ML19331B870

From kanterella
Jump to navigation Jump to search
LER 80-039/03L-0:on 800715,Train a Delcared Inoperable When R.W.Pump 8 Tripped & Could Not Be Restarted.Caused by Actuation of Breakers HEA86 Lockout Relay.Relay Reset & Pump Returned to Svc
ML19331B870
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 08/08/1980
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19331B868 List:
References
LER-80-039-03L, LER-80-39-3L, NUDOCS 8008130456
Download: ML19331B870 (1)


Text

_

LICENSEEi EVENT REPORT -

co=rna. stocx: 1 I I I I I l@ iPtEAsE Pa:Nr oa rvPE 4u. nEnuinto:wcamariem o i 3

con T s9 l Al tl al ni rl il@l o I o I- 10 lo lo 1010 26l-, uGEh5E UCENSEE CQoE B4 IS uGENSE NuveER *$ h loTYPE l@l JG 4l IlI 1ll 111[

bl GAT 54 @

MJ 1*R E

8 l L @ l 01 31 0l 01 0 13St l4 l8 @ l0 [7 il 15 l8 l0 l@lOl8l0l 60 El CoCM ET NUMSEM 6d EVENT C ATE 78 7S REPORT DA TE 80 Q l_ EVENT At 0400DESCRIPrlON on 7/15/80. river water (R.W.)

AND PROSA8LE CONSEQUENCES h Train A was declared 2ncoerable when it was  ;

g g noted that R.W. Pu:.9 No. 8 was tripped and could not be re<:2r ed.

(R.W. Pump No. 10 g g [ was out of service for maintenance.) Tech. Spec. 3.7.5 reauires both R.W. tra' ins.to g g [ be operable. Tech. Spec. 3.7.5 action statement requiremen:s were raet. Health and g

,0 6 l safety Cf the public were not affect &d.

I o 1 l '

I r

O a se L *

" I O 9 Yo'E TS suscSE covPoNENT COOE s OC'E so 7 s lW lE lh dh Wh lR lE lL IA h lN l h W hSt yoE h 9 30 11 12 13 14 19 20 LE EVENTvEAR sEouENTIAL REronTNo. CCCURRENCE REPCMT REVis10N

@ ,as=R'ROu [81ol l20 _] 1013191 1/l cCOE Iol31 TYPE NO.

28 22 24 I t. 1 [-j N A 26 24 IS 23 33 31 LOJ 04 o PLA T 32 IE HOURS

sg FOR 8. SUP Li Ld@J4L2J@ L1J@

3J L2J@ 10 I0 lo lo I L;.ij@ MAN FC RER 25 36 31 40 4 l4;': l@ la'@ Icl01810l@

A3 44 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h ' 4; Q l R.W. Train A could not be started due to the actuation of the break g [ relay.

g The breakers protective relay " targets" were checked and no cause could be I

g g determined for the lockout relay actuation.

The relay was raset and the pump was  ;

g l returned to service at 0423 on 7/15/80'.

1 i A t I 8 9 i

' r*A%7 sPowEn 80 oTNEnsTATus @$$sEoNEv'

@ [(Elh l1lolOlhl A VITY CC TENT NA l [ hlon+ n ,r M ervationoiscovEnYoEscRirTroN @

l KELEAsED OF RELE AsE AA40UNT CP ACTIVITY

, E izJ I 8 9 @ L1J@l 80 ti n i I u LOCATION OF RELEASE PERsCNNEL E**05UREs 44 45 I NUW3ER TYPE O EsCRIPTION - sa E 1010

' ' ' I o Gl z l@!

NA PERscNyd'mu',I.Es l NuveER **

oEscRiPTroN@

@ s9 7 {0}010l@l in 2 XA mq% ,,,

LCss 08 CR cauact To FAs LITY 4 l

TYPE CEsRiP fsome Ih jy ] 80 E,.,tzJet I i

_ Na

- 1

^

I d l yd ha I

    • "[s'cR,,

o Tion h ..

>8 ssv)E!.Eeo 81 NA Nec usE ontv ,

. io NAME ^

I

.: es I I ll Ill i I I I fa;li PMEPARER

  • E0"'

8008'130 _

PHONE:

. _.