ML19338D760

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LER 80-048/03L-0:on 800817,containment Atmosphere Gaseous & Particulate Radioactivity Monitoring Sys Were Declared Inoperable Due to Pump Failure & Pump Trip on Low Flow. Caused by Pump Burnout & Sys Flow Maladjustment
ML19338D760
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 09/16/1980
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19338D754 List:
References
LER-80-048-03L, LER-80-48-3L, NUDOCS 8009230729
Download: ML19338D760 (1)


Text

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- EVENT DESCRIPTION AND PROSABLE CONSEQUENCES O'o o 2 lAt 1628 on 8-17-80, 1730 on 8-17-80 and 1530 on 8-18-80, the containment atm'osphere .;

g [ particulate and gaseous radioact'ivity monitoring systems (R11 and R12 respectively) were]

o 4 gdeclared inoperable due to. pump failure (.lst and 2nd occurrence) and pump trio on low g g g lowf *(3rd occurrence) . Tech. Spec. 3.4.6.1, in part, requires R11 and R12 to be operabig o 3 [ Tech. Spec. 3.4.6.1 action statement requirements were met. 3imilar occurrence reported, g gin LER 78/037-03L-0. Following corrective action R11 and R12 were returned.to, service y g 1650 on 8-17-80, 2315 on 8-17-80 and 2115 on 8-18-80. Health /sAfetyofthepublic 2 s swas not arrected.

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  • 8009230729 .