05000348/LER-1980-048-03, /03L-0:on 800817,containment Atmosphere Gaseous & Particulate Radioactivity Monitoring Sys Were Declared Inoperable Due to Pump Failure & Pump Trip on Low Flow. Caused by Pump Burnout & Sys Flow Maladjustment

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/03L-0:on 800817,containment Atmosphere Gaseous & Particulate Radioactivity Monitoring Sys Were Declared Inoperable Due to Pump Failure & Pump Trip on Low Flow. Caused by Pump Burnout & Sys Flow Maladjustment
ML19338D760
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 09/16/1980
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19338D754 List:
References
LER-80-048-03L, LER-80-48-3L, NUDOCS 8009230729
Download: ML19338D760 (1)


LER-1980-048, /03L-0:on 800817,containment Atmosphere Gaseous & Particulate Radioactivity Monitoring Sys Were Declared Inoperable Due to Pump Failure & Pump Trip on Low Flow. Caused by Pump Burnout & Sys Flow Maladjustment
Event date:
Report date:
3481980048R03 - NRC Website

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- EVENT DESCRIPTION AND PROSABLE CONSEQUENCES O'o o 2 lAt 1628 on 8-17-80, 1730 on 8-17-80 and 1530 on 8-18-80, the containment atm'osphere g [ particulate and gaseous radioact'ivity monitoring systems (R11 and R12 respectively) were]

gdeclared inoperable due to. pump failure (.lst and 2nd occurrence) and pump trio on low o 4 g

g g low *(3rd occurrence). Tech. Spec. 3.4.6.1, in part, requires R11 and R12 to be operabig f

[ Tech. Spec. 3.4.6.1 action statement requirements were met. 3imilar occurrence reported, o 3 g gin LER 78/037-03L-0. Following corrective action R11 and R12 were returned.to, service y

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