 RB CKTBRK Control rod clutch power supply-breaker tripp_ed when switching power sources _ to-investigate
.,s '-
voltage spiking on' inverter C.
M 1
I-3 4
'F: Forced.
Reason:
Method:
Exhibit G-Instructions S: Scheduled A. Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram.
Entry Sheets for Licensee C. Refueling.
3-Automatic Scram.
Event Report (LER) File tNUREG-'
D. Regulatory Restriction --
4-Other (Explain) 0161)
E-Operator Training & License Examination F-Administ rative -
'5 (9/77)
II-Ot her (E xplain)
Exhibit I - Same Source G-Operational Eiror (Explain)
. -+ n y
D N7
~
~
= Refueling-Infon:ntion;, _
~
3 Fort Calhoun ;-. Unit f No. l~
s
. EcportiforM.the montli ending September'30, 1980 (1. 1ScheduledSte for,next' refueling shutdown.:
e Septembe 15, 1981 2d Scheduled date-for restartCfollowing refueling; November 15,.1981
. Will refueling:or. resumption of operation thereafter -
M3.
srequire-altechnicallspecification'changeor:other
. No-
~
11icense amendment?
,.; a. -If answer is yes, what, in general', will these bs? :
~
b; ~If answer is no,lias the reload fuel design chd core configuration been reviewed by
- your, Plant ~ Safety-Review Conmittice to deter-
. mine whether any unreviewed. safety: questions No.
are associated with the core reload. -
- c. lIf no such' review hasitaken place, when is
~it scheduled?,.
-September 1, 1981 4.
Scheduled.date(s) for submitting proposed licensing iaction andLsupport infouration.
t--
-5. DImportant licensing considerations associated with
~
refueling, eig., ncw orfdifferent fuel:: design or isupplier, unraicw d desian or performance analysis irethods, 'significant changes 'in fuel; design,: new operating procedures.'
133 asserrblies
~ 6. JThe nurberto'f fticl[ assemblies: 'a) in the core b)Lin; the-spent _ fuel pool:
19/
c): spent fuel:-pool-e storage capacity 483 xd) plarmed spent ' fuel pool:
.. g a
- <~
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1 storage capacity 483
- 7 4Tholprojected dateJof the 'last refueling thatL can be.
~
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-a:
+ : discharged.to the spentiifuel' pool" assu:ning the present -
' liceivicd: capacity. "
19"5 g_
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) OMAHA'PUBLIC' POWER DISTRICT..
Fort Calhoun' Station Unit No.ol
.y M
- [
. September;1980
^.f
- MonthlK 0perations_ Report s
MI; : OPERATIONS
SUMMARY
i 1The' Fort Calhoun Station was, operated.at stretch power during the month aof. September. Using alspecial test. procedure plant power and reactor.
-inletztemperature were' increased and performance. data obtained. To l accommodate : system load' power vas tinitially. reduced to 80% and: subse.
'quently to 655. : One' reactor trip occurred in September as a result of loss of power to.the control rod clutches. ~All' systems-responded-I
. normally.and the generator. was synchronized Lto the grid the same day.
l-Six' shift training continued and preparations vere completed for full-
-time' training of the hot license' candidates prior to the' late' fall exam.
' Normal operational testing requirements was completed as scheduled.
A.
PERFORMANCE CFR ACTERISTICS
'LER NumberL Deficiency i
LER-80-017 During nomal power operation, it was discovered
..by Operations personnel that the setpoint_. selector i
switches ' for RMO-61, ' stack particulate radiation-monitor,- were -set in the higher of the two 'setpoint
~
pos1tions. - This position ~is normally used when.
.te=perature inversions; exist. -At thi time.-of find--
.ing the switches'in the wrong position, an inversion did:not exist.
Tech.' Spec. 5.9 2(3) applies.
-LER-80-018 During normal ' operation a sample of the gas space-:-
. on the ;VCT vas being: drawn through the gas analyzer.
- A malfunction-of the sampling' apparatus-caused the inadvertant release of a small cyality 'of radio-active material,to"be. auxiliary building environment..
= Subsequently the material _was passed to the atmos :
phereLthrough the auxili m/ building ventilation:
- system. The release.vas; monitored o.
short duration' f
and vasewithin'the, Tech. Spec.flimits..' Notification
' of the NRC and'offsite support agencies was made
?per I.E.'Information Notice 80-16, Tech. Spec.
5 9 2.b(h)'and FCS Energency_ Plan.
~
t
. LER 020 1.During-normal? power operation,.it was. discovered <by;
- operatorfobservation that'the Axial Power Distribution-
~
f(APD) 'setpoints on~'D channel vere out - ~ f tolerance -
o
, f in the non-conservative direction. The other three channels-were operable at'the' time and vould have
!provideda necessary triplof the reactor'if necessary.
s sTechnidal Specification ~1.3(8), Table 1.1, Item 8, F
Y
~ '
- andl Figure 1;2 applies.
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Monthly:OherationsReport; August 198,0.
Page Two-A'. -
PERFORMANCE CHARACTERISTICS'(Continued):
! LER Number
_ ' Deficiency -
LER-80-021:
Transformer (Th).of-DG-l' failed. This transformer feeds.the. control circuitry for the 15 kw diesel oilfimmersion heater as vell as supplying power to
' alarm relays for the following-items: low lube-
-oil pressure,Llow;1ube oil level, high and/or lov
, lube oil temperature,-water. temperature, water level and water' pressure. During the time of the transformer failure, DG-2:as well as the 161 ky-
/
and 345 kb cystems vere available and operable.,cIn
-addition, DG-1 was considered inoperable'only during
~ths. time that the transformer and associated-equip-e ment were being changed out, i.e. only while DG-1 was'in " Local' Maintenance".
