05000348/LER-1980-039-03, /03L-0:on 800715,Train a Delcared Inoperable When R.W.Pump 8 Tripped & Could Not Be Restarted.Caused by Actuation of Breakers HEA86 Lockout Relay.Relay Reset & Pump Returned to Svc

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/03L-0:on 800715,Train a Delcared Inoperable When R.W.Pump 8 Tripped & Could Not Be Restarted.Caused by Actuation of Breakers HEA86 Lockout Relay.Relay Reset & Pump Returned to Svc
ML19331B870
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 08/08/1980
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19331B868 List:
References
LER-80-039-03L, LER-80-39-3L, NUDOCS 8008130456
Download: ML19331B870 (1)


LER-1980-039, /03L-0:on 800715,Train a Delcared Inoperable When R.W.Pump 8 Tripped & Could Not Be Restarted.Caused by Actuation of Breakers HEA86 Lockout Relay.Relay Reset & Pump Returned to Svc
Event date:
Report date:
3481980039R03 - NRC Website

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60 El CoCM ET NUMSEM 6d St EVENT C ATE 78 7S EVENT DESCRIPrlON AND PROSA8LE CONSEQUENCES h REPORT DA TE 80 Q l_ At 0400 on 7/15/80. river water (R.W.) Train A was declared 2ncoerable when it was g g noted that R.W. Pu:.9 No. 8 was tripped and could not be re<:2r ed.

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