LER-80-022
.During performance of ST-ESF-2, F.2-(B Safety
, Injection Actuation Signal ~ Surveillance Test) th'e -
86B/ VIAS
- lockout failed to trip due to a burnt coil. During the time of the incident, the
.86A/ VIAS *, the 86Al/ VIAS
- and'the 86B1/ VIAS
- vere operable and available.to initiate safeguards-equipment should the need arise.
" Ventilation Isolation Actuation Signal
.B.
CHANGES IN-OPERATING METHODS None
~
'C.
-RESULTS.OF SURVEILLANCE TESTS AND-INSPECTIONS-Surveillance tests as required by the' Technical Specifications -Section 3.0'and Appendix Bs. vere. performed in accordance with
~
the. annual surveillance test' schedule. The following is a
' summary:of the surveillance ; tests which results in Operations
~
-Incidents and.are not reported elsewhere in the report:
- Operations 1 y
- = Incident
..-Deficiency OI-1013< ~(ST-RPS-ll)
AD-1 Mdtrix' logic relay drop out lite 4
- remainsd / lit ' when hold. voltage was ' applied.
~
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?Mont'hly Operations Repol:t September 1980' 1
Page Three L.
CHANGES,. TESTS AND EXPERIMENTS CARRIED OUT WITHOUT COMMISSION D
APPROVAL' LProcedure Description
-SP-RPS-5.
- Excore Detector Symetric Offset Recalibration
~
- prior.to 1500 MWht/Results documented in procedure.
' DOR-79-180 Replacement of. Unqualified Transmitter in Loops 90r, 904,1109,1110/ Completed as designed.
DCR-79-148 Elimination of__ Turbine Trips Caused -by Battery Transients / Completed as designed.
E.
RESULTS OF-LEAK RATE TESTS ~
- No Leak Rate Tests were done during September.
F.
CHANGES IN PLANT GPERA.ING STAFF None G. -
TRAINING-Training for the month of' September included emergency procedures and sampling, new systems, Emergency Duty Officer.and fire brigade training for Operators. Safety' meetings and one hour a week train--
ing on supervisor selected topics for maintenance personnel.
" H.~
CHANGES, TESTS.AND EXPERIMENTS REQUIRING NUCLEAR REGULATORY COMMISSION AUTHORIZATION PURSUANT TO 10CFR50.59
.None-q!!lp Approved By
( L AQs-Fort Calhoun Station 1,
' MW f
)
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w-z LMhnthly: Operations Report LSeptember 1980i
.Pase'Four-II. MAIIITE3ANCE.(Significant Safety Related) s M. O.
Date Description Corrective Action-s
.6882
- 9'-2-80 Auxiliary Feedwater Setpoint.
Changed setpoints per CP-FWRS-A and CP-FWES-B.
13992
.'2-1-80 Aux. Bldg. HEPA Filters Changed filters 6828-8-20-80'-
SI-6D Magnatrol Lov Level Filled SI Tank Reference Legs
' Annunciator-on Level Instrument.
- 619h
.6-13-80
' Steam GeneratorsPressure Sigma.
Repaired meter failed.
6869-24-80 RMO-57 Pump von't run Rebuilt Pump
'h000= 1-80
Aux. Bldg. HEPA filters Changed filters
- 6158 6-20-80 DG-1 Exhaust System Leak Repaired Pipe
-6827 8-19-80
, Raw Water HCV-2879B will not open-Lubricate operator 70h0 9-80 "D"< Channel TU-3 Lov Flow pre-trip-Recalibrated trip unit
.setpoints.out of-specification.
f
.7018 9-6 RPS "D" Channel APD-Setpoints'out Rotated.svitches~and cleaned
- of Specification contacts.
16959 9 h 'RPS "AC" Matrix Relay Replaced AC-1 Relay and performed ST-RPS-11.
7017 9-5-80.
. RPS "D" Channel Trip Unit #3 front Replaced trip unit performed patch card connector Pin'#1-CP-RPS-3
~
672h' 9-8-80 WD-32 Analyzer leaks Inspected per procedure and
- repaired tubing leak.
l7065 9-11-80:
Lockout Relay 508 Replaced burned out relay
-.7057 9-10-80
' DG-1 Imersion Heater Transformer Replaced transformer
-7003 9-5-80 iRM_055 overboard Discharge in Cleaned RM-055
- alarm' l7032 9-8-80)
~ CPHS,86Al supervisory light Cleaned switches burned out 17.033-9-12-80 RCV-059 did close when RM-059'
- Repacked valve
_ packing too
-vas tripped:-
-tight.
ut.
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.2
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+
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Monthly; Operations Report.
~Sep.tember 1980
- Page Five '
- I; MAI:i'"ENA3CI'(Significant Safety Related) -
M. O. #
t Date-Description-Corrective Action l
- 7016 9-10-80.
CH-1B - New valves, ' valve seatis, '
. Completed per MP-CH-1-1 and pistons.-
T1611
- 9-22A80 ~
HCV-8814A: failed open-Replaced solenoid valve 1
'T142
'9-19-60' RRS "C" Channel TU-T calibrate Ccmpleted
-TA32' 9-18-80 LFP-1B Diesel Fire Pump runa hot Removed strainer-and. cleaned T
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